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Abstract:
87-001 l
On January 5, 1987 at 2242 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.53081e-4 months <br /> with the unit at 100% power, a Reactor Enclosure Secondary Containment Isolation (an Engineered' Safety Feature) occurred resulting from low differential pressure.
Automatic initiation of the Standby Gas Treatment System (SGTS) and the Reactor Enclosure Recirculation System (RERS) followed with the systems operating as designed.
The low differential pressure condition was created when the Reactor Enclosure supply air fans tripped on low supply air temperature following the loss of auxiliary (station heat) steam.
With the loss of supply air, excessive negative pressure was created in the Reactor Enclosure automatically tripping the exhaust air fans resulting in the low differential pressure isolation.
The duxiliary steam was restored, the low differential pressure isolation was reset and normal Reactor Enclosure ventilation was restored at 2245 hours0.026 days <br />0.624 hours <br />0.00371 weeks <br />8.542225e-4 months <br />.
There were no adverse consequences resulting from the event.
Actions to Prevent Recurrence have been reviewed and the Engineering and Research Department has been requested, through EPE 1084, to evaluate possible methods of improving the reliability of the auxiliary boilers.
8702090419 870204 PDR ADOCK 05000352
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UCENSEE EVENT REPORT ILEA) TEXT CONTINUATION m e e s n ein -
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Operating Mode 1 (Power Operation)
Reactor Power 100%
Description of the Event:
On January 5, 1987 at 2242 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.53081e-4 months <br /> with the unit at 100% power, a Reactor Enclosure Secondary Containment Isolation (an Engineered Safety Feature) occurred due to low Reactor Enclosure differential pressure.
Automatic initiation of the Standby Gas Treatment System (SGTS) and the
'A' Reactor Enclosure Recirculation System (RERS) followed with the systems operating as designed.
The low differential pressure condition occurred as a result of a series of events:
1)
The auxiliary steam system was lost which resulted in the automatic trip of the Reactor Enclosure supply air fans due to low supply air temperature.
2)
The loss of supply air caused excessive negative pressure in the Reactor Enclosure which automatically tripped the Reactor Enclosure exhaust air fans.
3)
The tripping of the exhaust air fans resulted in the low differential pressure between the Reactor Enclosure and the outside atmosphere and the subsequent isolation.
The EIIS Codes for the affected systems are BH (SGTS), VA.
(RERS), NG (Reactor Enclosure), and SA (Auxiliary Steam System).
Consequences of the Event:
There were no adverse consequences resulting from this event.
The containment ventilation systems, Standby Gas Treatment (SGTS) and Reactor Enclosure Recirculation (RERS) responded as designed.
If one of the two SGTS trains or one of the two RERS trains had become inoperable, the redundant trains would have operated as designed.
No radioactive release resulted A-2
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- - _..e ans eira from the event and the Reactor Enclosure Ventilation system was returned to normal operation within three minutes of the isolation.
Cause of the Event
CAUSE CODE:
Other (X)
This event was the result of a series of events resulting from the trip of an auxiliary steam boiler.
With the
'A' auxiliary boiler out-of-service for maintenance, the
'B' and
'C' boilers were supplying auxiliary steam to the plant at a rate of 20,000 lbs/hr.
When the
'C' auxiliary boiler tripped on high furnace pressure, the
'B' boiler was unable to maintain header pressure and tripped on low atomizing steam pressure.
Loss of the auxiliary steam to the Reactor Enclosure supply air heating coils resulted in an automatic trip of the supply air fans on low supply air temperature (freeze protection).
With the Reactor Enclosure exhaust fans still in operation, excessive negative pressure was created in the Reactor Enclosure resulting from the loss of supply air.
The increasing negative pressure caused the automatic trip of the exhaust air fans.
The Secondary Containment Isolation occurred when Reactor Enclosure to outside atmosphere differential pressure decreased to the trip setpoint of 0.1 inches of water.
The SGTS and RERS then automatically initiated and operated as designed.
