05000482/LER-2008-004

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LER-2008-004, Loss of Offsite Power Event When the Reactor Was De-fueled
Docket Numbersequential Revmonth Day Year Year Month Day Yearnumber No. 05000
Event date: 04-07-2008
Report date: 11-11-2009
Reporting criterion: 10 CFR 50.73(a)(2)(iv), System Actuation

10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(v), Loss of Safety Function
4822008004R01 - NRC Website

PLANT CONDITIONS PRIOR TO EVENT:

MODE - De-fueled Power- 000

BACKGROUND:

The Kansas Gas and Electric and Kansas City Power and Light transmission systems serve as the main outlet and source of offsite power for Wolf Creek Generating Station (WCGS). Connection of the station output to the system is achieved via a 345-kV overhead line from the plant yard to the Wolf Creek 345-kV switchyard [EDS Code: FK].

There are three 345-kV lines connecting the WCGS 345-kV Substation to the area transmission system. The three lines are as follows:

a.WCGS-LaCygne 345-kV Line:

58 miles long, connecting to the LaCygne Steam Electric Station which has three additional 345-kV lines.

b.WCGS-Rose Hill 345-kV Line:

98 miles long, connecting to the Rose Hill Substation southeast of Wichita. Rose Hill Substation has two additional 345-kV connections.

c.WCGS-Benton 345-kV Line: 90 miles long, connecting to the Benton Substation northeast of Wichita. Benton Substation has two additional 345-kV lines, one of which is to the Wichita 345-kV Substation, near the Gordon Evans Steam Electric Station.

If one of the three 345-kV lines faulted, the breakers located at WCGS Substation would trip, deenergizing the line.

Any one of the two remaining incoming 345-kV transmission lines at Wolf Creek Substation can carry the total Engineered Safety Features (ESF) load required for safe shutdown by controlled switching of the Wolf Creek substation breakers, providing a separate transmission line feeding each ESF transformer.

Two physically independent sources of offsite power are brought to the onsite power system. One circuit is fed from ESF transformer XNB01 and supplies power normally to its associated 4.16-kV Class 1 E bus [EllS Code: EK]. The other circuit is fed from one secondary winding of the startup transformer (S/U), through ESF transformer XNB02, and supplies power normally to its associated 4.16-kV Class IE bus. In addition, each offsite power circuit can be manually aligned to supply power to the opposite or both 4.16-kV Class IE busses, if required. Each of these offsite power circuits is designed to be available in sufficient time to ensure that specified acceptable fuel design limits and design conditions of the reactor coolant pressure boundary are not exceeded following a loss of all onsite power sources and the remaining offsite power circuit.

EVENT DESCRIPTION:

At 1017 on 4/7/2008, during the Refuel 16 Outage, work that was on-going in the WCGS Switchyard inadvertently caused a loss of offsite power (LOOP). The LOOP event was initiated when a Westar Senior Relay technician, from one of WCGS owner companies, closed the wrong set of trip links on a 345 kV breaker during the Rose Hill transmission line transfer/breaker failure trip preventative maintenance (PM) testing. Instead of closing the Rose Hill transmission line trip links, the technician closed the Plant Startup (PSU) primary and backup trip links, which are associated to the WCGS startup transformer protection. When the links were closed, the breaker failure circuitry associated to the startup transformer was enabled. With the incorrect links in service and when the manual trip signal was generated as a part of the PM activity, the remaining off-site power connections to the West 345 kV bus were de-energized by the opening of their associated breakers. This inadvertent action tripped the West 345 kV bus and caused the LOOP.

The "A" emergency diesel generator (EDG) [EllS Code: DG) and the "A" safety bus was out of service for maintenance. The "B" EDG automatically started and provided the electrical power needed for safety related equipment. At the time of the LOOP, all of the reactor fuel had been off-loaded from the core and was being stored in the spent fuel pool [EDS Code: DA). Spent fuel pool cooling was temporarily interrupted until Operations personnel restarted the spent fuel pool cooling pump at 1038, after the "B" EDG restored power.

