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NRCFarm 300 U.S. NUCLE 12 LEZULATL;dY COMMIS$80N APPROVED OMS NO.2190 4104 LICENSEE EVENT REPORT (LER)
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Perry Nuclear Power Plant, Unit 1 015 l 01010 l41410 1 lOFl014 Reactor Scram Results From Intermediate Range Neutron Monitors Upscale Trip Due To Excessive Feedwater Flow Uith Manual Control Of A Turbine Driven Feedwater Pump EVENT DATE 15)
LER NUMBER ($1 REPORT DATE (7)
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TELEPHONE NUMSER NAME AREA CODE Gregory A. Dunn, Compliance Engineer, Extension 6484 2 l 116 215 l 91-13171317 COMPLETE ONE LINE FOR EACH COMPONEst7 P AILURE DERCRISIO IN THis REPORT (13)
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On January 3, 1988 at 0630, a reactor scram occurred due to an upscale trip on the Intermediate Range Neutron Monitors (IRM). The scram was a result of excessive feedwater injection into the reactor vessel while plant operators were adjusting the manual speed control potentiometer for the B Turbine Driven Feedwater Pump (TDFP) turbine.
The causes of the event were instruction inadequacy and design deficiency.
Integrated Operating Instruction (101)-4 " Shutdown" did not provide adequate guidancc and a proper sequence for feedwater control during a plant shutdown with a TDFP. The TDFP minimum flow valves are undersized making manual control j
l of the TDFP necessary during low flow conditions. The Low Flow Controller provides very little overlap with the Startup Level Controller and therefore, was not being used during this event.
In order to prevent recurrence 101-4 has been revised to include specific guidance for feedwater control during shutdown when the Motor Driven Feedwater Pump is unavailable. The total flow capacity through the Low Flow Control
.I Valve will be increased in order to provide greater overlap with the Startup Level Controller. The low speed stop for the TDFPs when on the Startup Level Controller will be lowered. Additionally, the TDFP manual speed controllers will be changed to reduce the sensitivity and provide better control.
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8s4C P.rne 308A U.S. NUCLEA3 E EIULATG4Y COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Arenovfo ous No. atso-oso.
EXPIRES: t/31/N FActLITV esAaAE Hi DOCKET NUMBER (2)
LER NUMSER (6)
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i Perry Nuclear Power Plant, Unit 1 0 l5 l0 l0 l0 l4 l4 l0 8l 8 010l1 0l 1 42 OF 0 l4 I
swimm maw.v, mumma. macr amuun on January 3, 1988 at 0630, a reactor scram occurred due to an upscale trip on the Intermediate Range Neutron Monitors (IRM) [IG).
Prior to the event,.the plant was in Operational Condition 2 (Startup), conducting a reactor shutdown for a planned maintenance outage. Reactor thermal power was less than 1.0 percent of rated with reactor vessel [RPV] pressure approximately 800 psig.
At approximately 0100 a plant shutdown was commenced for a planned maintenance outage. The Motor Driven Feedwater Pump (MFP) [SJ) and the B Turbine Driven P
Feedwater Pump (TDFP) were in operation at the time, the A TDFP was out of service for repairs. At 0259 the MFP was secured when reactor power was decreased to approximately 40 percent. At 0414 the B TDFP was placed on the Startup Level Controller in automatic.
Operational Condition 2 was entered at 0550 and reactor vessel pressure was decreasing at a rate of approximately 7 psi per minute. As the feed demand.
signal decreased the Startup Level Controller reached its minimum output and the B TDFP discharge pressure remained steady at approximately 865 psig. At approximately 0625 reactor vessel level began to increase as reactor pressure decreased below the B TDFP discharge pressure. The operator at the controls placed the Startup Level Controller in manual and attempted to reduce the B TDFP turbine speed. When this was unsuccessful, the B TDFP control was transferred to the manual potentiometer and turbine speed reduced, subsequently causing reactor vessel level to decrease. Preparations for starting the MFP were commenced. However, the MFP was not immediately available due to the lube oil temperature having decreased below the minimum required for pump start.
y At 0629 a second operator was directed to increase the B TDFP turbine speed to compensate for decreasing reactor vessel level. A first adjustment was not large enough to overcome reactor pressure and start feedwater flow. A second increase on the manual potentiometer was made and flow to the reactor vessel commenced. The injection of cold eater caused a power surge and the IRMs began N
to increase. The operator at the controls attempted to range-up the IRMs to
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avoid the upscale trip but was unable to range-up all of the IRMs rapidly J
enough and at 0630 IRM channels B and C reached the upscale trip causing a reactor scram.
