IR 05000315/2019002
| ML19214A137 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 08/01/2019 |
| From: | Eric Duncan Reactor Projects Region 3 Branch 4 |
| To: | Gebbie J Indiana Michigan Power Co |
| References | |
| IR 2019002 | |
| Preceding documents: |
|
| Download: ML19214A137 (22) | |
Text
August 1, 2019
SUBJECT:
DONALD C. COOK NUCLEAR PLANT, UNITS 1 AND 2INTEGRATED INSPECTION REPORT 05000315/2019002 AND 05000316/2019002
Dear Mr. Gebbie:
On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Donald C. Cook Nuclear Plant, Units 1 and 2. On July 23, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at D.C. Cook. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Eric R. Duncan, Chief Branch 4 Division of Reactor Projects
Docket Nos. 05000315 and 05000316 License Nos. DPR-58 and DPR-74
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000315 and 05000316
License Numbers:
Report Numbers:
05000315/2019002 and 05000316/2019002
Enterprise Identifier: I-2019-002-0069
Licensee:
Indiana Michigan Power Company
Facility:
Donald C. Cook Nuclear Plant, Units 1 and 2
Location:
Bridgman, MI
Inspection Dates:
April 01, 2019 to June 30, 2019
Inspectors:
J. Ellegood, Senior Resident Inspector
T. Go, Health Physicist
J. Mancuso, Resident Inspector
R. Ruiz, Project Engineer
J. Rutkowski, Project Engineer
Approved By:
Eric R. Duncan, Chief
Branch 4
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Failure to Develop Procedures for Loss of Electrical Bus Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000315,05000316/2019002-01 Open/Closed None (NPP)71152 The inspectors identified a finding of very low safety significance and an associated non-cited violation (NCV) of TS 5.4.1.a when licensee personnel failed to have established procedures for the operation of the electrical distribution system as well as procedures for combating emergencies and other significant events, including a loss of electrical power to safety-related electrical Bus 21B. Because these procedures had not been established, the restoration of safety-related Bus 21B was delayed following a May 17, 2019, electrical fault in the 2-ABD-B switchgear.
Additional Tracking Items
Type Issue Number Title Report Section Status URI 05000315,05000316/
2018010-01 Record Retention Requirements of the Boron Injection Tank and its Associated Support Structure 71111.21M Closed
PLANT STATUS
Unit 1 began the inspection period shutdown and defueled for a refueling outage. On May 8, 2019, the licensee restarted Unit 1 and commenced power ascension. Unit 1 was subsequently held at about 50 percent power to address an East Main Feed Pump issue. On May 18, 2019, the licensee completed repairs to the East Main Feed Pump and resumed power ascension. On May 20, 2019, Unit 1 reached full power and remained at or near full power for the remainder of the inspection period.
Unit 2 operated at or near full power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Summer Readiness Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated the summer readiness of offsite and alternate Alternating Current (AC) power systems
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 AB 250 Volt Direct Current (VDC) Battery prior to CD 250 VDC Battery cell replacement, on June 6, 2019
- (2) Supplemental Diesel Generators following maintenance on June 6, 2019
71111.05A - Fire Protection (Annual)
Annual Inspection (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated fire brigade performance on June 20, 2019
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (4 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Unit 1 4 Kilovolt (kV) Switchgear Rooms on May 29, 2019
- (2) Unit 1 AB and CD 250 VDC Battery Rooms on May 29, 2019
- (3) Unit 2 4KV Switchgear Rooms on May 29, 2019
- (4) Unit 2 AB and CD 250 VDC Battery Rooms on May 29, 2019
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the main control room during plant heatup and restart from a refueling outage on May 8, 2019
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance during requalification training in the simulator on June 18, 2019
