05000348/FIN-2010002-03
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Finding | |
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Title | Violation of Technical Specification 5.4.1 for Failure to Maintain Procedures for Full Flow Recirculation After a Loss of Coolant Accident |
Description | The inspectors identified a Green NCV of TS 5.4.1 for the failure to maintain emergency procedure FNP-1/2-ESP-1.3, Transfer to Cold Leg Recirculation, Rev. 19. ESP-1.3 contained a step to verify containment sump level was sufficient to adequately cover the containment sump screens prior to initiating cold leg recirculation following a loss of coolant accident (LOCA) which led to a full flow recirculation. The containment sump level specified by the procedure was not sufficient to ensure suction vortexing and air ingestion into the emergency core cooling system (ECCS) would have been prevented. This finding was entered into the licensees corrective action program as condition report (CR) 20101101103. Planned corrective actions included issuing a standing night order to ensure adequate containment sump level is verified prior to transferring to cold leg recirculation and formally changing the value in ESP-1.3. This finding is more than minor because it affects the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of systems (containment spray and residual heat removal) that respond to initiating events (LOCAs which lead to full flow recirculation phase) to prevent undesirable consequences (i.e., core damage) and the cornerstone attribute of Procedure Quality, i.e. Operating (Post Event) Procedures (EOPs). The team assessed this finding using the SDP and determined that the finding was of very low safety significance (Green) because the inspectors determined that there was no loss of safety system function. Safety system function was determined to be maintained since the analyzed LOCAs in the accident analysis of the facility updated final safety analysis report (UFSAR) would introduce sufficient water into the containment from ECCS and the reactor coolant system (RCS) to provide sufficient containment sump level to ensure water level above the sump screens to prevent air introduction. This finding was reviewed for cross-cutting aspects and none were identified since the performance deficiency has existed since initial operation and is not indicative of current licensee performance |
Site: | Farley |
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Report | IR 05000348/2010002 Section 1R17 |
Date counted | Mar 31, 2010 (2010Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.17 |
Inspectors (proximate) | S Rose R Berryman C Even S Sandal L Pressley E Crowe S Shaeffer J Nadel |
INPO aspect | |
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Finding - Farley - IR 05000348/2010002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Farley) @ 2010Q1
Self-Identified List (Farley)
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