The operators performed the required actions of Off Normal Instruction (ONI)-C71 " Reactor Scram (Unit 1)" to place the plant in a stable condition.
At 0642 the MFP was started and placed on the Startup Level Controller to maintain reactor vessel level. The 3 TDFP was secured. The transient analysis was completed and approval to restart was granted by the Plant Manager on January 5.
The plant entered Operational Condition 2 on January 27 following; completion of the planned maintenance.
The causes of the event were instruction inadequacy and design deficiency.
Integrated Operating Instruction (101)-3 " Power Changes" and 101-4 "Shutdowr" did not provide adequate guidance to utilize the MFP, whenever available, for plant shutdown. 101-4 also failed to provide a proper sequence for feedwater control when the MFP is unavailable.
By making the decision to use the B TDFP and without other guidance, the operators were ultimately required to use manual potentiometer turbine speed adjustment for feedwater flow control. This
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NAC Perm mea U.S. NUCLEA:t KEIULATEY COMMMON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Armovfo cus =o. stso-oio4 EXPIRES: 8/31/N PACILITY NAMG til DOCKET NUMBER (21 ggg gygggg gg3 pggg gg, AR 0 ' $$,
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.emmumace== mumm method of feedwater control is extremely sensitive and has no feedback to dampen changes.
The Startup Level Controller and the Low Flow controller do not provide adequate overlap for easy transition from one mode of Feedwater control to the other. Manual control of the TDFP is required when reactor pressure decreases below 850 psi due to the flow capacity of the TDFPs minimum flow valves. The maximum flow through the TDFPs minimum flow valves is less than the minimum flow for the Startup Level Controller in automatic. If the capacity of the minimum flow valves was greater, the IDFP controlled by the Startup Level Controller could be utilized to reduce feedwater flow to the reactor vessel to zero.
The Low Flow Controller is utilized to control feedwater flow to the reactor vessel by establishing 100 psi differential pressure across the Low Flow Centrol Valve and throttling the valve to provide the required flow. This method of feedwater control provides the ability to more easily change flow in small incremental steps. However, the maximum capacity of the Low Flow Control Valve is approximately 800 gpm due to the limited span on the Low Flow Controller which allows very little overlap with the Startup Level Controller and therefore, was not being used during this event.
Reactor power level was low during this event and the resulting thermal transient was small. Plant systems responded to the plant transient as designed to maintain the plant in a safe condition. For high power levels, FSAR section 15.1.1 analyzed the Loss of Feedwater Heating as the limiting transient which leads to the reactor vessel receiving cooler feedwater flow.
The high neutron flux scram is the mitigating system and is designed to be single failure proof. Therefore, this event is considered to have no safety significance.
l A previous similar event occurred November 26, 1986 when a reactor scram f
occurred due to an upscale trip on the IRMs (LER 86-086). The scram was a-result of excessive feedwater injection into the reactor vessel during a plant startup while operators were adjusting the Manual Flow Controller of the TDFP A in preparation to transfer feedwater supply over from the MFP. The operator at the controls failed to recognize the magnitude of increasing feedwater flow and the increase in reactor vessel level while adjusting the TDFP A Manual Flow Controller. In response to the event all on-shift licensed operators received training regarding the operation of the Feedwater Control system and the i
sequence of events involved in this reactor scram. A contributing cause to the error was a lack of necessary precautions in the Feedwater Control system operating instruction. This instruction has been revised to caution the operator to ensure sufficient stabilization time is provided while performing controller adjustments.
l In order to prevent recurrence, specific guidance has been provided in 101-3 and 101-4 to utilize the MFP, whenever available, during plant shutdown ar.d steps added to provide a sequence for feedwater control when the MFP is unavailable.
mac r== toen u.s. mucLEAusiutuiny commiscion LICEN EE EVENT REPORT (LER) TEXT CONTINUATION Arenovio ous no. siso-oio..