Corrective Actions
The outside Assistant Operators (AOs) restarted the auxiliary boilers and restored the plant heating system.
Upon restoration of plant heat, the isolation was reset and reactor building ventilation systems were returned to normal operation.
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Action Taken to Prevent Recurrence:
The Engineering and Research Department has been requested, through EPE 1084, to evaluate possible methods of improving the reliability of the auxiliary boilers or mitigating the effects of the loss of auxiliary steam on the plant.
Previous Similar Occurrences:
Reactor enclosure ventilation isolations were reported in the following LERs: 84-041,84-045, 85-005,85-012, 85-018,85-020, 85-023,85-041, 85-067,85-089.
However, all of these events were of different root causes than this event.
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W IM M
.A PHILADELPHIA ELECTRIC COMPANY 23O1 M ARKET STREET P.O. BOX 8699 PHILADELPHIA. PA.19101 February 4, 1987 1215)841-4000 Docket No. 50-352 U.S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, DC 20555
SUBJECT:
Licensee Event Report Limerick Generating Station - Unit 1 This LER concerns a Reactor Enclosure Secondary Containment Isolation due to low differential pressure resulting from the loss of the Reactor Enclosure Ventilation System.
Reference:
Docket No. 50-352 Report Number:
87-001 Revision Number:
00 Event Date:
January 5, 1987 Report Date:
February 4, 1987 Facility:
Limerick Generating Station P.O. Box A, Sanatoga, PA 19464 This LER is being submitted pursuant to the requirements of 10 CFR 50.73(a)(2)(iv).
Very truly yours, 4
R.
H. Logue Assistant to the Manager Nuclear Support Department cc:
Dr. Thomas E. Murley, Administrator, Region I, USNRC l
E. M. Kelly, Senior Resident Site Inspector l
See Service List l
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| 05000352/LER-1987-001, :on 870105,reactor Encl Secondary Containment Isolation Occurred as Result of Low Differential Pressure. Caused by Events Resulting from Trip of Auxiliary Steam Boiler.Boiler Restarted & Heating Sys Restored |
- on 870105,reactor Encl Secondary Containment Isolation Occurred as Result of Low Differential Pressure. Caused by Events Resulting from Trip of Auxiliary Steam Boiler.Boiler Restarted & Heating Sys Restored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-002, :on 870121,NSSS Sys Isolation Occurred During Performance of Surveillance Test.Caused by Personnel Error. Technicians Counseled as to Importance of Performing Procedures in Correct Sequence |
- on 870121,NSSS Sys Isolation Occurred During Performance of Surveillance Test.Caused by Personnel Error. Technicians Counseled as to Importance of Performing Procedures in Correct Sequence
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-003, :on 870122,control Room Ventilation Sys Isolated & a Train of Control Room Emergency Fresh Air Supply (CREFAS) Sys Initiated.Caused by Design Deficiency. Control Room Ventilation Isolation Reset |
- on 870122,control Room Ventilation Sys Isolated & a Train of Control Room Emergency Fresh Air Supply (CREFAS) Sys Initiated.Caused by Design Deficiency. Control Room Ventilation Isolation Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-004, :on 870124,NSSS Sys Group VI C Isolation Occurred During Performance of Surveillance Test.Caused by Technician Error.Personnel Counseled |
- on 870124,NSSS Sys Group VI C Isolation Occurred During Performance of Surveillance Test.Caused by Technician Error.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-005, :on 870130,two Temporary Cables,Used to Collect Data During Startup,Incorrectly Routed & Not Connected to Proper Channelized Multiplexers.Caused by Improper Evaluation During Cable Installation |
- on 870130,two Temporary Cables,Used to Collect Data During Startup,Incorrectly Routed & Not Connected to Proper Channelized Multiplexers.Caused by Improper Evaluation During Cable Installation
