IR 05000155/1979009

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IE Insp Rept 50-155/79-09 on 790424-25.No Noncompliance Noted.Major Areas Inspected:Leakage at Control Rod Drive Penetration F2
ML19246B682
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 05/10/1979
From: Danielson D, Lee E K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19246B679 List:
References
50-155-79-09, 50-155-79-9, NUDOCS 7907180319
Download: ML19246B682 (3)


Text

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U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-155/79-09 Docket No. 50-155 License No. DPR-6 Licensee:

Consumers Power Company 212 West Michigan Avenue Jackson, MI 49201 Facility Name:

Big Rock Point Nuclear Generating Plant Inspection At:

Big Rock Point Site, Charlevoix, MI Inspection Conducted: April 24-25, 1979

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Inspector:

E. W. K. Le 7[

br+O-3, Approved By:

D. H. Danielson, Chief

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Engineering Support Section 2 Inspection Summary Inspection on April 24 and 25, 1979 (Report No. 50-155/79-09)

Areas Inspected: Leakage at Control Rod Drive Penetration No. F2.

The inspection involved a total of eight inspection-hours onsite by one NRC inspector.

Results: No items of noncompliance or deviations were identified.

339 265 7907180 3 @ p

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DETAILS Persons Contacted Principal Licensee Employees R. Abel, Senior Engineer

  • D.

DeMoor, Technical Engineer J. Rang, Operations and Maintenance Superintendent

  • Denotes those attending the exit inte rview.

Functional or Program Areas Inspected 1.

Leakage at Control Rod Drive Penetration No. F2 a.

Initial Identification by Licensee During hydrostatic testing of the reactor pressure vessel, the licensee noticed water was leaking at control rod drive penetration No. F2 when the pressure was at 900 psi.

The Leakage rate was 8 ml/ minute.

The hydrostatic test was then abandoned. Leakage appears to cease at ambient condition.

b.

Actions Being Considered By Th-Licensee It is the inspector's understanding that the following actions are being considered by the licensee:

(1) Take samples of scales on the bottom head of the reactor pressure vessel; (2) Perform hydrostatic test at 500 psi; 900 psi and 1500 psi to check for possible leaks of all the CRD penetrations; (3) Build a mock-up to qualify nondestructive testing; (4) Pressurize penetration F2 from the outside and check for bubbles inside the reactor pressure vessel with a renote camera.

c.

Visual Examination of CRD Penetrations The inspector visually inspected the CRD penetrations.

It was determined that (1) discoloration is severe around penetration F2; (2) discoloration around other penetrations in evident but not as severe as penetration F2 and (3)

leakage is not evident in penetration F2.

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No items of noncompliance or deviations were identified.

Exit Interview The inspector met with the licensee representatives (denoted in the Persons Contacted patagraph) on April 25, 19/9.

The inspector su=marized the scope and findings of the inspection. The licensee acknowledged the information.

339 267

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