IR 05000315/2019010

From kanterella
Jump to navigation Jump to search
Biennial Problem Identification and Resolution Inspection Report 05000315/2019010 and 05000316/2019010
ML19240A296
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/28/2019
From: Eric Duncan
Reactor Projects Region 3 Branch 4
To: Gebbie J
Indiana & Michigan Electric Co
References
IR 2019010
Download: ML19240A296 (16)


Text

August 28, 2019

SUBJECT:

DONALD C. COOK NUCLEAR PLANT, UNITS 1 AND 2BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000315/2019010 AND 05000316/2019010

Dear Mr. Gebbie:

On August 1, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at D.C. Cook Units 1 and 2 and discussed the results of this inspection with Mr. J. Petro, Managing Director of Engineering, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

The NRC inspectors documented one finding of very low safety significance (Green) in this report. The finding did not involve a violation of NRC requirements.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at D.C. Cook. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Eric R. Duncan, Chief Branch 4 Division of Reactor Projects

Docket Nos. 05000315 and 05000316 License Nos. DPR-58 and DPR-74

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000315 and 05000316

License Numbers:

DPR-58 and DPR-74

Report Numbers:

05000315/2019010 and 05000316/2019010

Enterprise Identifier: I-2019-010-0046

Licensee:

Indiana Michigan Power Company

Facility:

Donald C. Cook Nuclear Plant, Units 1 and 2

Location:

Bridgman, MI

Inspection Dates:

July 15, 2019 to August 01, 2019

Inspectors:

G. Hausman, Senior Reactor Inspector

J. Mancuso, Resident Inspector

J. Neurauter, Senior Reactor Inspector

J. Winslow, Resident Inspector

Approved By:

Eric R. Duncan, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at the Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process.

The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Unit 1 Steam Dump Valves Inadvertently Failed Open Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000315/2019010-01 Open/Closed

[H.14] -

Conservative Bias 71152B A self-revealed Green finding was identified when the licensee failed to ensure that all design specifications for the Unit 1 Alarm Log Computer (ALPC) associated with a reactor controls and instrumentation (RCI) system engineering change were met. Specifically, the licensee failed to ensure a design specification that the engineering workstation shall not include the capability for direct control functions was met when an engineer opened an ALPC human machine interface display screen on the system's Unit 1 engineering workstation and the steam dump valves re-positioned to 75 percent open.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the effectiveness of the corrective action program (CAP) in identifying, prioritizing, evaluating, and correcting problems.
  • Operating Experience, Self-Assessments, and Audits: The inspectors assessed the effectiveness of the stations processes for the use of operating experience, audits, and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs used to establish and maintain a safety conscious work environment.

INSPECTION RESULTS

Assessment 71152B Corrective Action Program: Based on the samples reviewed, the inspectors determined that the licensee's performance in the areas of problem identification and the implementation of the process for prioritizing and evaluating these problems adequately supported nuclear safety.

The inspectors performed reviews of the essential service water system and the auxiliary feedwater system. Additionally, the inspectors performed an expanded 5 year review of the emergency diesel generator system. As part of these reviews, the inspectors conducted system walkdowns and evaluated condition reports, engineering changes, and work orders. Interviews with licensee staff were also conducted as part of the reviews.

The inspectors identified a weakness in the effectiveness of corrective actions taken to resolve an issue documented in the CAP. A minor violation of 10 CFR 50, Appendix B, Criterion V was identified when the inspectors reviewed the corrective actions and effectiveness reviews for AR 2018-1045 associated with a root cause evaluation in the Security Department. This minor violation is documented in this inspection report.

Operating Experience and Self-Assessments and Audits: Based on the samples reviewed, the inspectors determined that the licensee's performance in each of these areas adequately supported nuclear safety.

The inspectors concluded that the licensee was generally effective in the use of operating experience in the CAP. When performing causal analyses and determining corrective actions, the inspectors determined that operating experience was routinely utilized and reviews were completed in accordance with licensee procedures. In addition, the team sampled operating experience from the NRC, industry, vendors, and third party groups and determined that for the samples selected that appropriate assessments for applicability to the licensee were performed.

The inspectors also reviewed licensee self-assessments and audits. The inspectors determined that the licensee was adequately performing self-assessments and audits in accordance with licensee procedures and implementing corrective actions as needed.

