05000458/FIN-2015002-01
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Finding | |
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Title | Inadequate Operating Margin for Reactor Protection System A Motor Generator Set for Overvoltage Protection Results in Loss of Shutdown Cooling |
Description | The inspectors reviewed a finding for the licensees failure to raise the overvoltage setpoint on the reactor protection system A motor generator set when the output of the generator was raised. This resulted in a reduction of the operating margin between the overvoltage trip setpoint and normal operating voltage. As a result, a spike in the output of the A motor generator on February 24, 2015, exceeded the overvoltage trip setpoint and caused the reactor protection system motor generator set output breaker to open which resulted in a loss of shutdown cooling while the reactor was shut down for refueling operations. With spent fuel in the reactor vessel, reactor coolant temperature increased 6.4 degrees until reactor protection system A was re-energized and shutdown cooling was restored. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2015-01216. The performance deficiency is more than minor, and therefore a finding, because it is associated with the Initiating Events Cornerstone attribute of configuration control, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the tripping of the reactor protection system A motor generator set output breaker, resulted in a loss of power to the reactor protection system. This subsequently caused a loss of shutdown cooling and decay heat removal while the plant was shut down for a refueling outage. The inspectors initially screened the finding in accordance with Inspection Manual Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process. The inspectors used NRC Inspection Manual 0609, Appendix G, Shutdown Operations Significance Determination Process, dated May 5, 2014, to evaluate the significance of the finding. The finding did not require a quantitative assessment because adequate mitigating equipment remained available and the finding did not constitute a loss of control, as defined in Appendix G. Therefore, the finding screened as Green. A cross-cutting aspect to this finding is not being assigned as this performance deficiency occurred in 1988 and therefore is not indicative of current licensee performance. |
Site: | River Bend |
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Report | IR 05000458/2015002 Section 4OA2 |
Date counted | Jun 30, 2015 (2015Q2) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | NRC identified |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | A Barrett B Parks G Warnick J Braisted J Jacobson J Ortega-Luciano J Sowa L Micewski R Laura |
INPO aspect | |
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Finding - River Bend - IR 05000458/2015002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (River Bend) @ 2015Q2
Self-Identified List (River Bend)
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