71111.12 - Maintenance Effectiveness
Quality Control (IP Section 02.02) (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:
- (1) Switchgear 2-ABD-B Bus Bar Replacement
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 2 250 VDC systems
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 2 600V Bus 21B recovery on May 18 and 19, 2019
- (2) Emergent Unit 2 CD 250 VDC battery cell replacement on June 6, 2019
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (3 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 1 11 Reactor Coolant Pump (RCP) Seismic Support Gap Out of Specification
- (2) Unit 1 Aggregate Operability Determination
- (3) Unit 2 Pressurizer Pressure Oscillations Due to Spray Valve Opening Intermittently
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
- (1) Unit 1 West Centrifugal Charging Pump Power Cable Replacement
71111.19 - Post-Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance tests:
- (1) Unit 1 Reactor Control and Instrumentation (RC&I) return to service testing following upgrade during Refueling Outage (RFO) U1C29
- (2) Unit 1 Solid State Protection System (SSPS) return to service testing following upgrade during RFO U1C29
- (3) Unit 1 Reactor Vessel V3 examinations following work during RFO U1C29
- (4) Unit 1 Upper Cavity inspections and Foreign Material Exclusion (FME) retrieval following work during RFO U1C29
- (5) U1 Fuel Upender following repairs during RFO U1C29
- (6) Unit 1 Reactor Coolant Pump (RCP) lateral bumper repair
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated RFO U1C29
===71111.21M - Design Bases Assurance Inspection (Teams)
The inspectors completed their review of Unresolved Item (URI)05000315/2018010-01; 05000316/2018010-01; Record Retention Requirements of the Boron Injection Tank. The review and closure of this URI did not constitute an inspection sample.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Inservice Testing (IP Section 03.01)
- (1) Unit 2 IHP-4030-228-005B, Train B Containment Equalization Fan Surveillance Testing, on June 20, 2019
Surveillance Tests (other) (IP Section 03.01)===
- (1) Unit 1 Low Power Physics Testing on May 8, 2019
- (2) Unit 1 Turbine-Driven Auxiliary Feedwater Testing on May 7, 2019
- (3) Unit 1 IHP-4030-151-010, Steam Generators 2 and 3 Steam Pressure Protection Set 3 Channel Operational Test and Calibration, on June 18,
RADIATION SAFETY
71124.03 - In-Plant Airborne Radioactivity Control and Mitigation
Engineering Controls (IP Section 02.01) (1 Sample)
The inspectors evaluated airborne controls and radioactive monitoring.
- (1) Installed Ventilation Systems:
- 2HV-AES-2; Auxiliary Building Ventilation Engineered Safety Feature Exhaust Fan #2
- 12-HV-AFX; Auxiliary Building Ventilation Fuel Handling and Exhaust Filter Unit
Temporary Ventilation Systems:
- Refuel Floor 650 Hold Down Spring Cutting Area
- Unit 1 Down Draft Table at 650 Upper Containment
- Unit 1 Lower Containment
Portable or Installed Monitoring Systems:
- Serial Number 342 at Refuel Floor 650
- Serial Number 631 at Unit 1 Lower Containment
- Serial Number 585 at Unit 1 Lower Containment
Self-Contained Breathing Apparatus for Emergency Use (IP Section 02.03) (1 Sample)
The inspectors evaluated self-contained breathing apparatus program implementation.
- (1) Status and Surveillance Records for Self-Contained Breathing Apparatuses (SCBAs):
- DW222039
- DW222036
- DW223151
- DW119016
- DW220024 SCBA Fit for On-Shift Operators:
- Three Operations Personnel
SCBA Maintenance Check:
- DW222039
- DW222036
- DW223151
- DW119016
- DW220024
Use of Respiratory Protection Devices (IP Section 02.02) (1 Sample)
The inspectors evaluated the licensees use of respiratory protection devices by:
- (1) Evaluations for the Use of Respiratory Protection:
- RWP-191154; Decontamination of Highly Contaminated Area Near Reactor Coolant Pump No. 13
- RWP-191140; Installation of Insulation of Reactor Coolant Pump No. 13
- RWP-191142; U1C29 Containment Scaffold Activities
Respiratory Protection Use During Work Activities:
- RWP-191105; U1C29 Reactor Lower Internal/Baffle Bolt Activities
- RWP-191175; U1C29 Regeneration Heat Exchanger Locked High Radiation Activities
Medical Fitness for Use of Respiratory Protection Devices:
- Three Operations Personnel
Observation of Donning, Doffing and Functional Test:
- Three Operations Personnel
- Two Radiation Protection Personnel
Respiratory Protection Device Evaluation
- Six Powered Air Purifying Respirators; PureFlo ICS Model PF60ESM
71124.04 - Occupational Dose Assessment
External Dosimetry (IP Section 02.02) (1 Sample)
- (1) The inspectors evaluated the licensees external dosimetry program implementation
Internal Dosimetry (IP Section 02.03) (1 Sample)
- (1) The inspectors evaluated the licensee's internal dosimetry program implementation
Whole Body Counts
- Whole Body Count performed on March 12, 2019
In-Vitro Internal Monitoring
- GEL Lab Tritium Analysis dated January 21, 2016 Dose Assessments Performed Using Air Sampling and Derived Air Concentration (DAC) Monitoring
- RWP-191175; Monitoring dated March 27, 2019
- RWP-191142; Monitoring dated March 19, 2019
Source Term Categorization (IP Section 02.01) (1 Sample)
- (1) The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity
Special Dosimetric Situations (IP Section 02.04) (1 Sample)
- (1) The inspectors evaluated special dosimetric situations:
Declared Pregnant Workers
- Declaration on February 14, 2019
- Declaration on November 6, 2018
Effective Dose Equivalent Exposures
- None Available
Shallow Dose Equivalent
- None Available
Neutron Dose Assessment
- None Available
71124.05 - Radiation Monitoring Instrumentation
Calibration and Testing Program (IP Section 02.02) (1 Sample)
The inspectors evaluated the calibration and testing program implementation.
- (1) The inspectors reviewed the following:
Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors, Portal Monitors, and Small Article Monitors
- SAM-12 No. 153
- GEM-5 No. 1 Personnel Contamination Monitor
- ARGOS No. 6 Personnel Contamination Monitor
Failure to Meet Calibration or Source Check Acceptance Criteria
- None were available during this inspection
Walkdowns and Observations (IP Section 02.01) (1 Sample)
The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.
- (1) The inspectors reviewed the following:
Portable Survey Instruments
- Eberline RM-20 No. 272 Calibrated on June 14, 2018
- Ludlum L-177 No. 156878 Calibrated on October 8, 2018
- Telepole TP-032 Calibrated on January 23, 2019
- Thermo Scientific RO-20 No. 356 Calibrated on April 22, 2019
- Eberline Thermo RO-20 No. 359 Calibrated on April 22, 2019
- Victoreen V-451 No. 1325 Calibrated on June 21, 2018
- Rados RDS-710756 Portable Hand Held Calibrated on August 13, 2018
- Rados RDS-710749 Portable Hand Held Calibrated on August 13, 2018
- Thermo E-600 With HP-270 Calibrated on May 4, 2019
- Hopewell BX-3-1 Calibrated on November 14, 2018
Source Check Demonstration
- Eberline Thermo RO-20 No. 359 Calibrated on April 22, 2019
- Rados RDS-710756 Portable Hand Held Calibrated on August 13, 2018
- Rados RDS-710749 Portable Hand Held Calibrated on August 13, 2018
- Thermo E-600 with HP-270 Calibrated on May 4, 2019
Area Radiation Monitors (ARM) and Continuous Air Monitors
- ARM 12-ERA-7505 Auxiliary Building 587 Monitor
- ARM 12-ERA-7006 TBX Nuclear Sample Room
- ARM 12-ERA-7000 TBX Nuclear Sample Room
- ARM 12-ERA-9403 Auxiliary Building 609 Hallway Area
- CAM AMS-4 No. 461 Eberline
- CAM AMS-4 No. 342 Eberline
- CAM AMS-4 No. 527 Eberline 609 Radwaste Handling Building
- CAM AMS-4 No. 586 Eberline Spent Fuel Pool Area
Personnel Contamination Monitors, Portal Monitors and Small Article Monitors (SAM)
- SAM-12 No. 153
- GEM-5 No. 1 Personnel Contamination Monitor
- ARGOS No. 6 Personnel Contamination Monitor
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15)===
- (1) PMP-7110-PIP-001 Reactor Oversight Program Performance Indicators and Monthly Operating Report Data; Occupational Exposure Control Data Samples; reviewed from January 1, 2018 through December 31, 2018
PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample.