| 10 CFR 50.73(a)(2)(vi) | | 05000352/LER-1987-006, :on 870218 & 19,control Room Ventilation Sys Isolated & Control Room Emergency Fresh Air Supply Sys Train B Initiated.Caused by Chlorine Analyzer D Falsely Indicating Chlorine Present.Ventilation Isolation Reset |
- on 870218 & 19,control Room Ventilation Sys Isolated & Control Room Emergency Fresh Air Supply Sys Train B Initiated.Caused by Chlorine Analyzer D Falsely Indicating Chlorine Present.Ventilation Isolation Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-007, :on 870223,discovered Eight Surveillance Test Procedures for Intermediate Range Monitor (IRM) Channel Functional Test Did Not Include Check of IRM Inoperative Function.Caused by Procedural Deficiency |
- on 870223,discovered Eight Surveillance Test Procedures for Intermediate Range Monitor (IRM) Channel Functional Test Did Not Include Check of IRM Inoperative Function.Caused by Procedural Deficiency
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000352/LER-1987-008, :on 870302,control Room Ventilation Sys Isolated Due to Chlorine Analyzer Failure.Cause of Probe Malfunction Investigated & Not Determined.Analyzer Probe Replaced |
- on 870302,control Room Ventilation Sys Isolated Due to Chlorine Analyzer Failure.Cause of Probe Malfunction Investigated & Not Determined.Analyzer Probe Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-009, :on 870306,control Room Ventilation Sys Isolated & Emergency Fresh Air Supply Sys Train B Actuated. Caused by False Signal from Channel D Chlorine Analyzer. Temporary Circuit Alteration Installed |
- on 870306,control Room Ventilation Sys Isolated & Emergency Fresh Air Supply Sys Train B Actuated. Caused by False Signal from Channel D Chlorine Analyzer. Temporary Circuit Alteration Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-010, :on 870326,surveillance Test Did Not Meet Tech Spec Requirements.Caused by Inadequate Local Leak Rate Surveillance Test Procedure.Shift Supervision Notified & Temporary Procedure Change Implemented |
- on 870326,surveillance Test Did Not Meet Tech Spec Requirements.Caused by Inadequate Local Leak Rate Surveillance Test Procedure.Shift Supervision Notified & Temporary Procedure Change Implemented
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000352/LER-1987-011, :on 870416,operation Personnel Discovered That Reactor Encl Recirculation Sys a Inoperable Since 870403. Cause Unknown.Operator Placed Circuit Breaker Charging Motor Disconnect Switch in on Position |
- on 870416,operation Personnel Discovered That Reactor Encl Recirculation Sys a Inoperable Since 870403. Cause Unknown.Operator Placed Circuit Breaker Charging Motor Disconnect Switch in on Position
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-012, :on 870418,reactor Encl Secondary Containment Isolated Due to Low Differential Pressure Between Reactor Encl & Outside.Caused by Loss of Instrument Air Supply to Pressure Converter.Air Supply Restored |
- on 870418,reactor Encl Secondary Containment Isolated Due to Low Differential Pressure Between Reactor Encl & Outside.Caused by Loss of Instrument Air Supply to Pressure Converter.Air Supply Restored
| 10 CFR 50.73(a)(2)(i) | | 05000352/LER-1987-013, :on 870508,reactor Encl Secondary Containment Isolated Due to Low Differential Pressure Between Encl & Outside Environ.Caused by Personnel Error.Sign Posted on Filter Entry Hatch |
- on 870508,reactor Encl Secondary Containment Isolated Due to Low Differential Pressure Between Encl & Outside Environ.Caused by Personnel Error.Sign Posted on Filter Entry Hatch
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000352/LER-1987-014, :on 870513,unplanned Nuclear Steam Supply Shutoff Sys Isolation Occurred When Momentary High Radiation Signal Received.Cause Unknown.Nuclear Steam Supply Shutoff Sys Isolation Logic Reset |