EXPIRES: 8/31/W F M M 09 DOCKET NUMBER W LtR NuMSER 14)
PAGE (3)
0l 1 0 l3 OF 0 l4 Perry Nuclear Power Plant, Unit I o l5 l0 lo j o l4 l4 l0 8l8 0 l0 l 1 verma== s-emmess
.nonewance==asmewnn An engineering evaluation was conducted to consider various options available to provide greater overlap of feedwater flow control between the Startup Level Controller and the Low Flow Controller. Either the flow to the reactor vessel when using the Startup Level Controller must be reduced or the flow through the Low Flow Controller must be increased in. order to provide the overlap. The Low Flow Controller will be recalibrates to increase the span allowing up to 2000 gpm flow through the Low Flow Control Valve. The low speed stop for the TDFPs when on the Startup Level Controller will be lowered which will allow the Startup Level Controller to control feedwater flow at a lower rate to the reactor vessel. Additionally, the TDFP manual speed controllers will be changed to reduce the sensitivity by installing a potentiometer with a greater number of turns.
It has been determined that with the above changes, increasing the size of the TDFP minimum flow valves is not necessary to provide adequate overlap between the Startup Level Controller and the Low Flow Controller.
Energy Industry Identification System Codes are identified in the text as [XX].
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| 05000440/LER-1988-001, :on 880103,reactor Scram Occurred Due to Upscale Trip on intermediate-range Neutron Monitors.Caused by Excessive Feedwater Injection Into Reactor Vessel While Adjusting Potentiometer.Low Speed Stop Lowered |
- on 880103,reactor Scram Occurred Due to Upscale Trip on intermediate-range Neutron Monitors.Caused by Excessive Feedwater Injection Into Reactor Vessel While Adjusting Potentiometer.Low Speed Stop Lowered
| | | 05000440/LER-1988-005, :on 880107,reactor Protection Sys Bus Power Supply Transfer Resulted in RHR Shutdown Cooling Isolation. Caused by Personnel Error.Operating Personnel Counseled & Plant Instructions Will Be Enhanced |
- on 880107,reactor Protection Sys Bus Power Supply Transfer Resulted in RHR Shutdown Cooling Isolation. Caused by Personnel Error.Operating Personnel Counseled & Plant Instructions Will Be Enhanced
| | | 05000440/LER-1988-006, :on 880119,reactor Protection Sys (RPS) B Motor Generator Set Output Circuit Breaker Tripped Open on Overvoltage,Resulting in Div II balance-of-plant Isolation. Caused by Small Random Disturbances in RPS Bus Voltage |
- on 880119,reactor Protection Sys (RPS) B Motor Generator Set Output Circuit Breaker Tripped Open on Overvoltage,Resulting in Div II balance-of-plant Isolation. Caused by Small Random Disturbances in RPS Bus Voltage
| | | 05000440/LER-1988-007, :on 880122,reactor Protection Sys Actuation Occurred Due to High Scram Discharge Vol Level.Caused by Personnel Error.Personnel Involved Counseled on Need to Perform More Thorough Review |
- on 880122,reactor Protection Sys Actuation Occurred Due to High Scram Discharge Vol Level.Caused by Personnel Error.Personnel Involved Counseled on Need to Perform More Thorough Review
| | | 05000440/LER-1988-008, :on 880123,unexpected Partial Div 2 NSSS Balance of Plant Isolation Occurred.Caused by Deficiency Involving Testability of Equipment.Review of Surveillance Instructions Performed |
- on 880123,unexpected Partial Div 2 NSSS Balance of Plant Isolation Occurred.Caused by Deficiency Involving Testability of Equipment.Review of Surveillance Instructions Performed
| | | 05000440/LER-1988-009, :on 880227,APRM Readings Misadjusted During Channel Calibr Surveillance Instruction.Caused by Error in Heat Balance Calculation.Surveillance Instruction Revised to Include Check of Heat Balance Calculation |