Safety Conscious Work Environment: The inspectors found no evidence of challenges to the licensee's safety conscious work environment (SCWE).

The licensee's employees appeared willing to raise nuclear safety concerns through at least one of several means available. The inspectors observed various station meetings, including those in which new CAP items were reviewed, and interviewed a representative cross-section of station personnel.

Additionally, the inspectors assessed the overall health of the Employee Concerns Program.

Specifically, the inspectors interviewed the Employee Concerns Program Manager, reviewed recent case logs and case files, and considered statements received during interviews with station personnel.

Unit 1 Steam Dump Valves Inadvertently Failed Open Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events

Green FIN 05000315/2019010-01 Open/Closed

[H.14] -

Conservative Bias 71152B A self-revealed Green finding was identified when the licensee failed to ensure that all design specifications for the Unit 1 Alarm Log Computer (ALPC) associated with a reactor controls and instrumentation (RCI) system engineering change were met. Specifically, the licensee failed to ensure a design specification that the engineering workstation shall not include the capability for direct control functions was met when an engineer opened an ALPC human machine interface display screen on the system's Unit 1 engineering workstation and the steam dump valves re-positioned to 75 percent open.

Description:

On May 7, 2019, with Unit 1 in Mode 3, and during RCI troubleshooting activities at the engineering workstation for the RCI system, the Unit 1 Group 1 steam dump valves unexpectedly re-positioned to 75 percent open as indicated on the Reactor Operator ALPC.

A licensee cause evaluation subsequently determined that during the troubleshooting activities that were in progress at the time of the event, an ALPC human machine interface display screen on the RCI system's engineering workstation that was opened as part of the troubleshooting activities caused an inadvertent demand signal to be sent to the Unit 1 steam dump valves, which caused the valves to re-position to 75 percent open. The licensee determined that software files stored on the engineering work station to support testing for a recently installed RCI system change were not removed and, as a result, the steam dump valves re-positioned when the engineering workstation was opened. This was contrary to the design specifications for the RCI engineering change, which stated that the engineering workstation shall not include the capability for direct control functions.

Corrective Actions: As a part of their immediate corrective actions, operators placed the steam dump control selector switches to off and ensured that the Unit 1 Group 1 steam dump valves re-positioned closed. Additionally, the licensee deleted the ALPC software files that resulted in the unexpected demand signal from the Unit 1 engineering workstation and performed an extent of condition review on Unit 2.

Corrective Action References: AR 2019-4970, Unit 1 Steam Dumps Failed Open

Performance Assessment:

Performance Deficiency: The licensee failed to ensure that all design specifications for the ALPC associated with an RCI system modification were met. Specifically, the licensee failed to comply with a design specification that the engineering workstation shall not include the capability for direct control functions, which was identified during troubleshooting by an engineer using the RCI system's engineering workstation when the steam dumps unexpectedly re-positioned to 75 percent open.

Screening: The inspectors determined the performance deficiency was more than minor because if left uncorrected, it would have the potential to lead to a more significant safety concern. Specifically, the inadvertent opening of the steam dump valves in Mode 3 caused a Reactor Coolant System pressure and temperature transient. However, if left uncorrected, when operating in Mode 1 the inadvertent opening of the steam dump valves could cause a significant power transient which would affect the Initiating Events cornerstone objective of limiting the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors answered No to all the Transient Initiators questions in Exhibit 1, Initiating Events Screening Questions. Therefore, the finding screened as having very low safety significance (i.e.,

Green).

Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. Specifically, in this instance, the licensee did not ensure that factory acceptance testing and post modification testing for the engineering workstation associated with the RCI system engineering change positively validated the design specification that the engineering workstation not include the capability for control functions. As a result, the licensee was unaware that the RCI system's engineering workstation could perform direct control functions due to the ALPC software files being located on the engineering workstation.

Enforcement:

The inspectors did not identify a violation of regulatory requirements associated with this finding.