Power for the safety related equipment was restored from offsite power by 1024 on 4/7/2008. The "B" EDG was manually shut down at 1249 on 4/7/2008.

As a result of the loss of offsite power, the control room staff entered the emergency plan and declared a Notification of Unusual Event (NUE). When offsite power was restored and the EDG shut down, the NUE was exited at 1250 on 4/7/2008. Plant safety was maintained at all times throughout the event and there were no injuries.

BASIS FOR REPORTABILITY:

The actuation of Engineered Safety Features (ESF) described in this event is reportable per 10 CFR 50.73(a)(2)(iv) (A), which requires reporting of "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B) of this section." Paragraph (B)(8) of 10 CFR 50.73(a)(2)(iv) includes "Emergency ac electrical power systems, including: emergency diesel generators (EDGs)..

This event is also considered reportable pursuant to 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. Specifically, the guidance in NUREG-1022, Rev.2, "Event Reporting Guidelines," states: "Both offsite electrical power (transmission lines) and onsite emergency power (usually diesel generators) are considered to be separate functions by GDC-17. If either offsite power or onsite emergency power is unavailable to the plant, it is reportable regardless of whether the other system is available. GDC-17 defines the safety function of each system as providing sufficient capacity and capability, etc., assuming that the other system is not available.

Reporting of this event pursuant to 10 CFR 50.73(a)(2)(v)(D) necessitates reporting the event as a Safety System Functional Failure in the associated NRC Performance Indicator for the fourth quarter of 2009.

ROOT CAUSE:

The cause of the LOOP was initiated by a human performance error. A Westar Senior Relay Technician inadvertently closed the wrong set of failure trip links (Plant Startup (PSU) breaker failure links) on a Switchyard breaker during the Rose Hill transmission line transfer/breaker failure trip testing PM activities.

The Outage Control Center suspended Switchyard work, with the exception of concrete pads being poured. It was determined that the work on the concrete pads was not in close proximity to electrical equipment and could not create additional risk.

Actions Taken:

Power for the safety related equipment was restored from offsite power and the emergency diesel generator was shut down.

Revisions to procedure AP 21C-001, "WCGS/Westar Substation," were completed to provide for improved interface during work activities in the switchyard. Procedure revisions made included the following:

  • Requirement for direct oversight of critical work activities.
  • Requirement for a designated WCNOC person as the Switchyard Coordinator for liaison between Westar and WCNOC.
  • Requirement for Westar work orders/instructions that involve WCGS switchyard work activities contain sufficient and specific details for successful completion of the work activity.

SAFETY SIGNIFICANCE:

The Outage Control Center performed a shutdown risk assessment the morning of 4/7/2008 at approximately 0400.

This was prior to the LOOP incident. The shutdown safety risk condition for the plant was Risk condition 2. Risk condition 2 indicates a moderate risk. There is a reduction in the equipment available for satisfying a shutdown safety function because of electrical power resources and decay heat removal.

The entire core was in the Spent Fuel Pool (SFP) and the SFP water inventory was full. The plant-operating mode was de-fueled. The Reactor Coolant System (RCS) pressure was 0 psig and the RCS temperature was 75 degrees F. The SFP time to boil was greater than 8.06 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Cooling to the SFP was restored in 21 minutes and the temperature rise of the SFP during the event was 2.3 degrees F. Diverse means for SFP make-up were available during the event. The diesel fire pump and "B" essential service water pump started and ran successfully during the event.

OPERATING EXPERIENCE/PREVIOUS EVENTS:

A review of recent WCGS plant events (LERs) involving a loss of off-site power produced three events, LERs 1995­ 006-00, 1999-005-00 and 2004-003-00. The events were not similar because it was determined that one off-site source was available and both diesels were available in each event and the causes were either equipment failure or small animal intrusion related faults. LER 2009-002-00 was submitted subsequent to this event and involved a loss of off-site power due a lightening strike on the LaCygne 345 kV line and subsequent loss of the Rose Hill and Benton 345 kV lines. This event was not similar as the plant was operating in MODE 1 and the event was initiated as a result of a natural phenomenon.