- on 880227,APRM Readings Misadjusted During Channel Calibr Surveillance Instruction.Caused by Error in Heat Balance Calculation.Surveillance Instruction Revised to Include Check of Heat Balance Calculation
| | | 05000440/LER-1988-010, :on 880310 & 11,RWCU Containment Isolations Occurred Due to Pump Room High Differential Temp.Caused by Inadequate Instructions.Roughing Filters in HVAC Sys AB Replaced |
- on 880310 & 11,RWCU Containment Isolations Occurred Due to Pump Room High Differential Temp.Caused by Inadequate Instructions.Roughing Filters in HVAC Sys AB Replaced
| | | 05000440/LER-1988-011, :on 880404,Train 1A of Diesel Generator Bldg Ventilation Sys for Diesel Generator Unexpectedly Started. Caused by Momentary Decrease in Control Tachometer Indication.Extensive Troubleshooting Performed |
- on 880404,Train 1A of Diesel Generator Bldg Ventilation Sys for Diesel Generator Unexpectedly Started. Caused by Momentary Decrease in Control Tachometer Indication.Extensive Troubleshooting Performed
| | | 05000440/LER-1988-012, :on 880427,automatic Reactor Scram Occurred Due to Reactor Water Level of Less than Level 3.Caused by Personnel Error & Procedural Inadequacy.Operators Involved Counseled & Sys Operating Instructions Revised |
- on 880427,automatic Reactor Scram Occurred Due to Reactor Water Level of Less than Level 3.Caused by Personnel Error & Procedural Inadequacy.Operators Involved Counseled & Sys Operating Instructions Revised
| | | 05000440/LER-1988-013, :on 880427,RWCU Sys Containment Isolation Occurred.Caused by Increase in Differential Flow Trip Setpoint &/Or Time Delay.Condition Under Evaluation & RWCU Flow Control Valves Engineering Design Change Initiated |
- on 880427,RWCU Sys Containment Isolation Occurred.Caused by Increase in Differential Flow Trip Setpoint &/Or Time Delay.Condition Under Evaluation & RWCU Flow Control Valves Engineering Design Change Initiated
| | | 05000440/LER-1988-014, :on 880428,reactor Protection Sys (RPS) Actuation Occurred on Reactor Vessel High Level.Caused by Failure of Contacts to Close in Bypass Relay for RPS Channel A.Relay Replaced & Tested & Old Relay Returned for Analysis |
- on 880428,reactor Protection Sys (RPS) Actuation Occurred on Reactor Vessel High Level.Caused by Failure of Contacts to Close in Bypass Relay for RPS Channel A.Relay Replaced & Tested & Old Relay Returned for Analysis
| | | 05000440/LER-1988-015, :on 880430,reactor Scram Occurred Due to Reactor Water Level of Less than Level 3.Caused by Procedural Deficiency.Operating Procedure Revised,Operators Involved Counseled & Operators Trained Re Events Sequence |
- on 880430,reactor Scram Occurred Due to Reactor Water Level of Less than Level 3.Caused by Procedural Deficiency.Operating Procedure Revised,Operators Involved Counseled & Operators Trained Re Events Sequence
| | | 05000440/LER-1988-016, :on 880504,unexpected RWCU Containment Isolation Occurred Due to Pump Room High Differential Temp. Caused by Personnel Error.Caution Added to Repetitive Task for Calibr of Time Delay for Fan a Trip Relay |
- on 880504,unexpected RWCU Containment Isolation Occurred Due to Pump Room High Differential Temp. Caused by Personnel Error.Caution Added to Repetitive Task for Calibr of Time Delay for Fan a Trip Relay
| | | 05000440/LER-1988-017, :on 880506,unexpected Scram of Group 3 Control Rods During Monthly Reactor Protection Sys Channel Test Occurred.Cause Not Readily Identified.Blown Fuse Replaced & Current & Voltage Monitored While Testing |
