LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl |
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NRC
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E Portland General Electric Company Trojan Nuclear Plant P.O. Box 439 Rainier, Oregon 97048 (503)S56-3713 August 3, 1981 CPY-5/4-81 9 i1*'
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5 lol Mr. R. H. Engelken, Director f
Nuclear Regulatory Commission, Region v 8
AUG J, 3 ;gg;,
1990 North Califc,rnia Boulevard gMD 7 Walnut Creek, California 94596 L
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Dear Sir:
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U1 In accordance with the Trojan Plant Operating License, Appendix A, uo anC Technical Specifications, Paragraph 6.9.1.7, we are submitting Licensee Event Report No. 81-13.
This report describes a situation where Reactor Coolant System identified leakage exceeded the maxin:um amount allowed by the Technical Specifications.
Sincerely, 0
C.
P'. Yundt General Manager CPY S:mae Attachments c:
LER Distribution List 5'A a
8108140226 810803 DR ADOCK 05000344 PDR-
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REPORTABLE OCCURRENCE i
1.
Report No.:
81-13 2.
a.
Report Date:
August 3,'1981 i
b.
Occurrence Date: July 3, 1981 3.
Facility: Trojan Nuclear Plant, P.O. Box 439, Rainier, Oregon 97048 4.
Identification of Occurrence:
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' Reactor Coolant System leakage of approximately 14 gallons per' minute-4 was experienced during the performance of a Reactor Coolant System.in-tegrity test.
This is in excess of the Technical-Specifications limit of 10 gallons per minute for identified leakage. The source was leak-ing drain valves on the Reactor Coolant loops.
Condit'ons Prior to Occurrence:
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The plant was'in-Mode 3 at the time of this event. Reactor Coolant System pressure was at 2335 psig for the jerformance of the Reactor.
Coolant System integrity test.
Reector Coolant temperature was 557'F.
6.
Description of Occurrence:
A Reactor Coolant System pressure test was being conducted to verify system integrity following a plant refueling. After increasing pres-sure to-2335 psig, plant personnel noted increased temperature and pressure in the Reactor Coolant Drain Tank'(RCDT). Efforts to cool:
the tank were unsuccessful.and a Containment entry was made to inspect for leakage. This inspection t.vealed that loop drains on A, B, and C loops appeared to be leaking to the RCDT. Calculations determined the Reactor Coolant leak rate to be approximately 14 gallons per minute.
The valves were retorqued to their hot torque values and the. leakage stopped.
7.
Designation of Apparent Cause of Occurrence:
The type of valve used to isolate the loop drains must be torqued to ensure they seat properly. Plant procedures did not specify this re-
- - quirement. As a result, the valves were checked shut during preopera-tional valve lineups but were not torqued.
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8.
Significance of Occurrence:
This event had no effect on plant or public safety. All leakage was contained in the Reactor Coolant Drain Tank and the Containment sump.
The Reactor-Coolant ' System integrity te.
is intended to identify and.
correct system leaks prior'to reactor startup.
In this instance the test accomplished this purpose.
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- - Corrective Action:
. The valves ~were torqued to tne correct values and the leakage was.
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stopped. Changes -will be made to plant procedures, to provide in -
i structions for:praperly torquing these valves.
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| 05000344/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000344/LER-1981-001-03, /03L-0:on 801212,blown Fuse Was Found in Breaker Control Power Circuit for Vent Supply Fan to turbine-driven Auxiliary Feedwater Pump Room.Cause Unknown.Fuse Replaced | /03L-0:on 801212,blown Fuse Was Found in Breaker Control Power Circuit for Vent Supply Fan to turbine-driven Auxiliary Feedwater Pump Room.Cause Unknown.Fuse Replaced | | | 05000344/LER-1981-002-03, /03L-0:on 810107,after Normal Sampling of RCS, Common Sample Containment Isolation Valve Failed to Close from Control Room.Caused by Inadequate Lubrication of Valve Stem.Valve Stem Cleaned & Lubricated | /03L-0:on 810107,after Normal Sampling of RCS, Common Sample Containment Isolation Valve Failed to Close from Control Room.Caused by Inadequate Lubrication of Valve Stem.Valve Stem Cleaned & Lubricated | | | 05000344/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000344/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000344/LER-1981-003-03, /03L-0:on 810130,min Required Number of Source Range Channels Not Met When Both Channels of Nuclear Source Range Indications Failed to Energize Automatically.Caused by Improper Actuation of Instrument Crowbar Circuit | /03L-0:on 810130,min Required Number of Source Range Channels Not Met When Both Channels of Nuclear Source Range Indications Failed to Energize Automatically.Caused by Improper Actuation of Instrument Crowbar Circuit | | | 05000344/LER-1981-004-03, /03L-0:on 810122,fan Cooling Unit for Pump Did Not Automatically Start During Periodic Operating Test of Containment Spray Pump B.Caused by Thermal Overload Trip on Fan Unit Supply Breaker B-2415.Overloads Reset | /03L-0:on 810122,fan Cooling Unit for Pump Did Not Automatically Start During Periodic Operating Test of Containment Spray Pump B.Caused by Thermal Overload Trip on Fan Unit Supply Breaker B-2415.Overloads Reset | | | 05000344/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000344/LER-1981-005-03, /03L-0:on 810305,valves MO-2052A & MO-2069A Forming Containment Boundary Between Containment Spray Sys & Recirculation Sump in Auxiliary Bldg Found Incorrectly Positioned.Caused by Personnel Error | /03L-0:on 810305,valves MO-2052A & MO-2069A Forming Containment Boundary Between Containment Spray Sys & Recirculation Sump in Auxiliary Bldg Found Incorrectly Positioned.Caused by Personnel Error | | | 05000344/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-006-03, /03L-0:on 810316,erratic Trip Setpoint Found on Engineered Safeguards Feature Steamline Pressure Channel 516.Caused by Failed Capacitator.Capacitator Replaced & Channel Calibr | 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Caused by Failure of Indicator Lamp Socket.Lamp Socket & Dc Fuse Replaced | | | 05000344/LER-1981-025, Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-025-03, /03L-0:on 811104,power to Preferred Instrument Bus Y11 Lost for 1 Minute Due to Failure of Output Current Sensing Relay on Associated Static Inverter.Caused by Normal Relay end-of-life.Relay Replaced | /03L-0:on 811104,power to Preferred Instrument Bus Y11 Lost for 1 Minute Due to Failure of Output Current Sensing Relay on Associated Static Inverter.Caused by Normal Relay end-of-life.Relay Replaced | | | 05000344/LER-1981-026, Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | |
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