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10 CPR 50.73 PHILADELPHIA ELECTRIC COMPANY LIMERICK GENER ATING ST ATION P. O.DO X A SAN ATOG A, PENNSYLV ANI A 19464 Docket Nos. 50-352 (216) 3271200 ext. 2000 50-353 u. t ucconu;c q.ja., (c.
License Nos. NPF-39 NPF-85
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U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
SUBJECT:
Licensee Event Report Limerick Generating Station - Units 1 and 2 I
This LER reports various Engineered Safety Feature actuations resulting from a spurious Division 1 Loss of Coolant Accident (LOCA) signal.
The spurious LOCA signal occurred while an Instrumentation and Controls technician was performing an incorrect surveillance test procedure.
Reference:
Docket Nos. 50-352 50-353 Report Number:
1-90-025 Revision Number:
0 Event Date:
November 10, 1990 Report Date:
December 7, 1990 Facility:
Limerick Generating Station P.O.
Box A, Sanatoga, PA 19464 This LER is being submitted pursuant to the requirements of 10 CPR 50.73(a)(2)(iv).
Very truly yours, y
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LICENSEE EVENT REPORT (LER)
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.On November 10, 1990, with Unit 1 in a refueling outage, an Instrumentation and Controls (I&C) technician was performing Surveillance-Test (ST) procedure ST-2-036-680-1, "Drywell Pressure Transmitter Sensing Line Blowback Procedure."
A
- - spurious Division 1 Loss of Coolant Accident (LOCA) signal occurred when he opened the LO side isolation valve to restore differential pressure switch PDS-59-106A.
Trapped pressurized air was then released down the instrument line when the LO side and two drywell pressure transmitters sensed the high pressure and initiated the LOCA signal.
The spurious LOCA signal caused automatic actuations of.a number of Engineered Safety Features which functioned as designed.
The actuations included a start of the
'lA' Core Spray (CS) pump with injection, opening of the lA' Low Pressure Coolant. Injection valve, a start of the Dll Emergency Diesel Generator, and tripping of the
'0A' Residual Heat Removal Service Water pump.
The consequences of this event were minimal.
Reactor' vessel inventory increased approximately 8 inchee due to the CS injection and reactor coolant temperature increased approximately 3 degrees due to termination of the shutdown cooling function The cause of the event was an incorrect procedure.
The I&C technician correctly performed the procedure as written.. The procedure will be revised to prevent similar future occurrencese A warning label will also be added to PDS-59-106A, PDS-59-106B, PDS-59-206A, and PDS-59-206B to alert I&C technicians of their unusual valving sequence, y,C,,,
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F tlCENSEE EVENT REPORT (LER) TEXT CONTINUATION no e o e c so.o t apintt 1,3146
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- - ne w au e nn Unit Conditions Prior to the Event:.
Unit 1 Operating Condition was 5 (Refueling) at 0% power level with the Reactor Pressure Vessel (RPV) pressure at 0 psig and the reactor cavity water level at 202 inches or 363.-Inches above the top of" active fuel.
Unit 2 Operating Condition was'l (Power Operation) at 100% power
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level.
The
'lA' Residual Heat Removal (RHR) system (EIIS BO) was in service in the shutdown cooling mode of operation.
The common
'OA' Residual' Heat Removal Service Water (RHRSW) system (EIIS:BI) pump was also in service providing shutdown-cooling to Unit 1.
There were,no structures, systems or components out of service which contributed to this event.
~
' Description of the Event:
On-November 10,-1990, a: contractor employed Instrumentation and Controls (I&C) technician was performing Unit 1 Surveillance Test
-(ST) procedure ST-2-036-680-1,-"Drywell Pressure l Transmitter Sensing Line Blowback Procedure."
At 2232 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.49276e-4 months <br /> he opened the LO side isolation valve to restore differential pressure switch-
'PDS-59-106A (see Figure 1) which resulted in a spurious Division 1 foss of Coolant-Accident _(LOCA)-signal.