(IP Section 02.16) (1 Sample)
- (1) PMP-7110-PIP-001 Reactor Oversight Program Performance Indicators and Monthly Operating Report; RETS/ODCM Radiological Effluent Occurrence Samples; Reviewed from January 1, 2018 through December 31, 2018
71152 - Problem Identification and Resolution
Annual Follow-Up of Selected Issues (IP Section 02.03) (2 Samples)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Capture of and review for applicability of operating experience with emphasis on items reported per the requirements of 10 CFR 21
- (2) Operator response to loss of Bus 21B
INSPECTION RESULTS
Unresolved Item (Closed)
Record Retention Requirements of the Boron Injection Tank and its Associated Support Structure 05000315,05000316/2018010-01 71111.21M
Description:
As part of follow-up inspection activities to address issues previously identified in Unresolved Item (URI)05000315/2018010-01; 05000316/2018010-01, the inspectors reviewed additional information provided by the licensee regarding the design and licensing basis of the boron injection tank and its associated support structure and consulted with technical staff from the Office of Nuclear Reactor Regulation (NRR). Based on this review, the inspectors sufficiently resolved the issues discussed in URIs05000315/2018010-01; 05000316/2018010-01 and consider URI 05000315/2018010-01; 05000316/2018010-01 closed. In particular, the inspectors did not identify any licensee actions that were inconsistent with the design and licensing basis of the boron injection tank and its associated support structure.
Corrective Action Reference(s): AR 2018-7104, Lack in Documentation for BIT (Boron Injection Tank) 1-TK-11, on 07/12/2018.
Failure to Develop Procedures for Loss of Electrical Bus Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems
Green NCV 05000315,05000316/2019002-01 Open/Closed None (NPP)71152 The inspectors identified a finding of very low safety significance and an associated non-cited violation (NCV) of TS 5.4.1.a when licensee personnel failed to have established procedures for the operation of the electrical distribution system as well as procedures for combating emergencies and other significant events, including a loss of electrical power to safety-related electrical Bus 21B. Because these procedures had not been established, the restoration of safety-related Bus 21B was delayed following a May 17, 2019, electrical fault in the 2-ABD-B switchgear.
Description:
On May 17, 2019, a Unit 2 electrical fault resulted in the loss of safety-related Bus 21B. The licensee immediately entered LCO 3.8.9, Distribution Systems - Operating, Condition A and declared Bus 21B and all of its associated loads inoperable. Control room staff subsequently identified that event response procedures had not been established to address the loss of Bus 21B and in lieu of a response procedure, consulted numerous resources to guide their response to the event. These resources included a number of alarm response procedures (ARPs) as well as Procedure OHP-4021-082-021, Removal and Restoration of Power to 600V Bus 21B and Associated Motor Control Centers. This procedure addressed the de-energization and restoration of Bus 21B as well as buses that were powered from Bus 21B in a non-emergency situation. Since these buses provide power to numerous safety-related loads, the procedure was intended to be implemented only with the plant in Mode 5, Mode 6, or Defueled. Coincident with the control room staff stabilizing the plant, Auxiliary Equipment Operators (AEOs) conducted a plant walkdown and determined that the 2-ABD-B switchgear was the source of the fault. The control room staff subsequently implemented actions to de-energize and electrically isolate the 2-ABD-B switchgear and to recover Bus 21B.
The Shift Technical Advisor subsequently identified that Power-Operated Relief Valve (PORV) block valve 2-NMO-152 received power from Bus 21B and confirmed that status lights for the valve were not illuminated. The PORVs were specifically addressed in Technical Specification (TS) 3.4.11, Pressurizer Power Operated Relief Valves (PORVs)and, if inoperable, in accordance with LCO 3.4.11 Condition A, required closing the associated block valve within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The crew was also required to perform the action of LCO 3.4.11 Condition C to place the associated PORV in manual control within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
Further, LCO 3.4.11 Condition H required that if the requirements of LCO 3.4.11 Condition A and/or Condition C were not met, that the plant be placed in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. However, the control room crew failed to promptly recognize that the PORV was rendered inoperable when power was lost to Bus 21B, and therefore the actions required by LCO 3.4.11 Condition A and LCO 3.4.11 Condition C, were not performed until about 1-1/2 hours after the LCO completion times of 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> had expired, but prior to the expiration of the requirement to place the plant in Mode 3.