- on 870513,unplanned Nuclear Steam Supply Shutoff Sys Isolation Occurred When Momentary High Radiation Signal Received.Cause Unknown.Nuclear Steam Supply Shutoff Sys Isolation Logic Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-015, :on 870514,HPCI Turbine Shut Down After Running for 25 Minutes.Caused by Loose Lead on Output of Flow Controller & Drift in Adjustment Valves Balance Chamber. Loose Lead Tightened & Valves Replaced |
- on 870514,HPCI Turbine Shut Down After Running for 25 Minutes.Caused by Loose Lead on Output of Flow Controller & Drift in Adjustment Valves Balance Chamber. Loose Lead Tightened & Valves Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000352/LER-1987-016, :on 870515,reactor Encl Secondary Containment Isolated.Caused by Const Worker Removing Instrument Cap from Outside Atmosphere Pressure Sensing Line.Instrument Cap Replaced & Isolation Reset |
- on 870515,reactor Encl Secondary Containment Isolated.Caused by Const Worker Removing Instrument Cap from Outside Atmosphere Pressure Sensing Line.Instrument Cap Replaced & Isolation Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-017, :on 870519,unplanned Nssss Group VI C Isolation Occurred When Momentary High Radiation Signal Received. Cause Unknown.Nssss Isolation Reset & Associated Wiring & Connections Inspected |
- on 870519,unplanned Nssss Group VI C Isolation Occurred When Momentary High Radiation Signal Received. Cause Unknown.Nssss Isolation Reset & Associated Wiring & Connections Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-018, :on 870520,leakage Rates of MSIVs & Total Primary Containment Leakage Exceeded Tech Spec Limit.Caused by Normal Wear.Msivs Repaired & Type B & C Pentrations Repaired |
- on 870520,leakage Rates of MSIVs & Total Primary Containment Leakage Exceeded Tech Spec Limit.Caused by Normal Wear.Msivs Repaired & Type B & C Pentrations Repaired
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-019, :on 870525,during Surveillance Test on Reactor Water Level Transmitter,Transmitter Vented Before Being Isolated Causing Pressure Oscillations.Caused by Personnel Error.Low Level Water Signal Reset |
- on 870525,during Surveillance Test on Reactor Water Level Transmitter,Transmitter Vented Before Being Isolated Causing Pressure Oscillations.Caused by Personnel Error.Low Level Water Signal Reset
| 10 CFR 50.73(a)(2)(i) | | 05000352/LER-1987-020, :on 870522,NSSSS Isolation of RWCU Occurred. Caused by Increased Temp in RWCU Pump Room Above 135 F Setpoint Due to Contractor Personnel Error.Isolation Valve Opened & RWCU Returned to Svc |
- on 870522,NSSSS Isolation of RWCU Occurred. Caused by Increased Temp in RWCU Pump Room Above 135 F Setpoint Due to Contractor Personnel Error.Isolation Valve Opened & RWCU Returned to Svc
| 10 CFR 50.73(a)(2)(i) | | 05000352/LER-1987-021, :on 870601,various Channel D Nuclear Steam Supply Shutoff Sys Isolations Occurred.Engineer Caused Short Circuit to Ground,Blowing Fuse Supplying Sys Isolation Circuit Logic.Fuse Replaced.Engineer Counseled |
- on 870601,various Channel D Nuclear Steam Supply Shutoff Sys Isolations Occurred.Engineer Caused Short Circuit to Ground,Blowing Fuse Supplying Sys Isolation Circuit Logic.Fuse Replaced.Engineer Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-022, :on 870609,two Penetrations Containing Testable O-ring Assemblies Not Included in Surveillance Test Procedures.Caused by Procedure Deficiency.Temporary Procedure Change Made |
- on 870609,two Penetrations Containing Testable O-ring Assemblies Not Included in Surveillance Test Procedures.Caused by Procedure Deficiency.Temporary Procedure Change Made
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-023, :on 870611,ESF Actuated Due to Failure of Battery Charger 1A1D103.Caused by Failure of Integrated Circuit Controller Card.Undervoltage Relays Mfg by Brown Boveri Corp Will Be Replaced |
