05000338/FIN-2009005-05
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Finding | |
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Title | Inadequate Procedure Results in Excess Letdown Heat Exchanger Leakage |
Description | A Green, self-revealing, non-cited violation of TS 5.4.1a was identified for the failure to adequately establish procedural requirements for component cooling (CC)water flow through the Unit 1 excess letdown heat exchanger (Hx) which resulted in a cracked Hx tube and excessive reactor coolant system (RCS) leakage when placing the Hx in service. The licensee entered this problem into their corrective action program as condition report 354523.This finding had a credible impact on safety due to continuous, excessive CC flow through the excess letdown Hx which caused a tube crack that allowed excessive intersystem leakage from the reactor coolant system (RCS) at approximately 60 gallons per minute for the 4 minutes in which the excess letdown heat exchanger was in service. The finding was more than minor because if left uncorrected it would have the potential to result in a more significant event involving multiple tube cracks with consequent leakage exceeding the capacity of a charging pump. In accordance with NRC inspection manual chapter (IMC) 0609, Significant Determination Process, the inspectors performed a phase 1 analysis and determined the finding required a phase 2 analysis by a regional senior reactor analyst (SRA) due to the finding resulting in RCS leakage that exceeded TS limits. The finding resulted in an intersystem leak from the RCS system into the CC system when the excess letdown Hx was placed into service; however, an intersystem LOCA was not addressed in the pre-solved risk table, therefore a phase 3analysis was performed by the SRA in accordance with the guidance of NRC IMC 0609, Appendix A. The SDP phase 3 risk evaluation resulted in a risk increase for the finding of less than 1E-6 for core damage frequency and less than 1E-7 for large early release frequency. The dominant sequence was an RCS leak into the CC system due to tube leakage in the excess letdown Hx when excess letdown was initiated, coupled with a failure of the charging function and a failure to isolate the leakage. Therefore, the finding was characterized as of very low safety significance (Green). The risk was low due to the magnitude of the leakage, which was less than the makeup capability of 1 charging pump, the availability of charging pumps to mitigate the leakage, and the high probability of accomplishing letdown isolation given the multiple operator cues and time availability. The finding had no cross-cutting aspects due to its legacy nature |
Site: | North Anna |
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Report | IR 05000338/2009005 Section 4OA3 |
Date counted | Dec 31, 2009 (2009Q4) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | J Caruso G Johnson D Dempsey J Furia G Dentel J Reece E Knutson G Mccoy R Clagg M Schneider M Balazik A Rao |
INPO aspect | |
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Finding - North Anna - IR 05000338/2009005 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (North Anna) @ 2009Q4
Self-Identified List (North Anna)
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