Following completion of the actions related to the inoperable PORV, the licensee continued preparations to restore power to Bus 21B. Subsequently, with the 2-ABD-B switchgear electrically isolated, the licensee unsuccessfully attempted to close the supply breaker to Bus 21B. The licensee did not initially understand the cause for this failure until an operator identified that an interlock between the Bus 21B breaker and a Bus 21B crosstie breaker was not satisfied with the crosstie breaker in its racked out position. Subsequently, the licensee racked the crosstie breaker into its test position, which satisfied the interlock requirement, and successfully closed the Bus 21B supply breaker to restore power to all of the Bus 21B loads.
Following restoration of Bus 21B, the licensee exited LCO 3.8.9 Condition A within the required LCO Allowed Outage Time (AOT). Technical Requirements Manual (TRM) 8.11.2, FLEX Plant Connection Points and Plant Components, and FLEX Plant Connection Points and Plant Components Combined with FLEX Portable Equipment, specified in Technical Requirements for Operation (TRO) 8.11.2 that the FLEX plant connection points and plant components specified in the FLEX Equipment Program shall be available. The Actions Section of TRO 8.11.2 included a Note, which specified that TRO 8.11.2 Condition entry was not required for the unavailability of plant components covered by Technical Specifications or other TRM sections. Therefore, until Bus 21B was restored, none of the conditions of TRO 8.11.2 was applicable. However, following restoration of Bus 21B and the 2-ABD-B switchgear, the inspectors conducted a plant walkdown and identified that the 2-ABD-B switchgear included a 600V FLEX connection point, and therefore the conditions of TRO 8.11.2 had been required to be met between the time that Bus 21B was restored to service and the 2-ABD-B switchgear was repaired and returned to service. TRO 8.11.2 Condition A required that if one or more required FLEX primary or alternate connection points or plant components specified in the FLEX Equipment Program were not available, then in accordance with Condition A.1 the licensee must immediately verify that a primary or alternate connection point was available. Furthermore, TRO 8.11.2 Condition C required that if the requirements of Condition A.1 were not met within the required completion time that, in accordance with Condition C.1, the licensee must immediately initiate action to implement compensatory measures. However, after the inspectors identified that the 2-ABD-B switchgear included a 600V FLEX connection point, the inspectors determined that licensee staff failed to perform any of the required actions of TRM 8.11.2 although the 2-ABD-B switchgear FLEX connection point was specified in the FLEX Equipment Program. The licensee restored the connection point to an available status on May 22, 2019, when the 2-ABD-B switchgear was restored.
Corrective Actions: Immediate corrective actions by the licensee included electrically isolating the faulted 2-ABD-B switchgear and re-energizing Bus 21B. The licensee subsequently replaced damaged bus bars and recovered the 2-ABD-B switchgear. The licensee also entered this issue into their corrective action program.
Corrective Action References: AR-2019-5318, Failure of Auxiliary Jacket Water Breaker Causes Loss of Bus 21B 600V, May 17, 2019
Performance Assessment:
Performance Deficiency: The inspectors concluded that the failure to have established procedures that addressed the operation of the electrical distribution system, including a fault in the 2-ABD-B switchgear that resulted in the loss of Bus 21B that included safety-related loads, was a performance deficiency. TS 5.4.1.a required that the licensee establish, implement and maintain procedures recommended in Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), which included procedures for the operation of the Alternating Current System and procedures for combating significant events including a loss of electrical power. However, the licensee failed to have established procedures for the operation of Bus 21B and its loads in Mode 1 and failed to have established procedures for combating a loss of Bus 21B. As a result of the licensee's failure to have established procedures for the operation of Bus 21B, and following an event that resulted in the loss of Bus 21B, licensee personnel failed to promptly identify that actions were required to place an inoperable PORV in manual control and close the associated block valve, and failed to verify that a FLEX primary or alternate connection point was available.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Procedure Quality attribute of the Mitigating Systems cornerstone. Specifically, the licensee failed to establish procedures to address the operation of the Alternating Current System and for combating significant events, including a loss of electrical power event. Specifically, the licensee failed to establish procedures to address the operation of electrical Bus 21B and the combating of a loss of electrical Bus 21B in Mode 1.