- on 880506,unexpected Scram of Group 3 Control Rods During Monthly Reactor Protection Sys Channel Test Occurred.Cause Not Readily Identified.Blown Fuse Replaced & Current & Voltage Monitored While Testing
| | | 05000440/LER-1988-018, :on 880505,investigation Determined That Elevation Changes Performed in Apr 1987 Failed to Result in Corrections to Test Instructions of Instrument Recalibrs. Caused by Personnel Error.Surveillance Instruction Revised |
- on 880505,investigation Determined That Elevation Changes Performed in Apr 1987 Failed to Result in Corrections to Test Instructions of Instrument Recalibrs. Caused by Personnel Error.Surveillance Instruction Revised
| | | 05000440/LER-1988-019, :on 880515,trains of Control Room Heating, Ventilation & Air Conditioning Declared Inoperable for Emergency Circulation Mode.Caused by Mechanical Failure of Compressor Guide Vane Linkage Connector |
- on 880515,trains of Control Room Heating, Ventilation & Air Conditioning Declared Inoperable for Emergency Circulation Mode.Caused by Mechanical Failure of Compressor Guide Vane Linkage Connector
| | | 05000440/LER-1988-020, :on 880605,reactor Scram Occurred Due to High APRM Neutron Flux Levels.Caused by Personnel Error.Automatic Mode of Flux Control Disabled Until Adjustments Completed & Personnel Involved Disciplined |
- on 880605,reactor Scram Occurred Due to High APRM Neutron Flux Levels.Caused by Personnel Error.Automatic Mode of Flux Control Disabled Until Adjustments Completed & Personnel Involved Disciplined
| | | 05000440/LER-1988-021, :on 880606,reactor Protection Sys Distribution Bus a Inadvertently Deenergized.Caused by Personnel Error. Operator Counseled & Disciplinary Action Taken to Sharpen Awareness & Increase Attention to Detail |
- on 880606,reactor Protection Sys Distribution Bus a Inadvertently Deenergized.Caused by Personnel Error. Operator Counseled & Disciplinary Action Taken to Sharpen Awareness & Increase Attention to Detail
| | | 05000440/LER-1988-022, :on 880607,0226 & 0530,Tech Specs Violated When Operation Change Completed Prior to Meeting All Applicable Tech Specs Surveillance Requirements.Caused by Personnel Error.Licensed Operators Will Be Trained in Event |
- on 880607,0226 & 0530,Tech Specs Violated When Operation Change Completed Prior to Meeting All Applicable Tech Specs Surveillance Requirements.Caused by Personnel Error.Licensed Operators Will Be Trained in Event
| | | 05000440/LER-1988-023, :on 880608 & 871027,reactor Scram & Containment Isolation Occurred on Loss of Electrical Distribution Busses Due to Inadvertent Breaker Operation.Caused by Personnel Error.Operator Counseled & Disciplinary Action Taken |
- on 880608 & 871027,reactor Scram & Containment Isolation Occurred on Loss of Electrical Distribution Busses Due to Inadvertent Breaker Operation.Caused by Personnel Error.Operator Counseled & Disciplinary Action Taken
| | | 05000440/LER-1988-024, :on 880616,spurious Spike in Recirculation Flow Demand Caused Increased Core Flow Resulting in Upscale Neutron Flux Trip & Subsequent Reactor Scram.Caused by Reinsertion of Automatic Flux Control Card |
- on 880616,spurious Spike in Recirculation Flow Demand Caused Increased Core Flow Resulting in Upscale Neutron Flux Trip & Subsequent Reactor Scram.Caused by Reinsertion of Automatic Flux Control Card
| | | 05000440/LER-1988-025, :on 880618,overtravel of Reactor Protection Sys (RPS) Power Transfer Switch Occurred,Resulting in Loss of Power to Both Busses & Full RPS Actuation.Caused by Personnel Error.Info Tag Installed & Design Change Planned |
- on 880618,overtravel of Reactor Protection Sys (RPS) Power Transfer Switch Occurred,Resulting in Loss of Power to Both Busses & Full RPS Actuation.Caused by Personnel Error.Info Tag Installed & Design Change Planned