The spurious LOCA r
sisnalcoccurred.when greater than-1.68 psig was-momentarily sensed by pressure transmitters PT-42-1N094A and PT-42-lN094E along -with the-RPV pressure below :455 psig.
A half scram signal was also generated by pressure, transmitter PT-42-lN050A due-to
- - the spurious high drywell-pressure condition. _Various Engineered Safety Feature (ESP) actuations were initiated.in addition to
- - control room' annunciation.
The Division'l LOCA-signal caused the following-automatic actions, as designed:
'lA' Core Spray (CS) (EIIS:BM) pump started =and injected suppression pool water into'the RPV,-
'lA' Low Pressure Coolant _ Injection (LPCI) injection value opened, D11/ Emergency Diesel Generator (EDG) (EIIS:EK)Estarted and the 1 associated Division 1 AC Safeguard power bus load shed occurred, and-
' Common '0A' Emergency. Service Water (ESW) '(EIIS:BI) pump started.
The load shed' caused the
'0A' RHRSW pump to trip.
Operators verified that the_ Division 1 LOCA signal was spurious, secured the
'1A' CS pump to terminate the RPV injection, closed the
'1A' LPCI--injection valve, and realigned the
'1A' RHR system to the
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ov o o e o n im ami w ast weasta m pocius,v s.anse 416 Lin 4ta.ef s tai
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ma Limerick cenerating station 0l0 0 l3 or 0l 5 o
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The D11 EDG and
'OA' ESW pump were then secured.
Operators also reset the LOCA signal.
At 2248 hours0.026 days <br />0.624 hours <br />0.00372 weeks <br />8.55364e-4 months <br /> operators started the 'OC' RHRSW pump in the
'A' loop of the RHRSW system which re-established shutdown cooling on Unit 1.
Unit 2 operation was unaffected by the activities involving the common systems.
A four (4) hour notification was made to.the NRC at 0117 hours0.00135 days <br />0.0325 hours <br />1.934524e-4 weeks <br />4.45185e-5 months <br /> on November 11, 1990, in accordance with 10CPR50.72(b)(2)(ii) because the event resulted in the automatic actuations of various ESP.
This report is being submitted in accordance with the requirements of 10 CPR 50.73(a)(2)(iv).
Analysis of the Event
The consequences of this event were minimal.
Procedure ST-2-036-680-1 is only performed during refueling operations so that this event could not have occurred under normal power operation.
There was no release of radioactive material to the environment as a result of this event.
RPV inventory increased approximately 8 inches from 202 inches to 210 inches while the
'1A' CS system injected for approximately one minute.
During the 15 minutes that shutdown cooling was not in service, reactor coolant temperature increased approximately 3 degrees from 114 degrees to 117 degrees.
The maximum reactor coolant temperature allowed by Technical Specifications (TS) is 140 degrees while in Operating Condition 5.
Operations personnt i had ample time to restore shutdown cooling prior to exceeding the TS limit since it would have taken over two hours to reach the temperature limit.
The redundancy in the common ESW and RHRSW systems made the consequences of this event minimal to Unit 2.
The portions of the ESW and RHRSW systems unaffected by this event were available to satisfy all Unit 2 requirements.
Cause of the Event
The cause of the event was an incorrect procedure.
Procedure ST-2-036-680-1 is performed during a refueling outage to ensure that instrument sensing lines which penetrate the primary containment are clean and unobstructed.
The pressure transmitters are isolated during the blowback operation.
The I&C technician correctly followed ST-2-036-680-1 in restoring the isolated pressure transmitters.
PT-42-lN094A and PT-42-lN094E were restored satisfactorily (see Figure 1).
PDS-59-106A was the last pressure instrument restored.
Just prior to restoration, the HI and LO side isolation valves were closed and the equalizing valve was open.
The HI side line to PDS-59-106A is connected to the Primary Containment Instrument Gas system which was in service operating at 100 psig pressure.
