IR 05000263/2025004

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Integrated Inspection Report 05000263/2025004
ML26016A558
Person / Time
Site: Monticello 
Issue date: 01/20/2026
From: Dariusz Szwarc
NRC/RGN-III/DORS/RPB3
To: Hafen S
Northern States Power Company, Minnesota
References
IR 2025004
Download: ML26016A558 (0)


Text

SUBJECT:

MONTICELLO NUCLEAR GENERATING PLANT - INTEGRATED INSPECTION REPORT 05000263/2025004

Dear Shawn Hafen:

On December 31, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Monticello Nuclear Generating Plant. On January 8, 2026, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Dariusz Szwarc, Chief Reactor Projects Branch 3 Division of Operating Reactor Safety Docket No. 05000263 License No. DPR-22

Enclosure:

As stated

Inspection Report

Docket Number:

05000263

License Number:

DPR-22

Report Number:

05000263/2025004

Enterprise Identifier:

I2025004-0058

Licensee:

Northern States Power Company, Minnesota

Facility:

Monticello Nuclear Generating Plant

Location:

Monticello, MN

Inspection Dates:

October 1, 2025, to December 31, 2025

Inspectors:

T. Hartman, Senior Resident Inspector

T. McGowan, Emergency Preparedness Inspector

K. Pusateri, Resident Inspector

J. Robb, Operations Engineer

T. Wingfield, Operations Engineer

Approved By:

Dariusz Szwarc, Chief

Reactor Projects Branch 3

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Monticello Nuclear Generating Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

The unit began the inspection period at rated thermal power. On December 22, 2025, the unit was lowered to approximately 55 percent rated thermal power for repairs to a main feedwater pump. On December 24, 2025, the unit returned to rated thermal power and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs)in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed onsite portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)division 1 emergency filtration train emergency service water system on October 02, 2025 (2)division 1 residual heat removal service water (RHRSW) on October 30, 2025

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1)fire zones 15 B, C, and D, 11 diesel generator room including 11 and 12 day tank rooms, on October 07, 2025 (2)fire zone 8, cable spreading room, on October 20, 2025

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating examination and biennial written examinations administered between the weeks of September 8, 2025, and October 20, 2025.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during power reduction for reactor feedwater pump repairs with reactor manual control system challenges on December 20, 2025.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated an NRC exam simulator requalification scenario on October 22, 2025.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1)unplanned entry into a risk informed completion time for an instrument failure in reactor core isolation cooling (RCIC) system on October 12, 2025 (2)emergent change in high-risk plan for reactor building main supply HVAC unit (VAC10A) per WO 700143690

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:

(1)14 residual heat removal (RHR) service water pump has low discharge pressure (2)division 2 RHR low pressure coolant injection outboard valve (MO2013) motor pinion concern with no set screw part traceability (3)division 1 RHR discharge to torus outboard valve (MO2006) loose motor pinion (4)12 RHR pump vibrations are in the inservice testing (IST) alert range

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.0102.03) (1 Sample)

(1) The inspectors evaluated the following submitted emergency action level and emergency plan changes:
  • EPLAN04, Monticello Emergency Action Level (EAL) Technical Basis Document, Rev. 3 This evaluation does not constitute NRC approval.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)

(1) Unit 1 (October 1, 2024, through September 30, 2025)

MS10: Cooling Water Support Systems (IP Section 02.09) (1 Sample)

(1) Unit 1 (October 1, 2024, through September 30, 2025) 71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1)safety-related grease expiring prior to use (2)reactor pressure vessel flange inner seal leakage

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program to identify potential trends that might be indicative of a more significant safety issue during the week ending December 12, 2025. Since April 1, 2025, the licensee, in accordance with FP-PA-ARP01, CAP Process, has written 36 corrective action documents to evaluate issues that are or could be considered trends. The inspectors did not identify any findings or violations of NRC requirements in the course of their review.

