LER-1980-003, During Evaluation of SEP Topic VI-3,incorrect Assumptions for Initiation of Containment Spray Were Determined to Have Resulted in Lower Predicted Peak Pressures.Reanalysis Corrected Calculations |
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~DATE TO LER DATED ~4038Q..
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NRC FORM366 17-771 PALISADES PLANT u. ~: Nuci:£~R*REGULA;ro~v'coMM1ss10N
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LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REOUiRE"o INFORMATIONI CONTROL BLOCK: I IQ 1
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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @
1During evaluation of the high energy line break SEP Topic, it was deter-
[QJ1J 1mined that incorrect assumptions for initiation of containment spray as
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1well as inaccuracies in SG mass-energy inventories resulted in predicted
(]JI) 1Peak containment pressures being lower than actual.
The recalculated contain-
£IIIJ I ment pressures would exceed design pressures under certain accident
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Event reportable ~er TS 6.9.2.A.8.
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CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUB CODE SUBCODE JS IB I@ ~@ 1.AJ@) IZ IZ I ZIZ I Z IZ I@ E.J@) fU@
9 10 11 12 13 18 19 20 t;:;'\\
LE R IRQ CV ENT YEAR v.y REPORT I 8 l 0 I NUMBER 21 22 SEQUENTIAL OCCURRENCE REPORT REPORT NO.
CODE TYPE I I 10 10 I 31 k::::J p 11 I 1U I.=1 23 24 26 27 28 29 JO 31 REVISION NO.
~
32 I
I 80 TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM l>UB.
SUPPLIER ACTION FUTURE EFFECT SHUTDOWN
~ ATTACHMENT NPRO-C PRIME COMP.
COMPONENT MANUFACTURER l.XJ@lXJ@)
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33 34 35 36 37 40 41 42 43 IZ 1919 19 I@
CAUSE DESCRIPTION ANO CORREC'rlVE ACTIONS.
.&.g 47 Jill] JErrors were apparently made during initial accident analyses.
Corrective IIITI I action __ has *been taken to reduce spray initiation time, and to reduce mass-
((I)) 1energy release into containment following a MSLB.
Calculated containment o::::rIJ 1peak pressures are now acceptable.
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STATUS
% POWER OTHER STATUS v:;:J [ill] LI@ 10 I 0 I Ol@I.... _N_A ___
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10 12 13 ACTIVITY CONTENT C\\
RELEASED OF RELEASE AMvUNT OF ACTIVITY EE] W@ ~@I NA I
7 8
9 10 11 7
METHOD OF DISCOVERY DESCRIPTION @
DISCOVERY LPJ@I SEP Evaluation cs 46 NA LOCATION OF RELEASE @.
45 PERSONNEL EXPOSURES t::;:,.
80 BO 80 NUMBER t:;::;-. TYPE DESCRIPTION\\~
ITEi I 0 I 01 0 '~@,___NA 1
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11 12 13 80 PERSONNEL INJURIES I'.:";\\
NUMBER.
OESCRIPTION6 ETIJ b 10 I 0*1@~------_N_A ______________________ __,
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9 11 12 so LOSS o* OR DAMAGE TO FACILITY l4j\\
TYPE
DESCRIPTION
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NRC USE ONLY
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N_A _________________ _.
I II II II I II II I 68 69 80 so
consumers Power company General Offices: 212 West Michigan Avenue,.Jackson, Michigan 49201
- Area Code 517 788-0550 May 13, 1980 Mr James G Keppler Office of Inspection & Enforcement Region III*
U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - UPDATE TO LICENSEE EVENT REPORT 80-003 -
CONTAINMENT SPRAY
"'
Licensee Event Report (LER)80-003 was submitted to the NRC Region III office on April *3, 1980.
An update to this LER is on the reverse side of this letter.
Also attached is a two page report which contains the actions taken with regard to this LER.
David P Hoffman (Signed)
David P Hoffman Nuclear Licensing Administrator CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC Resident Inspector - Palisades Attachment (2 pages)
Attachment to LER 80-003/01-X-l Consumers Power Company Palisades Nuclear Plant Docket 50-255
Description
During review of SEP Topic VI-3 it was discovered the total activation time for the containment spray was in excess of the initiation times of 30 and 33 seconds published in FSAR, Section 14.18.1.