Per the ST
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..c, mm v em procedure, the I&C technician opened the HI side isolation valve to PDS-59-106A pressurizing the instrument line to 100 psi up to L
the LO side' isolation valve.
The equalizing valve was then closed.
Finally, the LO side isolation valve was opened which released the pressurized air trapped between the equalizing valve and LO side-isolation valve down the instrument'line such that,
PT-42-lN094A and PT-42-lN094E momentarily sensed the high
- pressure-and-initiated a_-Division 1 LOCA-signal.
Corrective Actions
Procedure ST-2-036-680-1 will be revised to restore PDS-59-106A-and PDS-59-106B prior to restoration of other pressure transmitters.
This revision prevents the other pressure transmitters-from sensing momentary high pressure in the instrument-line and-actuating various ESF.
In additlon, the-i valving sequence to= restore the pressure _ switches will be revised
- - to'first open the LO-side _ isolation valve.. The equalizing valve
- isLthen: closed.
Finally, _the HI side isolation valve is opened.
This new valving sequence wi'll prevent-trapping pressurized air on the-LO side of the' pressure switch and releasing lt down the in'strument.line. :An additional-caution will be added to the procedure..to-alert the_I&C technician of the possibility of generating a LOCA signal.
Unit 2 procedure ST-2-036-680-2 will receive-similar revisions. 'The other procedures which isolate andJrestore_.these pressure-. switches _were reviewed and contained the correct valving sequence...'.A warning label will also be added
'to PDS-59-106A,-PDS-59-106B,'PDS-59-206A, and PDS-59-206B to alert I&C-technicians-of their unusual valving _ sequence.
This-
- will-aid personnel performing work on these pressure instruments for-reasons other than_-sensing line blowback procedures,-such as'
- - maintenance-activities.
.A review was performed and did not identify any similar configurations where a deviation from the normal pressure instrument valving sequence was required'to avoid-any' adverse conditions'.
Previous Similar Occurrences:
'LER 1-85-037',-1-85-040, 1
1 87-019, and'l-87-042 reported ESP
_actuations_.resulting_from spurious LOCA signals.
Each occurred
' as a result of a personnel error involving failure to correctly follow procedures.,The corrective actions for these previous occurrences could not:have prevented-the-spurious LOCA signal and ESP'actuationsfreported in this LER.
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| | | Reporting criterion |
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| 05000353/LER-1990-001, :on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent Info |
- on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent Info
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-001-01, :on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program Revised |
- on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-002-01, :on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures Adequate |
- on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures Adequate
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000353/LER-1990-002, :on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer Restored |
- on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer Restored
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-003, :on 900208,HPCI Sys Inboard Isolation Valve Isolated During Isolation Logic Surveillance Test.Caused by Mfg Error.Program for Replacement/Rework of Trip Units Being Implemented.Estimated Completion Date Dec 1993 |
- on 900208,HPCI Sys Inboard Isolation Valve Isolated During Isolation Logic Surveillance Test.Caused by Mfg Error.Program for Replacement/Rework of Trip Units Being Implemented.Estimated Completion Date Dec 1993
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-003-01, :on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation Reset |
- on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation Reset
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-003, :on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time Reset |
- on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-004, :on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure Revised |
- on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure Revised
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-005, :on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program Improved |
- on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program Improved