Significance: The inspectors assessed the significance of the Finding-using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors reviewed the issue in accordance with Inspection Manual Chapter (IMC) 0609 Appendix A.
Using Exhibit 2, the inspectors determined the issue specific to restoration of Bus 21B screened as having very low risk significance (i.e., Green) because it was not inoperable for longer than the TS Allowed Outage Time (AOT). The inspectors concluded that the failure to complete the TRM actions within the required completion time was also of very low risk significance (i.e., Green) because the inspectors answered No to all of the questions in Exhibit 2. The issue related to the inoperable PORV block valve required a Detailed Risk Evaluation (DRE) because the loss of power to the block valve represented a loss of the ability to isolate the associated PORV in the event the PORV failed to close following a open demand signal.
The inspectors modeled the inoperability of a pressurizer PORV block valve for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to bound the time in excess of the AOT the block valve was inoperable. Using this duration, the Standardized Plant Analysis Risk (SPAR) model calculated an Incremental Conditional Core Damage Probability (ICCDP) of 1.5E10-10. With this very low risk impact, the inspectors concluded that the issue was of very low risk significance (i.e., Green). The inspectors consulted with the regional Senior Reactor Analyst (SRA) regarding their conclusion. The SRA agreed that the issue was of very low risk significance.
Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.
Enforcement:
Violation: TS 5.4.1.a requires, in part, that written procedures shall be established, implemented and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. NRC Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), Revision 2, Appendix A, Section 3.s(2), Electrical Systems - Onsite, includes procedures for the operation of the Alternating Current System and Section 6.c, Procedures for Combatting Emergencies and Other Significant Events - Loss of Electrical Power, includes procedures for combating significant events including a loss of electrical power event.
Contrary to the above, as of May 17, 2019, the licensee failed to establish procedures to address the operation of the Alternating Current System and for combating significant events, including a loss of electrical power event. Specifically, the licensee failed to establish procedures to address the operation of electrical Bus 21B while in Mode 1 and for combating a loss of electrical Bus 21B.
Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On April 11, 2019, the inspectors presented the URI 05000315/2018010-01; 05000316/2018010-01 inspection results to Mr. J. Petro and other members of the licensee staff.
- On April 18, 2019, the inspectors presented the Radiation Protection inspection results to Mr. S. Lies, Site Vice President, and other members of the licensee staff.
- On June 6, 2019, the inspectors presented the Radiation Monitoring Instrumentation and Performance Indicator Verification Review inspection results to Mr. S. Lies, Site Vice President, and other members of the licensee staff.
- On July 23, 2019, the inspectors presented the integrated inspection results to Mr. J. Gebbie and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Procedures
2-OHP-4021-
033-001
Supplemental Diesel Generator Operations
2-OHP-4021-082-
006
Operation of 2AB & 2CD Battery Chargers
Corrective Action
Documents
AR 2017-10698
Maintenance Rule Scoping Documents Do Not Comply with
Site Procedures
10/22/2017
AR 2018-4810
Unexpected CR Alarm U2 AB Battery Ground