- on 870611,ESF Actuated Due to Failure of Battery Charger 1A1D103.Caused by Failure of Integrated Circuit Controller Card.Undervoltage Relays Mfg by Brown Boveri Corp Will Be Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-024, :on 870611,nuclear Steam Supply Shutdown Sys Isolation of Refuel Floor Ventilation Occurred Due to Low Negative Differential Pressure Between Refuel Floor & Outside Environ.Caused by Personnel Error |
- on 870611,nuclear Steam Supply Shutdown Sys Isolation of Refuel Floor Ventilation Occurred Due to Low Negative Differential Pressure Between Refuel Floor & Outside Environ.Caused by Personnel Error
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-025, :on 870611,determined That Control Rod Block Logic Required by Tech Specs Inoperable.Caused by Personnel Error.Control Rod Shuffle Immediately Suspended,Limit Switches Returned to Normal & Contacts Cleaned |
- on 870611,determined That Control Rod Block Logic Required by Tech Specs Inoperable.Caused by Personnel Error.Control Rod Shuffle Immediately Suspended,Limit Switches Returned to Normal & Contacts Cleaned
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-026, :on 870612,nuclear Steam Supply Shutoff Sys Isolation Signal & Reactor Scram Signal Occurred.Caused by Nondestructive Radiographic Exams Being Performed on Main Steam Line A.Isolation & Scram Signals Reset |
- on 870612,nuclear Steam Supply Shutoff Sys Isolation Signal & Reactor Scram Signal Occurred.Caused by Nondestructive Radiographic Exams Being Performed on Main Steam Line A.Isolation & Scram Signals Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-027, :on 870615,reactor Protection Sys (RPS) B & Uninterruptible Power Source Series Breakers Shunt Tripped. Cause Unknown.Rps Power Supply Restored & Nuclear Steam Supply Shutoff Sys Reset |
- on 870615,reactor Protection Sys (RPS) B & Uninterruptible Power Source Series Breakers Shunt Tripped. Cause Unknown.Rps Power Supply Restored & Nuclear Steam Supply Shutoff Sys Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-028-01, :on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 |
- on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104
| | | 05000352/LER-1987-028, :on 870610,during Security Computer Outage, Firewatch & Security Escort Failed to Perform Hourly Fire Watch Insps.Caused by Failure to Follow Tech Spec 3.7.7 During Outage.Duties Reviewed W/Personnel |
- on 870610,during Security Computer Outage, Firewatch & Security Escort Failed to Perform Hourly Fire Watch Insps.Caused by Failure to Follow Tech Spec 3.7.7 During Outage.Duties Reviewed W/Personnel
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-029, :on 870616,various Nuclear Steam Supply Shutoff Sys Isolations Occurred.Caused by Incomplete Review of Implementation Method of Mod to Assess Potential Impact on Facility Operations.Review Underway |
- on 870616,various Nuclear Steam Supply Shutoff Sys Isolations Occurred.Caused by Incomplete Review of Implementation Method of Mod to Assess Potential Impact on Facility Operations.Review Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-030, :on 870604 & 05,failure to Perform Monthly Functional Tests of Channels D & B of Refueling Area Ventilation Exhaust Radiation Monitors Discovered.Caused by Personnel Error.Surveillance Tests Performed |
- on 870604 & 05,failure to Perform Monthly Functional Tests of Channels D & B of Refueling Area Ventilation Exhaust Radiation Monitors Discovered.Caused by Personnel Error.Surveillance Tests Performed
| | | 05000352/LER-1987-031, :on 870613,hot Maint Shop Ventilation Operating W/O Exhaust Radiation Monitoring.Caused by Personnel Not Following Procedures for Responding to Alarms. Shop Shut Down & Personnel Counseled |
- on 870613,hot Maint Shop Ventilation Operating W/O Exhaust Radiation Monitoring.Caused by Personnel Not Following Procedures for Responding to Alarms. Shop Shut Down & Personnel Counseled