| | | 05000440/LER-1988-026, :on 880623,reactor Scram Occurred Due to Unexpected Turbine Trip.Caused by Mechanical Failure of Trip Latch Assembly.Defective Parts Replaced & Proper Clearances within Mechanism Established by Machining Various Surfaces |
- on 880623,reactor Scram Occurred Due to Unexpected Turbine Trip.Caused by Mechanical Failure of Trip Latch Assembly.Defective Parts Replaced & Proper Clearances within Mechanism Established by Machining Various Surfaces
| | | 05000440/LER-1988-027, Forwards LERs 88-026 & 88-028.LER 88-027 Will Be Forthcoming | Forwards LERs 88-026 & 88-028.LER 88-027 Will Be Forthcoming | | | 05000440/LER-1988-028, :on 880623,trains of Control HVAC Shifted Into Emergency Recirculation Mode Due to High Toxic Gas Signals. Caused by Heavy Black Smoke Exhausting from Auxiliary Boiler.Affected Ethylene Oxide Detectors Recalibr |
- on 880623,trains of Control HVAC Shifted Into Emergency Recirculation Mode Due to High Toxic Gas Signals. Caused by Heavy Black Smoke Exhausting from Auxiliary Boiler.Affected Ethylene Oxide Detectors Recalibr
| | | 05000440/LER-1988-029, :on 880812,standby Liquid Control Pump B Suctional Manual Isolation Valve Inadvertently Left Closed Resulting in Trains Being Inoperable.Caused by Personnel Error.Counseling Session Will Be Held |
- on 880812,standby Liquid Control Pump B Suctional Manual Isolation Valve Inadvertently Left Closed Resulting in Trains Being Inoperable.Caused by Personnel Error.Counseling Session Will Be Held
| | | 05000440/LER-1988-030, :on 880823,offgas Pretreatment Sample Not Taken & Analyzed,Per Tech Spec 3.3.7.1.Caused by Personnel Error. Procedure Change Requiring Technicians to Review Daily Limiting Condition for Operations Implemented |
- on 880823,offgas Pretreatment Sample Not Taken & Analyzed,Per Tech Spec 3.3.7.1.Caused by Personnel Error. Procedure Change Requiring Technicians to Review Daily Limiting Condition for Operations Implemented
| | | 05000440/LER-1988-031, :on 880220,quarterly Surveillance Instruction Removing Water from Div 2 & 3 Fuel Oil Storage Tanks Missed. Caused by Personnel Error.Procedure Will Be Changed to Enhance Communications Between Reviewers & Coordinators |
- on 880220,quarterly Surveillance Instruction Removing Water from Div 2 & 3 Fuel Oil Storage Tanks Missed. Caused by Personnel Error.Procedure Will Be Changed to Enhance Communications Between Reviewers & Coordinators
| | | 05000440/LER-1988-032, :on 880826,failure of Ball Valve & Door Seal Result in Inoperable Containment Airlock Doors & Momentary Loss of Containment Integrity While Technician Exits Containment.Work Orders Will Be Initiated |
- on 880826,failure of Ball Valve & Door Seal Result in Inoperable Containment Airlock Doors & Momentary Loss of Containment Integrity While Technician Exits Containment.Work Orders Will Be Initiated
| | | 05000440/LER-1988-033, :on 880901,RCIC Sys Inboard Containment Isolation Occurred.Caused by Leak Detection Transmitter Failure Due to Internal Short Circuit Between Diaphragm & Capacitor Plate.Transmitter Replaced |
- on 880901,RCIC Sys Inboard Containment Isolation Occurred.Caused by Leak Detection Transmitter Failure Due to Internal Short Circuit Between Diaphragm & Capacitor Plate.Transmitter Replaced
| | | 05000440/LER-1988-034, :on 880903,unexpected Automatic Start of Div 1 Diesel Generator Bldg Ventilation Sys Occurred.Caused by Failure of 125/24-volt Dc Converter in Control Circuitry. Converter Replaced & Retests Satisfactorily Performed |