04/30/2018
GT 2019-1626
STRIDE STI-19-02; Change Battery Surveillance Test
Interval
2/20/2019
Engineering
Changes
Replacement Vertical Bus, MCC 2-ABD-B
05/19/2019
Engineering
Evaluations
2543
Supporting EC-56979 Busbar Requirements
Work Orders
55529338-01
Battery AB, CD, and N-Train Battery Quarterly Surveillance
05/24/2019
Corrective Action
Documents
AR 2019-3488
Boric Acid Deposit on the #4 Reactor Coolant Pump Seal
Injection 2 Line
04/03/2019
AR 2019-3126
Aggregate ODE or U1C29
03/26/2019
AR 2019-6101
Unexpected Lowering in Pressurizer Pressure
06/15/2019
Corrective Action
Documents
Resulting from
Inspection
AR 2019-4856
RCP-Loose Lateral Restraining Bumper Shim
05/05/2019
Engineering
Changes
Contingency 1-80007R-1 Cable Replacement
Procedures
PMP-5040-SDP-
001
Standard Design Process Interface
PMP-5040-SDP-
001
Standard Design Process Interface
Drawings
1-2-3834-5
N.S.S.S. Support Framing Coolant Pump Support Sections
& Details - D.C. Cook Nuclear Plant
Engineering
Changes
EC-0000052453-
Unit 1 Reactor Controls & Instrumentation (RCI), Calibration
Testing of Inputs for Control Group 2
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
EC-0000052453-
Unit 1 Reactor Controls & Instrumentation (RCI), Calibration
Testing of Inputs for Control Group 4
EC-0000054411-
U1 Solid State Protection System (SSPS) Train B Upgrade
Functional Testing
Miscellaneous
CYCLE 10912-
11007
Online Daily Cycle (U1 DGAB)
03/19/2019
Procedures
1-EHP-4030-134-
203
Unit 1 LLRT - Test Sketch Leak Rate Data Sheet
1-OHP-4030-132-
217B
DG1AB Load Sequencing & ESF Testing
Work Orders
55454613-09
MTI, 1-QRV-171, Check Indications, Adjust/Calibrate Limit
Switches
03/29/2019
Miscellaneous
DIT-S-06353-00
Unit 1 Cycle 28, End-of-Cycle (EOC) Time-to-Boil
Information
2/04/2019
R-EDG-DGAB-
0904
Unit 1 AB Diesel Generator Jacket Water Pump Clearance
R-NI-FMS-0657
Flux Mapping System Clearance
Procedures
1-OHP-4021-001-
001
Plant Heatup from Cold Shutdown to Hot Standby
1-OHP-4021-001-
2
Reactor Start-Up
2-EHP-4030-
2-356
Low Power Physics Tests with Dynamic Rod Worth
Measurement
2-THP-6010-
RPP-413
ALARA Plan Template
04/24/2019
Radiation
Surveys
SW_VSDS-M-
20190425-1
U1-U/C Upender Survey for Diving
04/24/2019
Radiation Work
Permits (RWPs)
191186
U1C29 - Spent Fuel Pool Transfer Canal and Refuel Cavity
Diving Activities
71111.21M Corrective Action
Documents
AR 2018-7104
Lack in Documentation for BIT 1-TK-11
07/12/2018
Miscellaneous
Section III
1968 thru
Winter 1969
Addenda
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Section VIII
1968 thru
Winter 1969
Addenda
Corrective Action
Documents
GT 2019-6188
1-IHP-4030-151-010 Step 4.15.4 Needs a Note
06/18/2019
Procedures
1-IHP-4030-151-
010
Steam Generators 2 and 3 Steam Pressure Protection Set 3
Channel Operational Test and Calibration
1-OHP-4030-156-
017T
Turbine Driven Auxiliary Feedwater System Test
2-EHP-4030-
2-356
Low Power Physics Tests with Dynamic Rod Worth
Measurement
2-IHP-4030-228-
005B
Train B CEQ Fan Surveillance and Engineered Safety
Feature Response Time Test
Calculations
S279303
Fit Test Report
04/10/2019
Corrective Action
Documents
AR-2017-8946
Auxiliary Building Fuel Area Fan Charcoal, Door Seals and
Latches Needed to be Replaced
09/16/2017
AR-2018-0654
Evaluate Available Charcoal Run Time for 1-HV-AES-1;
Percent Efficiency was 96.37 %
01/22/2018
Miscellaneous
353790 - 0
TRI Air Testing, Inc.; Laboratory Report Compressed
Air/Gas Quality Testing
2/01/2019
55526138-01
OPFP, Air Hawk SCBA Monthly Inspection
07/30/2018 -
2/06/2018
Procedures
FPP-2281-RES-
201
Maintenance and Repair of Respiratory Devices
FPP-2281-RES-
210
Respiratory Fit Testing With the Portacount
PMP-2281-RES-
001