| 10 CFR 50.73(a)(2)(i) | | 05000352/LER-1987-032, :on 870612,failed to Locate Neutron Fluence Wire Specimen Dosimeter,Violating Tech Spec Surveillance Requirements 4.4.6.1.4.Caused by Dosimeter Never Being Installed.Lost Part Analysis Prepared |
- on 870612,failed to Locate Neutron Fluence Wire Specimen Dosimeter,Violating Tech Spec Surveillance Requirements 4.4.6.1.4.Caused by Dosimeter Never Being Installed.Lost Part Analysis Prepared
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000352/LER-1987-033, :on 870701,control Room Ventilation Sys Isolated.Caused by Spurious Spike of Main Control Room Ventilation Chlorine Detector Due to Defective Solder Connection.Ventilation Sys Restored |
- on 870701,control Room Ventilation Sys Isolated.Caused by Spurious Spike of Main Control Room Ventilation Chlorine Detector Due to Defective Solder Connection.Ventilation Sys Restored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-034, :on 870715,four Safety Relief Valves Discovered 3% Over Setpoint Drift.Caused by Corrosion Bonding Between Stellite Pilot Valve,Seat & Labyrinth Seal Clearance Restriction.Valves Replaced & Refurbished |
- on 870715,four Safety Relief Valves Discovered 3% Over Setpoint Drift.Caused by Corrosion Bonding Between Stellite Pilot Valve,Seat & Labyrinth Seal Clearance Restriction.Valves Replaced & Refurbished
| 10 CFR 50.73(a)(2)(i) | | 05000352/LER-1987-035, :on 870715,unexpected Actuation of Nssss Occurred.Caused by Personnel Error Since Scope of Work Performed & Procedures Followed Not Specific.Preventive Maint Program Revised |
- on 870715,unexpected Actuation of Nssss Occurred.Caused by Personnel Error Since Scope of Work Performed & Procedures Followed Not Specific.Preventive Maint Program Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-036, :on 870722,grab Sample from RHR Svc Water Loop B Taken 30 Minutes Late.Caused by Personnel Error. Technician Verified No Change Occurred in Sample Analysis & Sampling Intervals Returned to Every 8 H |
- on 870722,grab Sample from RHR Svc Water Loop B Taken 30 Minutes Late.Caused by Personnel Error. Technician Verified No Change Occurred in Sample Analysis & Sampling Intervals Returned to Every 8 H
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-037, :on 870725,nuclear Steam Supply Shutoff Sys Inboard Isolation Occurred Due to Blown Fuse.Caused by Personnel Error.Fuse Replaced,Isolation Reset & Individual Counseled |
- on 870725,nuclear Steam Supply Shutoff Sys Inboard Isolation Occurred Due to Blown Fuse.Caused by Personnel Error.Fuse Replaced,Isolation Reset & Individual Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-038, :on 870802,nuclear Steam Supply Shutoff Sys Isolation Occurred.Caused by Short to Ground During Temporary Circuit Alteration Installation Due to Personnel Error.Personnel Counseled |
- on 870802,nuclear Steam Supply Shutoff Sys Isolation Occurred.Caused by Short to Ground During Temporary Circuit Alteration Installation Due to Personnel Error.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-039, :on 870731,technician Failed to Take Grab Sample of Reactor Encl Cooling Water Sys,Per Tech Specs. Caused by Personnel Error.Technicians Instructed on Importance of Sampling on Time |
- on 870731,technician Failed to Take Grab Sample of Reactor Encl Cooling Water Sys,Per Tech Specs. Caused by Personnel Error.Technicians Instructed on Importance of Sampling on Time
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-040, :on 870804,actuation of Group I Nuclear Steam Supply Shutoff Sys Occurred.Caused by Short Circuit from Poor Connection on Relay Logic Board Connector.Isolation Reset & Faulty Connection Removed & Remade |
- on 870804,actuation of Group I Nuclear Steam Supply Shutoff Sys Occurred.Caused by Short Circuit from Poor Connection on Relay Logic Board Connector.Isolation Reset & Faulty Connection Removed & Remade
