IR 05000277/1979006

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IE Insp Repts 50-277/79-06 & 50-278/79-05 on 790220-23 & 0312-16.Noncompliance Noted:Access Control & Personnel Authorizations.Details Withheld (Ref 10CFR2.790)
ML19254E823
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 08/08/1978
From: Greenman E, Havens O, Mccabe E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
To:
Shared Package
ML19254E802 List:
References
50-278-79-05, 50-278-79-5, 79-277-79-06, 79-277-79-6, NUDOCS 7911020362
Download: ML19254E823 (1)


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U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSRECTION AND ENFORCEMENT Region I 50-277/79-06 Report No.

gn_p7p/7o_ng 50-277 Docket No.

sn_p7a DPR-44 C

License No. npR-56 Priority

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Category r

Licensee:

Philadelphia Electric Company 2301 Market Street Philadelphia, Pennsylvania 19101

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Facility Name:

Peach Bottom Atomic Power Station, Units 2 & 3 Inspection at:

Delta, Pennsylvania Inspection conducted:

February 20-23 and March 12-16, 1979 Inspectors: h w ##7t GP

f G.

nman, Reactor Inspector date signed date signed Other Accompanying Personnel:

0. H. Havens, 0IE, H0 date signed Approved by:

P. C AM 3 s.

e l el'7 'l E. C. McCabe, Jr., Chief, Reactor Projects date signed Section No. 2, R0&NE Branch

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Inspection Summary:

Inspection on February 20-23 and March 12-16,1979 (Combined Report Nos. 50-277/79-06; 50-278/79-05 Areas Inspected: Routine, unannounced inspection by a regional based inspector of plant operations, facility tours, review of monthly operating report, followup on previously identified unresolved items, security program reviews during the trans-itional period just prior to February 23, 1979 regarding plan implementation and requirements of 10 CFR 73 and independent effort.

The inspection involved 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> onsite at Unit 2 and 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> onsite at Unit 3 by one NRC regional based inspector.

Results: Two items of noncompliance were identified related to security plan re-quirements (Infraction - Access control - paragraph 5.a (2.790(d); and Deficiency -

personnel authorizations - paragraph 5.c (2.790(d)).

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Region I Form 12 (Rev. April 77)

iT]f 1 7911020

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DEIAILS E

1.

Persons Contacted C. Anderson, Operations Engineer R. Fleishmann, Assistant Station Superinter. dent S. Roberts, Results Engineer S. Tharpe, Security Supervisor W. T. Ullrich, Station Superintendent J. Winzenried, Technical Engineer Other licensee representatives were contacted during the inspection.

These included engineering personnel, administrative personnel, reactor operators, shift supervision, security personnel and health physics pers'i'nnel.

2.

Previous Inspection Item Update (Closed) Unresolved items (277/79-04-02; 278/79-03-02): Torus Water Volume.

Licensee Event Report Nos. 2-79-12 and 3-79-9 were filed by the licensee.

The inspector reviewed a revised ST9.1-2 "The Surveillance Log" and a change dated March 7, 1979 to the procedure which tightened torus limits to account for pressure. The inspector had no further questions regarding this matter at this time.

3.

Logs and Records The following logs and records were reviewed without comment except as noted within this report.

Logs were reviewed pursuant to the licensee's administrative requirements.

a.

Shift Supervision Log - February 20 - March 16, 1979 b.

Reactor Operators Log, Unit 2 - February 20 - March 16,1979 c.

Reactor Operators Log, Unit 3 - February 20 - March 16,1979 d.

Jumper Log - Current Entries Unit 2 a d Unit 3 e.

Operations Work and Information Forms - Current f.

Maintenance Request Log Units 2 and 3 - Sampling No unacceptable conditions were identified.

4.

Facility Tours Facility tours were conducted on an unescorted basis at Unit 2 and Unit 3.

Areas examined included security access controls, verification of minimum control room staffing requirements and general plant status.

Inspections were conducted to determine the general state of cleanliness, housekeeping and included observation of plant conditions.

No significant fluid leaks 1249 132

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were observed.

The inspector checked equipment operab'ility and verified by comparison of selected control room and in plant instrumentation that limiting conditions for operation were being satisfied. The inspector discussed alann status with operators. Operators were knowledgable of plant conditions and the reasons for alarms.

Numerous high radiation doors required to be locked were checked and found to be secured. The inspector also confirmed the st-tus of selected locked valves.

No un-acceptable conditions were identified.

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THIS PAGE INTENTIONALLY LEFT BLANK, IT CONTAINED 2.790 INFORMATION NOT FOR PUBLIC DISCLOSURE 1249 134

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THIS PAGE INTENTIONALLY LEFT BLANK, IT CONTAINED 2.790 INFORMATION, NOT FOR PUBLIC DISCLCSURE.

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6.

Review of Monthly Operating Reports The following licensee report has been reviewed in office:

Peach Bottom Atomic Power Station Monthly Operating Reports for January 1979 dated February 13, 1979.

This report was reviewed pursuant to Technical Specifications and verified to determine that Operating Statistics included shutdowns and that narrative summaries of the month's operating experience were contained therein.

No unacceptable conditions were identified.

7.

Exit Interview At periodic intervals during the course of this inspection, meetings were held with senior facility management to discuss inspection scope and findings.

Licensee representatives acknowledged inspection findings.

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