Control and Use of Respiratory Protection Devices
Radiation Work
Permits (RWPs)
RWP-191140
Installation of Insulation of RCP No. 13
RWP-191105
Reactor Baffle Bolt Inspection and Repair Activities Include
Lower Internal Movements
RWP-191154
Decontamination of Highly Contaminated Area Near Reactor
Coolant Pump No.13
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
RWP-191175
Medium Risk: Valve Maintenance Activities
Calculations
212
Multiple WBC Summary Sheet for Contaminated Individuals
03/11/2019 -
03/14/2019
DPW Report
Declared Pregnant Women Radiation Exposure Monitoring,
Reporting and Dose Control
04/09/2017 -
01/09/2019
RWP-191175
Valve Maintenance Activities; Total Effective Dose
Equivalent Evaluation Based on Derived Air Concentration
of Particulate
03/22/2019
Corrective Action
Documents
AR-2019-3655
Worker Received a Level 2 Particle Percon on the Left Shirt
Sleeve in Clean Area at 609 Elevation Auxiliary Building
West Hallway
04/08/2019
Procedures
2-THP-6010-
RPP-212
Operation of the ORTEC Fastscan Whole Body Counter
PMP-6010-RPP-
100
Radiation Exposure Monitoring, Reporting and Dose Control
Calibration
Records
2-THP-6010-
RPC-515
AMS-4 No.586 Calibration Data Sheet
01/03/2019
2-THP-6010-
RPC-515
AMS-4 Calibration Data Sheet No. 585
2/20/2019
2-THP-6010-
RPC-516
Calibration of the Mirion Technologies RDS-31 Meter and
Smart Probes; No. RDS-712427
2/18/2019
2-THP-6010-
RPC-516
Calibration of the Mirion Technologies RDS-31 Meter and
Smart Probes; SN RDS-712427
01/22/2019
2-THP-6010-
RPC-517
Calibration of Portable Dose-Rate Instrument Calibration
Data Sheet
01/14/2019
2-THP-6010-
RPC-525
Calibration of the Radiological Contamination Friskers; RM-
14/RM-20/L-177 Calibration Data Sheet; RM-14 No. 8702
11/07/2019
2-THP-6010-
RPC-535
Calibration of the ORTEC Fastscan Whole Body Counter;
Reference Standard and Calibration Confirmation
Worksheet; SN. FS-2
09/13/2018
2-THP-6010-
RPC-537
Calibration of the F&J Battery Powered Air Sampler
Calibration Data Sheet; SN BPLV-10398 CRP-362
11/12/2018
2-THP-6010-
RPC-555
Calibration of the MGP Model AMP-50 and AMP-100 Area
Monitor
04/20/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
2-THP-6010-
RPC-577
Calibration of the Ludlum 3030P Alpha-Beta Counter Data
Sheet; SN 264783
2/11/2019
2-THP-6010-
RPC-596
Calibration of the Thermo Scientific Small Article Monitor
SAM-12 No. 148
04/17/2019
2-THP-
6010RPC-517
Calibration of Portable Dose-Rate Instruments RO-20 No.
356
04/01/2019
2-THP-6020-
INS-526
Gamma Spectrometry Using ORTEC Global Value and
Gamma Vision Software; Performed on Detector Nos. 3 and
10/31/2016
Radiation Safety
& Certified
Services RSCS
Calibration
Certificate No.
2603129836-0
Thermo Scientific Model E-600R Calibration with Model
Probe SHP-270; SN 02603
2/22/2019
Procedures
2-THP-6010-
RPC-515
Calibration of the Eberline Model AMS-4
71151
Miscellaneous
PI Verification
PMP-7110-PIP-
001
Reactor Oversight Program Performance Indicators for
Monthly Operating Report Data
January
2018 through
December
2018
PMP-7110-PIP-
001
Reactor Oversight Program Performance Indicators and
Monthly Operating Report Data; RETS/ODCM Radiological
Effluent Occurrences
01/2018 -
2/2018
PMP-7110-PIP-
001
Reactor Oversight Program Performance Indicators and
Monthly Operating Report Data; Occupational Exposure
Control Effectiveness
01/2018 -
2/2018
Corrective Action
Documents
AR 2019-5318
Failure of Auxiliary Jacket Water Breaker Causes Loss of
21B 600V
05/17/2019
AR 2019-5592
Bus Restoration Procedure Inappropriately N/A'd
05/28/2019
GT-2017-13010
2018 Part 21 Tracking Items
2/20/2017
GT-2019-0164
2019 Part 21 Tracking Items
01/07/2019
Procedures
PMP-7030-P21-
001
Processing and Reporting of Defects and Noncompliances
8