05000440/LER-2019-004-01, Loss of Feedwater Heating Results in Loss of Safety Function

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Loss of Feedwater Heating Results in Loss of Safety Function
ML19310F569
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 11/06/2019
From: Payne F
FirstEnergy Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-19-251 LER 2019-004-01
Download: ML19310F569 (6)


LER-2019-004, Loss of Feedwater Heating Results in Loss of Safety Function
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v), Loss of Safety Function
4402019004R01 - NRC Website

text

FENOC FirstEnergy Nuclear Operating Company Perry Nuclear Power Plant P.O. Box 97 10 Center Road

Perry, Ohio 44081 Frank Payne 440-280-5382 Vice President November 6, 2019 L-19-251 10 CFR 50.73(a)(2)(v)(A) 10CFR50.73(a)(2)(v)(D)

ATTN:

Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555-0001

SUBJECT:

Perry Nuclear Power Plant Docket No. 50-440, License No. NPF-58 Licensee Event Report Submittal Enclosed is Licensee Event Report (LER) 2019-004-01, "Loss of Feedwater Heating Results in Loss of Safety Function".

This supplement is being submitted to update the cause analysis and corrective actions associated with this event.

There are no regulatory commitments contained in this submittal.

If there are any questions or if additional information is required, please contact Mr. Glendon Burnham, Manager - Regulatory Compliance, at (440) 280-7538.

Sincerely,

Enclosure:

LER 2019-004-01 cc:

NRC Project Manager NRC Resident Inspector NRC Region III Regional Administrator

Enclosure L-19-251 LER 2019-004-01

NRC FORM 366 (04-2018)

U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

(See Page 2 for required number of digits/characters for each block)

(See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/readinq-rm/cloc-collections/nureqs/staff/sr1022/r3/

APPROVED BY OMB:

NO. 3150-0104 EXPIRES:

3/31/2020

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. Facility Name Perry Nuclear Power Plant
2. Docket Number 05000-440
3. Page 1

OF

4. Title:

Loss of Feedwater Heating Results in Loss of Safety Function

5. Event Date
6. LER Number
7. Report Date
8. Other Facilities Involved Month Day Year Year Sequential Number Rev No.

Month Day Year Facility Name Docket Number 05000 08 06 2019 2019 004 01 11 06 2019 Facility Name Docket Number 05000

9. Operating Mode

)

El No 15.

Expected Submission Date Abstract (Limit to 1400 spaces, i.e., approximately 14 single-spaced typewritten lines)

On August 6, 2019, at 1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />, while performing feedwater heater alignments, a partial loss of feedwater heating occurred due to the isolation of the 5A and 6A feedwater heaters, resulting in lowering the temperature of feedwater to the reactor vessel by approximately 38 degrees F.

This caused the Turbine First-Stage pressure to be outside of the normal calibration value, thereby changing instrumentation setpoints, and resulting in the INOPERABILITY of Reactor Protection System (RPS) instrumentation functions for Turbine Stop Valve Closure and Turbine Control Valve Fast Closure, End of Cycle Recirculation Pump Trip (EOC-RPT) instrumentation, and Control Rod Block instrumentation.

The Direct Cause is determined to be the continued rise of water level in the heater, after the emergency drain valve reached 100% demand, actuating the high-high isolation level switch.

The apparent cause was determined to be inadequate organizational communication following a change in the feedwater heater level control tuning strategy.

A contributing cause was determined to be a lack of written guidance for Instrument and Control (I&C) technicians to perform the feedwater heater mode transfer successfully..

The increase in risk for this event is considered very small in accordance with the Regulatory Guidance.

This event is reported in accordance with 10 CFR 50.73(a)(2)(v)(A) and 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function.

NRC FORM 366 (04-2018)

Energy Industry Identification System (EMS) codes are identified in the text as [XX].

INTRODUCTION

On August 6, 2019, with the plant in Mode 1

at approximately 65 percent rated thermal power, a partial loss of high pressure feedwater heating [SN] occurred when feedwater heaters 5A and 6A [HX] isolated on high-high level during the transfer of the 5A heater level control [LC] from startup to normal mode.

In startup level control mode, the emergency drain controllers [LIC] are operating the normal drain valves [LCV] and the normal drain controllers are operating the emergency drain valves. The 5A and 6A heater isolations resulted in a lower feedwater temperature which impacted certain Reactor Protection System (RPS) [JC], End of Cycle Recirculation Pump Trip (EOC-RPT), and Control Rod Block instrumentation setpoints that are derived from the main turbine [TG] first stage pressure.

At 1729 hours0.02 days <br />0.48 hours <br />0.00286 weeks <br />6.578845e-4 months <br />, notification was made to the NRC Operations Center (Event Notification ENS 54203) in accordance with 10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to shutdown the reactor and place it in a safe condition, and mitigate the consequences of an accident.

This event is being reported in accordance with 10 CFR 50.73(a)(2)(v)(A) and 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function.

EVENT DESCRIPTION

On August 6, 2019 at 1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />, feedwater heaters 5A and 6A automatically isolated on high-high level during an attempt to transfer from startup to normal mode on the 5A heater level controller.

The transfer from startup to normal mode for the 5A heater occurred at 65 percent reactor power.