INSPECTION RESULTS

No findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 8, 2026, the inspectors presented the integrated inspection results to S. Hafen, Site Vice President, and other members of the licensee staff.
  • On December 19, 2025, the inspectors presented the Emergency Action Level and emergency plan changes inspection results to B. Carberry, Emergency Preparedness Manager, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

215423

RHR Service Water System Prestart Valve Checklist

71111.04

Procedures

215434

Emergency Service Water System Prestart Valve Checklist

A.308

Cable Spreading Room

71111.05

Fire Plans

A.315-B

No. 11 Diesel Generator Room & No. 11 & No. 12 DG

Day Tank Rooms

Miscellaneous

RQ-SS175

RCIC Leak, Loss of Stator Water Cooling with High Power

ATWS

71111.11Q

Procedures

2300

Reactivity Adjustment

2/20/2025

Procedures

FP-WM-IRM01

Integrated Risk Management

71111.13

Work Orders

WO 700143690

Perform Mechanical PM on V-AC10A Rx Bldg. Main

Supply HVAC Unit

01/29/2019

501000089688

MO2013 Motor Pinion Concern

09/10/2024

501000098840

RHR Pump Vibrations Elevated into the Alert Range

During Procedure 025504-IA12

05/15/2025

501000102811

Pinion Gear was Loose on the Motor Shaft During Extent of

Condition Inspection

09/09/2025

501000103587

RHRSW Pump Pressure Low During RTS

10/06/2025

Corrective Action

Documents

501000105806

RSW Pump Low Pressure at B RHR HX

2/05/2025

501000105620

Motor Pinion Inspection Enhancements

11/25/2025

501000105630

MOV Set Screw Not Retained

11/25/2025

501000105656

NRC Question on 7001437650010 Redundant Steps

2/01/2025

71111.15

Corrective Action

Documents

Resulting from

Inspection

501000106124

NRC Question on P202B Maintenance

2/15/2025

501000094114

MNGP Ops Memo 2405 vs. EPFAQ 201804

01/16/2025

501000102376

EPLAN Document Alignment

08/27/2025

501000102591

EPLAN01 Rev 1 Change Summary Incorrect

09/02/2025

501000102592

Emergency Plan Submittal was Late

09/02/2025

501000102731

Documents Not Updated for EPLAN Change

09/05/2025

Corrective Action

Documents

501000103510

EPLAN/EPIP Misalignment

09/30/2025

EPLAN01

Standard Emergency Plan

71114.04

Procedures

EPLAN02

Emergency Plan Annex

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

EPLAN04

Monticello Emergency Action Level (EAL) Technical Basis

Document

MSPI Margin Report - MS0608, 4Q243Q25

10/28/2025

MSPI Derivation Reports; Cooling Water, Residual Heat

Removal; Unavailability Index; Unit 1

10/1/2024 -

09/30/2025

MSPI Derivation Reports; Cooling Water, Residual Heat

Removal; Unreliability Index; Unit 1

10/1/2024 -

09/30/2025

MSPI Basis Document

71151

Miscellaneous

MSPI Basis Document

501000012629

SR Grease Expiration Concern

05/30/2018

501000012696

SR Grease Past Expiration Date

06/01/2018

501000098976

Vessel Flange Seal Leak

05/19/2025

501000101552

Vessel Flange Leakage 4A-35 Received

08/02/2025

501000102090

Seal Leak Parameter Action Level Reached

08/17/2025

501000102132

Flange Seal Leak Growing

08/18/2025

501000102188

Condition Update for WO 70055219

08/21/2025

Corrective Action

Documents

501000102290

ACMP Threshold Value Updated

08/22/2025

Engineering

Evaluations

608000000211

Grease Used in Safety-Related Equipment Exceeded Shelf

Life

Adverse Condition Monitoring Plan - Vessel Flange Seal

Leak Alarm

Adverse Condition Monitoring Plan - Vessel Flange Seal

Leak Alarm

Monticello Station Log

08/01/2025 -

08/22/2025

Miscellaneous

ODMI 2508

Type 2 Operation Decision Making Issue Evaluation - Rx

Vessel Flange Leak

C.6004-A35

Vessel Flange Seal Leak

71152A

Procedures

FP-SC-PE05

Shelf Life Program

501000100107

NOS Adverse Trend: Maintenance PU&A

06/18/2025

501000101787

Trend in Work H Rule CAPS

08/08/2025

501000102721

Trend CAP - Door Issues at MNGP

09/05/2025

71152S

Corrective Action

Documents

501000104174

Potential Trend in Rework

10/17/2025

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

501000105262

Trend in CAP Closure and Causal Eval

11/13/2025

501000105615

Trend in CAP Behaviors

11/25/2025

Miscellaneous

MT POT TREND Keyword Search 04012025 to 11302025

2/03/2025

Procedures

FP-PA-ARP01

CAP Process

68