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-041, :on 870806,NSSS Isolations Occurred Due to Channel Reactor B Trip.Caused by Loose Power Supply Cable Connection to Radiation Monitor.Isolations Reset & Loose Connection Tightened |
- on 870806,NSSS Isolations Occurred Due to Channel Reactor B Trip.Caused by Loose Power Supply Cable Connection to Radiation Monitor.Isolations Reset & Loose Connection Tightened
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-042, :on 870818,spurious High Drywell Pressure Signal Combined W/Existing Low Reactor Pressure Resulted in LOCA Signal.Caused by Personnel Error Due to Failure to Follow Approved Procedures.Personnel Counseled |
- on 870818,spurious High Drywell Pressure Signal Combined W/Existing Low Reactor Pressure Resulted in LOCA Signal.Caused by Personnel Error Due to Failure to Follow Approved Procedures.Personnel Counseled
| | | 05000352/LER-1987-044, :on 870822,discovered That Remote Shutdown Panel Operability Test Did Not Comply W/Tech Spec Surveillance Requirement 4.3.7.4.2.Caused by Procedure Deficiencies & Communication Failure |
- on 870822,discovered That Remote Shutdown Panel Operability Test Did Not Comply W/Tech Spec Surveillance Requirement 4.3.7.4.2.Caused by Procedure Deficiencies & Communication Failure
| 10 CFR 50.73(a)(2)(i) | | 05000352/LER-1987-045, :on 870830,standby Gas Treatment Sys Initiated. Caused by Polyphase Fault to Ground on Unit 2 Load Ctr Transformer,Producing Low Voltage Condition on Unit 1 Instrument Panel.Transformer Returned to Mfg |
- on 870830,standby Gas Treatment Sys Initiated. Caused by Polyphase Fault to Ground on Unit 2 Load Ctr Transformer,Producing Low Voltage Condition on Unit 1 Instrument Panel.Transformer Returned to Mfg
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-046, :on 870907,reactor Protection Sys Initiated Full Reactor Scram.Caused by Instrument Air Supply Root Valves Not Fully Open.Root Valves Opened Fully & Scram Reset |
- on 870907,reactor Protection Sys Initiated Full Reactor Scram.Caused by Instrument Air Supply Root Valves Not Fully Open.Root Valves Opened Fully & Scram Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-047, :on 870914,isolation of Main Control Room HVAC Occurred.Caused by Elevated Chlorine Levels in Control Encl HVAC Intake Plenum.Electronic Indications Checked & Verified to Be Operating Properly |
- on 870914,isolation of Main Control Room HVAC Occurred.Caused by Elevated Chlorine Levels in Control Encl HVAC Intake Plenum.Electronic Indications Checked & Verified to Be Operating Properly
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-048, :on 870919,reactor Scrammed Following Main Turbine Trip on electro-hydraulic Control Low Oil Pressure. Caused by Failure of Tubing Socket Weld in Fluid Actuating Supply Line.Failed Weld Replaced W/New Section |
- on 870919,reactor Scrammed Following Main Turbine Trip on electro-hydraulic Control Low Oil Pressure. Caused by Failure of Tubing Socket Weld in Fluid Actuating Supply Line.Failed Weld Replaced W/New Section
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1987-049, :on 870919,Tech Spec 3.4.1.4 Surveillance Test ST-6-043-390-1 Re RCS Temp Missed.Caused by Operator Not Performing Applicable Steps.Procedure Revised |
- on 870919,Tech Spec 3.4.1.4 Surveillance Test ST-6-043-390-1 Re RCS Temp Missed.Caused by Operator Not Performing Applicable Steps.Procedure Revised
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1987-050, :on 870917,reactor Enclosure Secondary Containment Isolated.Caused by Leak in Instrument Air Line to Reactor Enclosure Exhaust Fan Blade Pitch Control Device. Leak Repaired.Similar Tubing Will Be Inspected |
- on 870917,reactor Enclosure Secondary Containment Isolated.Caused by Leak in Instrument Air Line to Reactor Enclosure Exhaust Fan Blade Pitch Control Device. Leak Repaired.Similar Tubing Will Be Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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