Minor Violation 71152B Minor Violation: The inspectors reviewed AR 2018-1045 associated with a root cause evaluation in the Security Department. During the review, the inspectors identified that one of the corrective actions to prevent recurrence (CAPRs) associated with the supervisory review of electronic logs was not being performed as written. Specifically, the Corrective Action Review Board (CARB) approved CAPR 2018-1045-28 to, Establish a requirement for Security supervision to perform a shiftly review of new electronic logs. The inspectors, however, identified that Security supervision was only reviewing a portion of the new electronic logs shiftly, and not performing a full review of electronic logs shiftly as directed by the CAPR. Licensee procedure PMP-7030-CAP-002, Condition Action and Closure, Step 3.3, states, in part, that CARB concurrence is required for the following:...CAPR approvals; CAPR modifications; and making any changes to an open CAPR assignment that has been previously reviewed and concurred with by CARB. However, CAPR 2018-1045-28, which was a CAPR assignment that had been previously reviewed and concurred with by CARB, was modified by Security supervision to only review a portion of the new electronic log shiftly without CARB approval. The inspectors identified this as a minor violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings. This issue was documented in the licensee's CAP as AR 2019-7109.

Screening: The inspectors determined the performance deficiency was minor. Consistent with the guidance in IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, the inspectors determined that the performance deficiency was not a finding of more than minor significance based on answering 'No' to all of the more-than-minor screening questions. The inspectors also reviewed the examples of minor issues in IMC 0612, Appendix E, Examples of Minor Issues, and determined that this issue was most closely related to Example 4.a in that that this was a procedural error that had no safety impact.

Enforcement:

This failure to comply with 10 CFR 50, Appendix B, Criterion V constituted a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On August 1, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Mr. J. Petro, Managing Director of Engineering, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Calculations