The resultant isolation of the 5A and 6A heaters lowered feedwater temperature going to the reactor by approximately 38 degrees F.

Setpoints for the RPS Turbine Stop Valve [ISV] and Control Valve [FCV] fast closure scram bypass inputs, EOC-RPT instrumentation, and Control Rod Block Rod Withdrawal Limiter (RWL) come from pressure transmitters [PT] located on each of the turbine first-stage pressure taps.

While in the power range of the reactor, turbine first stage pressure is essentially linear with increasing power.

When the main turbine first-stage pressure is below that equivalent to 38 percent of rated thermal power; trip units [PM] in each RPS channel actuate relays [RLY] to bypass the. Turbine Stop Valve and Control Valve closure scrams, the EOC-RPT function is enabled, and the Control Rod Block RWL is bypassed.

With a lower than normal turbine first-stage pressure due to an abnormal feedwater temperature, the relation of the main turbine first-stage pressure to reactor power is no longer in calibration; therefore, the setpoint for percent reactor thermal power at which the bypass functions occur will not be correct.

Operators entered into Limiting Conditions of Operation (LCO) for Technical Specifications (TS) 3.3.1.1, RPS Instrumentation Channels A, B, C, D, E, F, G, and H for Turbine Stop Valve Closure; TS 3.3.1.1, RPS

Instrumentation Channels A, B, C, and D for Turbine Control Valve Fast Closure, Trip Oil Pressure Low; TS 3.3.4.1, End of Cycle Recirculation Pump Trip (EOC-RPT) Instrumentation; and TS 3.3.2.1, Control Rod Block Instrumentation for Rod Withdrawal Limiter (RWL).

According to procedure ONI-N36, Loss of Feedwater Heating, Attachment 3 specifies that compliance with one of the following four actions is required for unplanned reductions in feedwater temperature:

Restore the feedwater temperature within the TS action time(s)

Disable the bypass by removing the four trip units (C71-N652A, B, C, D) for RPS and EOC-RPT.

Implement setpoint changes for the trip units within the TS action time(s)

Reduce power to </= 38 percent within the TS Action Time(s)

At 1422 hours0.0165 days <br />0.395 hours <br />0.00235 weeks <br />5.41071e-4 months <br />, the four trip units were removed to disable the bypass function and obtain compliance with the TS action time to restore Operability.

At 1631 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.205955e-4 months <br /> feedwater heaters 5A and 6A were restored to service, and at 1915 hours0.0222 days <br />0.532 hours <br />0.00317 weeks <br />7.286575e-4 months <br /> the trip units were reinstalled to re-enable the bypass function.

CAUSE OF EVENT

The Direct Cause was determined to be the continued rise of water level in the heater, after the emergency drain valve reached 100% demand, actuating the high-high isolation level switch.

The Apparent Cause was determined to be inadequate organizational communication.

A change in the feedwater heater level control tuning strategy resulted in reduced operational flexibility for transferring feedwater heater drain controls with no compensatory changes in procedures or practices.

The 5A feedwater heater normal controller is tuned for steady state operations with the intent to dampen heater level oscillations at 100 percent reactor power.

With this tuning strategy, the ability of Operations to perform the transfer from emergency control to normal control at greater than 62 percent reactor power is restricted.

Additionally, no mitigating action, such as lowering feedwater heater water level prior to performing the transfer, was identified.

A contributing cause was determined to be a lack of written guidance for the Instrument and Control (I&C) technicians that provides guidelines for performing the feedwater heater transfers successfully.

EVENT ANALYSIS

A Probabilistic Risk Assessment (PRA) evaluation was performed for the August 6, 2019 loss of feedwater heating. A conservative analysis of this event results in delta Core Damage Frequency (CDF) and delta Large Early Release Frequency (LERF) values that are well below the acceptable thresholds discussed in Regulatory Guide 1.174. The increase in risk for this event is therefore considered very small in accordance with the Regulatory Guidance.

This event is being reported in accordance with 10 CFR 50.73(a)(2)(v)(A)

and 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function.

CORRECTIVE ACTIONS

Feedwater heater 5A was successfully returned to service on the normal level controller and functioned as expected.

Operations will revise procedure IOI-0003, Power Changes, to move a current caution note that states, "Do not exceed 62% reactor power until Heaters 5A and 5Bj normal drain controllers are operating the normal drain valves and Heaters 5A and 5B emergency drain controllers are operating the emergency drain valves."

The caution note will be moved to prior to the step directing the transfer from the emergency to the normal drain controllers.

Included in the caution note will be the following: transferring from emergency drain to normal drain can cause heater level oscillations and an isolation; lowering heater level setpoints is recommended prior to performing this task; and removal of the trip units specified in ONI-N36, Attachment 3, to preclude the loss of safety function in the event of a feedwater heater isolation.

Additionally, I&C will develop a procedure to incorporate lessons learned from this event to aid the I&C technicians in performing feedwater heater mode transfer successfully.

Lessons learned will include lowering heater water level prior to performing the transfer and ensuring reactor power level is acceptable prior to performing the task.

PREVIOUS SIMILAR EVENTS

A review of LERs and the corrective action database for the past three years identified no similar events.(04-2018)