| 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-006-01, :on 900312,automatic Actuation of HPCI Sys & Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Spurious Low Reactor Water Level Signal. Event Discussed at I&C Group Meeting |
- on 900312,automatic Actuation of HPCI Sys & Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Spurious Low Reactor Water Level Signal. Event Discussed at I&C Group Meeting
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-006, :on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All Counties |
- on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All Counties
| | | 05000352/LER-1990-007, :on 900222,high Radiation Reactor Protection Sys Actuation & Isolation Setpoints Set Outside Required Limits.Caused by Personnel Error by Nonlicensed Employee. Setpoints Adjusted & Personnel Counseled |
- on 900222,high Radiation Reactor Protection Sys Actuation & Isolation Setpoints Set Outside Required Limits.Caused by Personnel Error by Nonlicensed Employee. Setpoints Adjusted & Personnel Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-007-01, :on 900330,actuations of Primary Containment & Reactor Vessel Isolation Control Sys ESF Occurred.Caused by Gross Failure of Inverter Inductor.Inverter Bypassed,Shunt Trip Breaker Closed & Isolations Reset |
- on 900330,actuations of Primary Containment & Reactor Vessel Isolation Control Sys ESF Occurred.Caused by Gross Failure of Inverter Inductor.Inverter Bypassed,Shunt Trip Breaker Closed & Isolations Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-008-01, :on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to Mfg |
- on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to Mfg
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-009, :on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector Replaced |
- on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-010, :on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of Cause |
- on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of Cause
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-011, :on 900713,reactor Encl Secondary Containment Isolation or Low Differential Pressure Occurred.Caused by Severed Instrument Air Line.Instrument Air Line Repaired on 900713 |
- on 900713,reactor Encl Secondary Containment Isolation or Low Differential Pressure Occurred.Caused by Severed Instrument Air Line.Instrument Air Line Repaired on 900713
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-011, :on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm Repositioned |
- on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm Repositioned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-011-02, :on 900713,positive Differential Pressure Condition Between Reactor Encl Secondary Containment & Outside Atmosphere Occurred,Resulting in Blowout Panel Actuation.Caused by Severed Air Supply Line |
- on 900713,positive Differential Pressure Condition Between Reactor Encl Secondary Containment & Outside Atmosphere Occurred,Resulting in Blowout Panel Actuation.Caused by Severed Air Supply Line
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-012-02, :on 900715,reactor Scram Occurred Due to Main Turbine Trip on Low Main Condenser Vacuum Due to Failed Pipe.Caused by Insufficient Pipe Support Resulting in Vibration Induced Metal Fatigue.Pipe Replaced |
- on 900715,reactor Scram Occurred Due to Main Turbine Trip on Low Main Condenser Vacuum Due to Failed Pipe.Caused by Insufficient Pipe Support Resulting in Vibration Induced Metal Fatigue.Pipe Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-012, :on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable Sleeved |
- on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable Sleeved
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-013-02, :on 900831,RCIC Sys Isolation Occurred.Caused by Personnel Error Resulting in Procedural Noncompliance. Procedural Compliance & Higher Attention to Detail Reinforced to Personnel |
- on 900831,RCIC Sys Isolation Occurred.Caused by Personnel Error Resulting in Procedural Noncompliance. Procedural Compliance & Higher Attention to Detail Reinforced to Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-013, :on 900611,review of Dc Electrical Distribution Sys Identified That Divs 1 & 2 Had Inadequate Isolation Capability Between Class 1E & non-Class 1E Components & Also Had under-rated Dc Fuses |
- on 900611,review of Dc Electrical Distribution Sys Identified That Divs 1 & 2 Had Inadequate Isolation Capability Between Class 1E & non-Class 1E Components & Also Had under-rated Dc Fuses
