05000336/FIN-2008008-01
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Finding | |
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| Title | Failure to Ensure Equipment Necessary for Fire Safe Shutdown Available |
| Description | The team identified that Dominion failed to administratively control and ensure the availability of all necessary fire safe shutdown equipment to perform manual actions in the 4kV upper switchgear room. This finding was determined to be of very low safety significance (Green) and a NCV of the Millstone Nuclear Power Station, Unit 2 Operating License condition 2.C.(3), Fire Protection. The team determined that this finding was more than minor because it was associated with the external factors attribute (fire) of the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, Dominion did not ensure that an electrical flash jacket necessary to perform local breaker operations was available in the upper 4kV switchgear room. Actions to restore the A diesel generator would have been delayed for a fire in the lower 4kV switchgear room. The team assessed this finding in accordance with NRC IMC 0609, Appendix F, Fire Protection Significance Determination Process. This finding affected post-fire safe shutdown systems. This finding screened to very low safety significance (Green) in Phase 1 of the SDP because it was assigned a low degradation rating. A low degradation rating was assigned because additional electrical flash jackets were onsite and the local breaker operations would likely have been performed within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The safe shutdown analysis most restrictive timeline for a fire in the lower switchgear room required a charging pump restored within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> for reactor coolant system makeup. Local breaker operations in the upper 4kV switchgear room would be needed to support ac power to a charging pump. The team determined that this finding had a cross cutting aspect in the area of human performance because personnel did not return an electrical flash jacket to its proper storage location even though it was clearly labeled for the upper 4kV switchgear room. (H.4(b)) (Section 1R05.01 |
| Site: | Millstone |
|---|---|
| Report | IR 05000336/2008008 Section 1R05 |
| Date counted | Dec 31, 2008 (2008Q4) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.05 |
| Inspectors (proximate) | E Huang D Orr J Rogge M Halter |
| CCA | H.12, Avoid Complacency |
| INPO aspect | QA.4 |
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Finding - Millstone - IR 05000336/2008008 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Millstone) @ 2008Q4
Self-Identified List (Millstone)
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