SD-180731-001

Component Cooling Water (CCW) System Heat Exchanger

(HE-15E/W) Tube Flaw Structural Evaluation

Corrective Action

Documents

AR 00863160

Inadequate Evaluation on NSAL-00-009

01/07/2010

AR 2010-3656

1-ABD-B-3D Breaker Tripped Open When Pump Auto

Started

10/14/2010

AR 2013-1347

Fuel Injector Pump Spraying Fuel Oil on Diesel Surveillance

07/18/2014

AR 2013-6194

Reserve Feed Tripped Due to a Fault

06/19/2014

AR 2014-15099

Identified Pin Hole Leak in 2-HV-AFP-EAC Essential Service

Water Piping

2/02/2014

AR 2014-9231

AutoPIPE - Time History Error

08/06/2014

AR 2014-9877

Foreign Material Exclusion Cover Installed on AB Diesel

Generator Vent Caused Indicator Problems

2/19/2016

AR 2015-14015

Bentley Software STAAD.Pro Has Critical Errors

10/28/2015

AR 2015-14961

Inability of Component Cooling Water System to Supply

Make Up

11/17/2015

AR 2015-6917

Unit 1 AB Emergency Diesel Generator Tripped During Post

Maintenance Testing Run

2/24/2017

AR 2015-8935

PAA 15-05-01 Interface Between Design Engineering and

Procurement Engineering

07/10/2015

AR 2015-8935-46

Evaluate Change Management Plan Effectiveness

06/01/2017

AR 2015-8935-47

Final Effectiveness Review Based Upon Revised Change

Management Plan

06/12/2017

AR 2016-13049

Unit 2 CD Emergency Diesel Generator Essential Service

Water Supply Line Pipe Degradation

11/10/2016

AR 2016-14625-

Interim Effectiveness Review - Emergency Diesel Generator

Delivery Valve Holder

11/03/2017

AR 2016-14625-

Perform Final Effectiveness Review - Emergency Diesel

Generator Delivery Valve Holder

2/13/2017

AR 2016-8003

Unit 1 CD Emergency Diesel Generator Seized Fuel Injection

Pump Failure Analysis

05/24/2017

AR 2017-13059

U1 TDAFP Failed Surveillance, Failed to Reach Rated

Speed

2/21/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 2017-1330

AREOR 2015 Contained Documentation Errors

2/02/2017

AR 2017-2597

Primary Water Does Not Meet Operating Basis Earthquake

Design Requirements

03/06/2017

AR 2017-3227

Commercial Grade Part Installed on Safety Related

Component

03/24/2017

AR 2017-3711

Declining Performance Trend of CAP Quality

04/10/2017

AR 2017-4629

Part 21 Relay Found in 1-CD Emergency Diesel Generator

OME-150-CD Inverter

06/13/2017

AR 2017-5836

Unit 2 Containment Spray Additive Tank Percent Sodium

Hydroxide Below Administration Limit

06/12/2017

AR 2017-6217

Compensatory Action Will Not Supply Adequate Flow for

CCW Makeup

06/22/2017

AR 2017-6571

U1 EMDAFP Outboard Bearing Housing Cap Missing Gasket

07/06/2017

AR 2017-7002

NCV 2017-007-01: EDC Procedure Provides Incorrect

Guidance

07/21/2017

AR 2017-7015

NCV 2017-007-01: Operability Evaluation Performed for AR

00863160

07/21/2017

AR 2017-7192

Worker Entered Radiologically Controlled Area Without

Radiation Work Permit or Self-Reading Dosimeter

07/25/2017

AR 2017-7211

NCV 2017-007-01: Timely Resolution of Potentially Non-

Conforming/Degraded Issues

07/27/2017

AR 2017-8605

Material Grade Change Not Captured in Impact Review for

Engineering Changes

09/08/2017

AR 2017-8607

Seismic and Piping Calculations Do Not Match Installation

Engineering Change

09/08/2017

AR 2017-8921

1-MDFPX2B Relay Failed Testing

09/16/2017

AR 2017-9683

Insufficient Maintenance of Safety Related Components

09/29/2017

AR 2018-0634

Unit 1 Letdown Safety Lifted While Removing Letdown

Orifice

05/23/2018

AR 2018-10405

Discrepancy between Design and UFSAR Damping Values

11/14/2018

AR 2018-10443

Commercial Grade Dedication Deficiency

11/15/2018

AR 2018-1045

Root Cause Evaluation in Security Department

01/31/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 2018-3506

Radiation Protection Did Not Verify Dose Rates for Unit 1

CLV Work

03/27/2018

AR 2018-6917

Potential Commonality in Recent Repeat Events

07/05/2018

AR 2018-7570