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-013-01, :on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626 |
- on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626
| 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-014-02, :on 900906,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Lack of Attention to Detail Resulting in Procedural Noncompliance.Personnel Counseled |
- on 900906,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Lack of Attention to Detail Resulting in Procedural Noncompliance.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-014-01, :on 900705,group III Primary Containment & Reactor Vessel Isolation Control Sys Isolation Signal Occurred,Initiating RWCU Sys Isolation.Causes Included High Outside Air Temp.Normal Ventilation Restored |
- on 900705,group III Primary Containment & Reactor Vessel Isolation Control Sys Isolation Signal Occurred,Initiating RWCU Sys Isolation.Causes Included High Outside Air Temp.Normal Ventilation Restored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-015-01, :on 900813,RWCU Sys Isolation Occurred. Isolation Resulted from High Regenerative HX Room Temp. Caused by Leaking Sys Vent Valves.Leaking Valves Replaced |
- on 900813,RWCU Sys Isolation Occurred. Isolation Resulted from High Regenerative HX Room Temp. Caused by Leaking Sys Vent Valves.Leaking Valves Replaced
| | | 05000353/LER-1990-015-02, :on 900910,reactor Scram Occurred Due to Spurious Trip Signal from Steam Leak Detection Sys Temp Switch.Caused by Equipment Failure.Temp Switch TTS-25-216D Was Replaced |
- on 900910,reactor Scram Occurred Due to Spurious Trip Signal from Steam Leak Detection Sys Temp Switch.Caused by Equipment Failure.Temp Switch TTS-25-216D Was Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-016-01, :on 900811,Tech Spec 3.7.6.4 Not Met Since Halon Sys Inoperable |
- on 900811,Tech Spec 3.7.6.4 Not Met Since Halon Sys Inoperable
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-016-01, :on 900815,Tech Spec Limiting Condition for Operation Action Not Implemented within Required Time Period Due to Firewatch Employee Failure to Perform Surveillance Procedure.Caused by Personnel Falsifying Tests |
- on 900815,Tech Spec Limiting Condition for Operation Action Not Implemented within Required Time Period Due to Firewatch Employee Failure to Perform Surveillance Procedure.Caused by Personnel Falsifying Tests
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000353/LER-1990-016-02, :on 900811,failure to Meet Tech Spec 3.7.6.4 Since Halon Sys Inoperable & Tech Spec Action Not Taken in Appropriate Time Period |
- on 900811,failure to Meet Tech Spec 3.7.6.4 Since Halon Sys Inoperable & Tech Spec Action Not Taken in Appropriate Time Period
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(8) | | 05000353/LER-1990-017-02, :on 900916,inadvertent Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred |
- on 900916,inadvertent Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-017-01, :on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse Replaced |
- on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-018-02, :on 901030,north Stack Wide Range Monitor Exceeded 7-day Limit for Inoperability of Tech Spec 3.3.7.5 |
- on 901030,north Stack Wide Range Monitor Exceeded 7-day Limit for Inoperability of Tech Spec 3.3.7.5
| | | 05000352/LER-1990-018-01, :on 900830,common Plant Water & Steam Barriers in Degraded Condition & Unit Placed in Unanalyzed Condition. Detailed Cause Analysis Will Be Provided.Task Force Established |
- on 900830,common Plant Water & Steam Barriers in Degraded Condition & Unit Placed in Unanalyzed Condition. Detailed Cause Analysis Will Be Provided.Task Force Established
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000353/LER-1990-019-02, :on 901101,half-scram & Isolations Resulted from Loss of Power to Rps/Uninterruptible Supply Panel Due to Inverter Damage |
- on 901101,half-scram & Isolations Resulted from Loss of Power to Rps/Uninterruptible Supply Panel Due to Inverter Damage
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-019-01, :on 901101,various Actuations of Primary Containment & Reactor Vessel Isolation Control Sys,Esf & Channel B RPS half-scram Occurred.Caused by Damaged Connector in Inverter Circuitry |
- on 901101,various Actuations of Primary Containment & Reactor Vessel Isolation Control Sys,Esf & Channel B RPS half-scram Occurred.Caused by Damaged Connector in Inverter Circuitry