- on 880903,unexpected Automatic Start of Div 1 Diesel Generator Bldg Ventilation Sys Occurred.Caused by Failure of 125/24-volt Dc Converter in Control Circuitry. Converter Replaced & Retests Satisfactorily Performed
| | | 05000440/LER-1988-035, :on 880914,primary Containment Integrity Was Compromised for 30 in That Upper Containment Airlock Inner Door Seals Were Deflated W/Outer Door Open.Caused by Failure of Door Interlock.Engineering Evaluation Initiated |
- on 880914,primary Containment Integrity Was Compromised for 30 in That Upper Containment Airlock Inner Door Seals Were Deflated W/Outer Door Open.Caused by Failure of Door Interlock.Engineering Evaluation Initiated
| | | 05000440/LER-1988-036, :on 880917,Channels B & D of MSIV Low Condenser Vacuum Isolation Instrumentation Declared Inoperable.Caused by Debris/Water Intrusion Into Instrument Lines.Instrument Lines Will Be Cleared on Monthly Basis |
- on 880917,Channels B & D of MSIV Low Condenser Vacuum Isolation Instrumentation Declared Inoperable.Caused by Debris/Water Intrusion Into Instrument Lines.Instrument Lines Will Be Cleared on Monthly Basis
| | | 05000440/LER-1988-038, :on 880911,control Rods Inserted in Violation of Tech Spec 3.1.4.2, Reactivity Control Sys. Caused by Procedural Deficiency.Integrated Operating Instruction Revised & Event Reviewed During Training |
- on 880911,control Rods Inserted in Violation of Tech Spec 3.1.4.2, Reactivity Control Sys. Caused by Procedural Deficiency.Integrated Operating Instruction Revised & Event Reviewed During Training
| | | 05000440/LER-1988-039, :on 880928,RWCU Sys Containment Isolation Occurred During Plant Startup When Feedwater Flow to Reactor Initiated.Caused by Indicated High Differential Flow.Design Change to Replace RWCU Initiated |
- on 880928,RWCU Sys Containment Isolation Occurred During Plant Startup When Feedwater Flow to Reactor Initiated.Caused by Indicated High Differential Flow.Design Change to Replace RWCU Initiated
| | | 05000440/LER-1988-040, :on 881007,train B of Control Room HVAC Sys Inoperable for Emergency Recirculation Mode W/Train a out-of-svc for Planned Maint.Caused by Degradation of Wire Insulation.Control Wiring & Actuator Replaced |
- on 881007,train B of Control Room HVAC Sys Inoperable for Emergency Recirculation Mode W/Train a out-of-svc for Planned Maint.Caused by Degradation of Wire Insulation.Control Wiring & Actuator Replaced
| | | 05000440/LER-1988-041, :on 881013,RCIC Sys Inboard Containment Isolation Occurred Due to Leak Detection (Ld) Transmitter Failure.Caused by Internal Short Circuit Between Ctr Diaphragm & Low Side Capacitor Plate.Evaluation Underway |
- on 881013,RCIC Sys Inboard Containment Isolation Occurred Due to Leak Detection (Ld) Transmitter Failure.Caused by Internal Short Circuit Between Ctr Diaphragm & Low Side Capacitor Plate.Evaluation Underway
| | | 05000440/LER-1988-042, :on 881021,reactor Protection Sys Actuation Occurred Due to APRM Channel Exceeding Neutron flux-high Setdown Trip Setpoint.Caused by Local Power Range Monitor Failure.Failed Channel Removed from Svc |
- on 881021,reactor Protection Sys Actuation Occurred Due to APRM Channel Exceeding Neutron flux-high Setdown Trip Setpoint.Caused by Local Power Range Monitor Failure.Failed Channel Removed from Svc
| | | 05000440/LER-1988-043, :on 881030,HPCS Pump Room Cooler Inadvertently Started During Performance of Breaker Retest.Caused by Procedural Deficiency.Retest Guidelines Will Be Added to Generic Electrical Instructions for Maint |
- on 881030,HPCS Pump Room Cooler Inadvertently Started During Performance of Breaker Retest.Caused by Procedural Deficiency.Retest Guidelines Will Be Added to Generic Electrical Instructions for Maint
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