Component Cooling Water to Essential Service Water Leak

Identified on Unit 1 East Component Cooling Water Heat

Exchanger

07/27/2018

AR 2018-8046

Unsupported 1 Safety Injection Line at 1-GSI-R509

08/13/2018

AR 2018-9481

High Steam Generator Sodium Concentration in Unit 2

10/09/2018

AR 2019-1165

Staff Did Not Fully Correct Identified Condition

2/05/2019

AR 2019-1409

Issue with Effectiveness Review Performed in 2016-2026-18

2/13/2019

AR 2019-1677

Problem Identification and Resolution Self-Assessment

Finding

2/21/2019

AR 2019-1680

Problem Identification and Resolution Self-Assessment

Finding

2/21/2019

AR 2019-1681

Problem Identification and Resolution Self-Assessment

Finding

2/21/2019

AR 2019-3227

Degraded Concrete Pier in Unit 1 Forebay

03/28/2019

AR 2019-3285

Potential Issue Identified with Corrective Actions

03/29/2019

AR 2019-3770

Water Leaking from 1-HV-AFP-T2AC, TDAFP Room Cooler

04/12/2019

AR 2019-4188

1-HV-AFP-T2AC Piping Leak

04/21/2019

AR 2019-4968

Steam Dump Controller Failed

05/07/2019

AR 2019-4970

Unit 1 Steam Dumps Failed Open

05/07/2019

AR 2019-5396

N-44 Was Declared Inoperable

07/13/2019

AR 2019-5469

1-WRV-772 and 1-WRV-762 Failed Full Stroke on Backup

Air

05/22/2019

AR 2019-6920

1AB Emergency Diesel Generator Assumed Load After

Divorcing from T11A Bus

07/16/2019

GT 2017-9541

RA-NRC Bulletin Gap Analysis

09/27/2017

GT 2018-0355

Evaluate EN 53151 Defect in Thermostatic Valve Assemblies

01/11/2018

GT 2018-10826

High Pressure Coolant Injection Inboard Steam Valve Failure

2/03/2018

GT 2018-4488

Enhancements to 12-EHP-4030-056-218

10/17/2018

GT 2019-5044

Refuel Platform Hoist Failure During Fuel Movement

05/09/2019

Corrective Action

AR 2019-6942

Logs were Not Completed or Identified

07/17/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Resulting from

Inspection

AR 2019-7109

Procedure Step Was Not Implemented as Intended

07/22/2019

AR 2019-7471

Deficiencies in AR 2015-14015 - STAAD.Pro Critical Errors

08/01/2019

Engineering

Changes

EC 52453

Unit 1 - Reactor Controls Instrumentation System Upgrade

EC 55754

Install Mechanical Jumper

06/25/2018

Miscellaneous

Management Screening Committee Agenda

Various

Daily Screened Actions

Various

Operating Experience Screening Committee Agenda

07/18/2019

Nuclear Safety Culture Assessment Summary

05/19/2017

Corrective Action Review Board (CARB)

Various

50.59 Evaluation

2015-0479-01

2-TM-15-49-R2: Compensatory Action in Support of

Component Cooling Water Passive Failure

11/25/2015

50.59 Screen

2015-0479-01

2-TM-15-49-R2: Compensatory Action in Support of

Component Cooling Water Passive Failure

11/24/2015

50.59 Screen

2017-0331-00

EC 55754: Compensatory Action in Support of Component

Cooling Water Failure

10/27/2017

FCR 55461-006

Field Change Request: Modification and Addition of Supports

Located on 3 Inch Primary Water Piping (EC 55461 HC

Revision 0)

LER 315/2010-

001-00

AB Emergency Diesel Generator Fuel Oil Transfer Pumps

Inoperable

06/18/2010

LER 315/2013-

2-00

System Actuation of the Unit 1 CD Emergency Diesel

Generator

06/24/2013

LER 315/2014-

2-00

Non-Compliance with LCO 3.8.1 During Surveillance

Preparations

10/20/2014

LER 315/2015-

001-00

Plant Shutdown Required by Technical Specifications

07/29/2015

LER 316/2005-

001-00

Reactor Trip from RCP Bus Under-Voltage Signal

Complicated by Diesel Generator Output Breaker Failure

01/09/2006

LER 316/2016-

2-00

Emergency Diesel Generators Declared Inoperable Due to a

Manufacturing Design Issue

2/09/2017

LER 316/2018-

001-00

Valid Actuation of the Unit 2 CD Emergency Diesel

Generator During Testing

06/04/2018

NEI 16-07

Technical Report - Improving the Effectiveness of Issue

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Resolution to Enhance Safety and Efficiency