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-019-01, :on 900915,special Rept for Diesel Generator Surviellance Test Failure |
- on 900915,special Rept for Diesel Generator Surviellance Test Failure
| | | 05000352/LER-1990-019-02, :on 900915,diesel Generator Surveillance Test Failure Reported.Diagnostic Testing Inconclusive on Cause & No Subsequent Failure Noted.No Addl Corrective Actions Planned |
- on 900915,diesel Generator Surveillance Test Failure Reported.Diagnostic Testing Inconclusive on Cause & No Subsequent Failure Noted.No Addl Corrective Actions Planned
| | | 05000352/LER-1990-020-01, :on 900918,personnel Manually Initiated Main Control Room Ventilation Sys Chlorine Isolation Due to High Toxic Chemical Concentration Signal |
- on 900918,personnel Manually Initiated Main Control Room Ventilation Sys Chlorine Isolation Due to High Toxic Chemical Concentration Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-020-02, :on 901119,primary Containment post-LOCA Radiation Monitoring Sys Declared Inoperable Due to Deficient Circuit Board in Three of Four Channels.Caused by Inadequate Design Review.Replacement Installed |
- on 901119,primary Containment post-LOCA Radiation Monitoring Sys Declared Inoperable Due to Deficient Circuit Board in Three of Four Channels.Caused by Inadequate Design Review.Replacement Installed
| 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-021-02, :on 901206,emergency Diesel Generator D21 Output Breaker Tripped on Reverse Power & Declared Inoperable.Caused by Closure of Cross Current Control Relay Contacts.Relay Replaced |
- on 901206,emergency Diesel Generator D21 Output Breaker Tripped on Reverse Power & Declared Inoperable.Caused by Closure of Cross Current Control Relay Contacts.Relay Replaced
| | | 05000352/LER-1990-021-01, :on 900911,seismic Monitoring Sys Declared Inoperable in Preparation for Performance of Surveillance Test Procedure |
- on 900911,seismic Monitoring Sys Declared Inoperable in Preparation for Performance of Surveillance Test Procedure
| | | 05000352/LER-1990-022-01, :on 901003,emergency Diesel Generator Sys Start Failed |
- on 901003,emergency Diesel Generator Sys Start Failed
| | | 05000352/LER-1990-023-01, :on 901015,emergency DGs Discovered to Be Inoperable on Various Occasions,Resulting in Condition Prohibited by Tss.Caused by Inadequate Testing of Redundant Rectifier Banks for Emergency DGs |
- on 901015,emergency DGs Discovered to Be Inoperable on Various Occasions,Resulting in Condition Prohibited by Tss.Caused by Inadequate Testing of Redundant Rectifier Banks for Emergency DGs
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-024-01, :on 901025,RCIC Sys Inoperable Due to Physical Separation Deficiency Between Class 1E & Non-Class 1E Cables Due to Personnel Error |
- on 901025,RCIC Sys Inoperable Due to Physical Separation Deficiency Between Class 1E & Non-Class 1E Cables Due to Personnel Error
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-025-01, :on 901110,spurious LOCA Signal Resulted in ESF Actuations |
- on 901110,spurious LOCA Signal Resulted in ESF Actuations
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-026-01, :on 901118,full Reactor Scram Signal Generated on High Reactor Pressure Vessel Pressure of 1,033 Psig. Caused by Personnel Error.Operator Counseled & Event Will Be Included in Operator Training |
- on 901118,full Reactor Scram Signal Generated on High Reactor Pressure Vessel Pressure of 1,033 Psig. Caused by Personnel Error.Operator Counseled & Event Will Be Included in Operator Training
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-027-01, :on 901120,reactor Scram Signal Occurred When Intermediate Range Monitor F Spiked Upscale Causing RPS Channel B Half Scram.Caused by Equipment Problem Coincident W/Performance of RPS Surveillance Procedure |
- on 901120,reactor Scram Signal Occurred When Intermediate Range Monitor F Spiked Upscale Causing RPS Channel B Half Scram.Caused by Equipment Problem Coincident W/Performance of RPS Surveillance Procedure
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-028-01, :on 901126,instrumentation & Controls Personnel Discovered That Facility Tech Specs Required Surveillance Requirements Not Met for Two Intermediate Range Monitors.W/ |
- on 901126,instrumentation & Controls Personnel Discovered That Facility Tech Specs Required Surveillance Requirements Not Met for Two Intermediate Range Monitors.W/
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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