05000458/FIN-2015001-01
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Finding | |
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Title | Failure to Perform Adequate Operability Evaluations on Degraded High Pressure Core Spray System |
Description | The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to perform an adequate operability evaluation in accordance with Entergy Procedure EN-OP-104, Operability Determination and Functionality Assessment. Specifically, operations staff failed to properly evaluate leakage from the suppression pool through the high pressure core spray system. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2014-04004. The failure to perform an adequate operability determination for leakage from the safety-related suppression pool was a performance deficiency. This performance deficiency is more than minor, and therefore a finding, because it adversely affected the configuration control attribute of the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, a subsequent operability determination classified the suppression pool as inoperable. The inspectors used NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, to evaluate the issue. The finding required a detailed risk evaluation because it involved the potential loss of system and/or function. A Region IV senior reactor analyst performed a detailed risk evaluation for the issue. In the detailed risk evaluation, the senior reactor analyst concluded that the finding was determined to have very low safety significance (Green) because the high pressure core spray system would have remained functional for 21 days which is in excess of the probabilistic risk assessment mission time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The finding also did not screen as risk significant for large early release frequency. The finding has a cross-cutting aspect in the area of human performance associated with Challenge the Unknown: Individuals stop when faced with uncertain conditions. Risks are evaluated and managed before proceeding. Specifically, station operators, and the condition review group, failed to evaluate the condition of the suppression pool when the source of the leakage was uncertain [H.11]. |
Site: | River Bend |
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Report | IR 05000458/2015001 Section 1R15 |
Date counted | Mar 31, 2015 (2015Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.15 |
Inspectors (proximate) | A Barrett B Parks G Warnick I Anchondo J Sowa N Greene P Elkmann P Hernandez |
Violation of: | 10 CFR 50 Appendix B Criterion V |
CCA | H.11, Challenge the Unknown |
INPO aspect | QA.2 |
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Finding - River Bend - IR 05000458/2015001 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (River Bend) @ 2015Q1
Self-Identified List (River Bend)
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