NEI Efficiency

Bulletin: 17-14

Improving the Effectiveness of Issue Resolution to Enhance

Safety and Reliability

ODMI 1-18-001

Component Cooling Water Leakage Trending

05/01/2019

Operability

Evaluations

AR 2018-3803-1

Increasing Trend in Vibrations and Noise on 1-PP-7E

Essential Service Water

04/08/2018

AR 2018-7570-1

Component Cooling Water to Essential Service Water Leak

Identified on Unit 1 East Component Cooling Water Heat

Exchanger

08/02/2018

Procedures

1-OHP-4021-003-

001

Letdown, Charging and Seal Water Operation

1-OHP-4024-122

Annunciator #122 Response: Plant Service

1-OHP-4024-130

Annunciator #130 Response: Makeup Water System

2-EHP-5043-

CGD-001

Commercial Grade Dedication

2-EHP-5043-

EDC-001

Evaluation of Degraded/Non-Conforming Conditions

2-EHP-5043-

ERP-001

Engineering Review of Procurement Documents

2-OHP-5030-

016-001

Supplying Essential Service Water to Component Cooling

Water for Makeup Using a Temporary Modification

2-THP-6010-

RPP-006

Radiation Permit (RWP) Processing

2-THP-6010-

RPP-104

Personnel Dosimetry Use in Varying Radiation Fields

2-THP-6010-

RPP-401

Performance of Radiation and Contamination Surveys

2-THP-6010-

RPP-407

Special Radiological Evolutions

2-THP-6020-

CHM-309

Make-Up Plant

2-OHP-4024-222

Annunciator #222 Response: Plant Service

DTG-EQR-003

System Health Report

DTG-NCAP-001

Processing Non-Corrective Action Program Actions

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ECP Desktop

Guideline

Employee Concerns Program

PMI-2015

Policy for Maintaining A Safety Conscious Work Environment

PMI-7030

Corrective Action Program

PMI-7034

Self-Assessment and Bench-Marking Programs

PMP-7030-CAP-

2

Condition Action and Closure

PMP-7030-CAP-

004

Conduct of Effectiveness Reviews

PMP-7030-CAP-

005

Conduct of Causal Evaluations

PMP-7030-MOP-

001

Corrective Action Program Management Oversight Process

PMP-7034-SAP-

001

Conduct of Self Assessments

SPP-2060-SFI-

106

Security Conduct of Operations

Self-Assessments

System Health Report: Essential Service Water - Unit 1

Q2 - 2018

System Health Report: Essential Service Water - Unit 1

Q4 - 2018

System Health Report: Essential Service Water - Unit 2

Q2 - 2018

System Health Report: Essential Service Water - Unit 2

Q4 - 2018

GT 2017-0614

Measuring & Test Equipment Quick Hit Self-Assessment

11/14/2017

GT 2017-0651

Equipment Status Control Quick Hit Self Assessment

11/20/2017

GT 2018-0493

Chemistry Primary Water System Quick Hit Self-Assessment

11/13/2018

GT 2018-0497

Conduct of Chemistry Quick Hit Self-Assessment

03/05/2019

GT 2018-0500

Management of Non-Conforming Conditions Quick Hit Self-

Assessment

04/24/2019

GT 2018-0947

Measuring & Test Equipment Quick Hit Self-Assessment

01/14/2019

GT 2018-0966

Operations Decision Making Quick Hit Self Assessment

11/13/2018

GT 2018-10453

NRC Inspection Full Self Assessment - PI&R

11/15/2018

GT 2018-11397

Behaviors Excellence Plan Effectiveness

05/01/2019

GT 2018-1678

Radiological Hazard Assessment and Exposure Controls, In-

Plant Radioactivity Control and Mitigation, and Occupational

04/02/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Dose Assessment Full Self-Assessment

GT 2018-2898

Exam Administration and Evaluation Methods Quick Hit Self

Assessment (Rhew)

2/20/2018

GT 2018-4227

Standard Design Process - Expectations for Effective Design

Changes Quick Hit Self-Assessment

2/20/2018

NOS-17-06

Nuclear Oversight Audit: Corrective Action Program

07/13/2017

NOS-17-10

Nuclear Oversight Audit: Engineering, Design Control, and

Inservice Inspection/Inservice Testing

11/16/2017

NOS-18-01

Nuclear Oversight Audit: Radiological Environmental

Monitoring Program (REMP)/Process Control Program

2/15/2018

NOS-19-01

Nuclear Oversight Audit: Radiological Environmental

Monitoring Program/Off-site Dose Calculation Manual

03/18/2019

NOS-19-05

Nuclear Oversight Audit: Corrective Action Program

07/30/2019

Work Orders

WO 55405314

Perform Ultrasonic Test on Piping Downstream of 2-WHO-

718 Heat Exchanger

10/13/2016

WO 55481604

MTM, 1-HE-15E, Inspect for Tube Leaks, Install Tube Plugs

05/30/2019

WO 55492331

Perform License Renewal Activity: System Engineer

Walkdown - Unit 2 Essential Service Water System

03/12/2018

WO 55502751

1-WPX-731-V1, EC-55711, Replace Valve & Upstream

Piping

09/22/2017

WO 55502754

1-WPX-735-V1, EC-55711, Replace Valve & Upstream

Piping

09/20/2017

WO 55503076

2-WPX-736-V1, Replace Valve EC-55895

04/18/2018

WO 55503077

2-WPX-732-V1, Replace with 2 Valve/Piping EC-55895

04/05/2018

WO 55503450

Install Pipe Supports 12-APW-R4002, R4003, R4004

2/05/2019

WO 55506808

Unit 1 CCW Cross Tie Valve Seat Leak Test

11/04/2017

WO 55506809

Unit 2 CCW Cross Tie Valve Seat Leak Test

04/12/2018

WO 55510794

Perform License Renewal Activity: System Engineer

Walkdown - Unit 1 Essential Service Water System

03/22/2019