05000443/LER-2012-004, Regarding Manual Actuation of the Service Water Cooling Tower

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Regarding Manual Actuation of the Service Water Cooling Tower
ML13002A050
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 12/26/2012
From: O'Keefe M
NextEra Energy Seabrook
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
SBK-L-12267 LER 12-004-00
Download: ML13002A050 (4)


LER-2012-004, Regarding Manual Actuation of the Service Water Cooling Tower
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(iv), System Actuation
4432012004R00 - NRC Website

text

NEx~eram ENERGY(

S SEA BROO K December 26, 2012 10 CFR 50.73 Docket No. 50-443 SBK-L-12267 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 Seabrook Station Licensee Event Report (LER) 2012-004-00 Manual Actuation of the Service Water Cooling Tower Enclosed is Licensee Event Report (LER) 2012-004-00. This LER reports an event that occurred at Seabrook Station on October 31, 2012. This event is being reported pursuant to the requirements of 10 CFR 50.73(a)(2)(iv)(A).

Should you require further information regarding this matter, please contact me at (603) 773-7745.

Sincerely, NextEra Energy Seabrook, LLC Mich'e-1 O'Keefe Licensing Manager cc:

NRC Region I Administrator J. G. Lamb, NRC Project Manager NRC Senior Resident Inspector NextEra Energy Seabrook, LLC, P.O. Box 300, Lafayette Road, Seabrook, NH 03874

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010)

Estimated burden per response to comply with this mandatory collection request: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear LICENSEE EVENT REPORT (LER)

Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects.resourse@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

7

3. PAGE Seabrook Station 05000443 1 OF 3
4. TITLE Manual Actuation of the Service Water Cooling Tower
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
13. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REV MONTH FACLITYNAME DOCKET NUMBER NUMBER NO.

FACILITY NAME DOCKET NUMBER 10 31 2012 2012 -

004 00 12 26 2012

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)

El 20.2201(b)

El 20.2203(a)(3)(i) 17 50.73(a)(2)(i)(C)

El 50.73(a)(2)(vii)

El 20.2201(d)

El 20.2203(a)(3)(ii)

[] 50.73(a)(2)(ii)(A)

[3 50.73(a)(2)(viii)(A)

El 20.2203(a)(1)

El 20.2203(a)(4)

El 50.73(a)(2)(ii)(B)

El 50.73(a)(2)(viii)(B)

El 20.2203(a)(2)(i)

El 50.36(c)(1)(i)(A)

El 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

10. POWER LEVEL

[] 20.2203(a)(2)(ii)

[] 50.36(c)(1)(ii)(A) 0 50.73(a)(2)(iv)(A)

El 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

El 50.36(c)(2)

El 50.73(a)(2)(v)(A)

El 73.71(a)(4)

El 20.2203(a)(2)(iv)

El 50.46(a)(3)(ii)

[E 50.73(a)(2)(v)(B)

El 73.71(a)(5) 048 El 20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

El 50.73(a)(2)(v)(C)

E] OTHER El 20.2203(a)(2)(vi)

El 50.73(a)(2)(i)(B)

El 50.73(a)(2)(v)(D)

Specify in Abstract below or in This event resulted in a valid manual actuation of the SW cooling tower and met the reporting criteria of 10 CFR 50.73(a)(2)(iv) for actuation of an emergency service water system that does riot normally run and that serves as an ultimate heat sink. The operators responded to the event in accordance with approved procedures. No adverse consequences resulted from this event, and this incident had no adverse impact on the health and safety of the public or the plant and its personnel. This event did not involve a safety system functional failure. No inoperable structures, systems, or components contributed to this event.

Corrective Actions

The corrective action for this event includes replacing the degraded spray header strainers.

Similar Events

A review of the corrective action program and previous LERs identified no similar events in the last five years.

Additional Information

The Energy Industry Identification System (EIIS) codes are included in this LEPR in the following format: [EIIS system identifier, ElIS component identifier].