05000321/FIN-2011003-01
From kanterella
Jump to navigation
Jump to search
Finding | |
---|---|
Title | Failure to promptly identify and take corrective actions to ensure Bussmann fuses identified by the Part 21 notification 2005-37 were removed from use in safety related applications |
Description | A self-revealing NCV of 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, was identified for failure to promptly identify and take corrective actions to ensure Bussmann fuses identified by the Part 21 notification 2005-37, were removed from use in safety related applications. Corrective actions taken include replacing the KTN-R 10 amp fuses on the 1B emergency diesel generator with fuses manufactured after 1991, placing a hold on all KWN-R and KTN-R fuses size 30 amps below manufactured between 1987 and 1991, and replacement of these fuses with new KWN-R and KTN-R fuses with a date code 2009 or newer. This violation has been entered into the licensees corrective action program as condition report (CR) 2010116039. Failure to promptly identify and take corrective actions to ensure Bussmann fuses identified by the Part 21 notification 2005-37 were removed from use in safety related applications is a performance deficiency. This performance deficiency is more than minor because it is associated with the Equipment Performance attribute and adversely affected the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, on December 23, 2010, the Hatch 1B emergency diesel generator #3 stop circuitry operability light was discovered not illuminated on panel 1R43-P003B. Without power to this circuitry the 1B emergency diesel generator is inoperable and unavailable to provide its required safety function. The significance of this finding was screened using IMC 0609 Attachment 4, table 4a. The risk significance screening required a Phase 3 analysis, because the finding screened as potentially risk significant due to a seismic initiating event. The regional senior reactor analyst (SRA) performed a Phase 3 analysis for the finding. The analysis included two parts, the first covering the time period of total inoperability of the fuse; and the second covering the exposure time from when the non qualified fuses were installed until they were replaced, when they were subject to potential seismic failure. Calculations were performed using the NRCs plant specific risk models. The short exposure time for the first analysis, and the low likelihood of a seismic event at the plant for the second analysis, caused the combined result to be a very low risk condition. The finding was determined to be Green in the SDP. Because the performance deficiency occurred in 2006 and is outside the past three years, no cross-cutting aspect is assigned. |
Site: | Hatch ![]() |
---|---|
Report | IR 05000321/2011003 Section 4OA2 |
Date counted | Jun 30, 2011 (2011Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | A Nielsen B Collins C Dykes D Hardage E Morris J Rivera R Bernhard R Kellner S Shaeffer T Chandler |
INPO aspect | |
' | |
Finding - Hatch - IR 05000321/2011003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Hatch) @ 2011Q2
Self-Identified List (Hatch)
| ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||