The time required to fill the pipe headers, in combination with diesel and pump starting times, accounts for most of the difference.
The containment pressure analysis due to a LOCA, described in FSAR, section 14.18, is not considered to be significantly affected by the longer spray initiation since peak pressures occur prior to the assumed shorter spray initiation times.
During a LOCA one of the functions of the sprays is to limit the peak pressure after recirculation occurs, but containment spray does not influence the initial pressure rise.
Peak pressures for MSLB's in the 1969 analysis, summarized in Amendment 14 (item 14.11), occurred after the sprays were assumed to be activated.
The sprays were then-partial cause for limiting the peak pressure during a MSLB.
The MSLB was therefore considered for reanalysis.
Following discussion with Combustion Engineering (CE) and Bechtel to plan corrective actions, CE discovered an error in the 1968 mass release data for MSLB.
This error affects only the reactor full load case and results in approximately a 5% increase in total mass release to containment.
Cause of Deviation The cause of the iricorrectly assumed spray initiation time was an apparent oversight in which the 30 second start time for ESS equipment are closed onto the diesel bus.
Another oversight was apparently-nade in the analysis for mass and energy release performed by CE in 1968.
This error resulted in the published integrated flow from the intact* steam generator prior to isolation being too low.
Corrective Action
Reanalysis of the full load MSLB assuming losS-of offsite power and diesel failure and*using ~orrected spray initiation times showed containment design pressure to be exceeded.
The error in the mass and energy release data accounts for a majority of the calculated pressure increase.
The no-load analysis has assumed offsite power is available which is consistent with the philosophy in the FSAR Amendment 15 Item 14.3 and Amendment 17, Item 5 and 6.
The assumed most severe single active*failure is a containment spray pump failure.
The contributing factors for the no-load results exceeding containment pressure are an apparent overly conservative calculation of no-load steam generator inventory and the stroke time of the containment spray isolation valve *.
Para.metric analysis has been completed assuming varied steam generator water levels, filling the containment spray system headers, and tripping the MSIV in a shorter interval, thereby reducing the mass release from the intact steam generator.
Necessary modifications in plant operation have been made based on this analysis.
These changes will allow the plant to operate within plant design constraints.
.. ~........
The changes are:
(1)
Closure of the MSIVs.on containment high pressure as well as on steam generator low pressure.
In conjuction with this, an analysis has been completed which concludes that MSIV closure will occur in less than 1 second after receipt of the initiating signal.
(2)
Resequencing of loads on the emergency diesel generators,.
such that the containment spray pumps are started sooner.
(3)
Partial filling of the containment spray system piping, in order to further reduce containment spray initiation times.
(4)
Imposition of a 1 psig limit on containment initial pressure.
( 5)
Modification of the containment spray isolation valve actuator to reduce the stroke time and in turn reduce the containment spray initiation time.
Proposed changes to the Palisades Plant Technical Specifications will be submitted to incorporate items (1), (3) and (4) above as_
Technical Specification operability requirements.
It.sh0uld be noted that operating restrictions (1) through (5) were derived from a parametric analysis; accordingly, if operating experience indicates one or more of the restrictions to be unsatisfactory, the analysis will necessarily be reperformed to derive a new set of operating restrictions.
Accordingly, proposed technical specification changes will not be submitted until sufficient operating experience indicates the above restrictions to be acceptable.
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| 05000255/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000255/LER-1980-001-01, /01T-0:on 800109,pipe & Pipe Support Stress Analyses Per IE Bulletin 79-14 Identified Lines Not Meeting FSAR Criteria for SSE or Obe.Apparently Caused by Differences in Design Documents & as-built Conditions | /01T-0:on 800109,pipe & Pipe Support Stress Analyses Per IE Bulletin 79-14 Identified Lines Not Meeting FSAR Criteria for SSE or Obe.Apparently Caused by Differences in Design Documents & as-built Conditions | | | 05000255/LER-1980-002-03, /03L-0:on 791023,during Routine Testing of Hydraulic Snubbers,Snubber S-6,located on Main Steam Line, Failed to Meet Test Acceptance Criteria.Caused by Loose Accumulator Oil Fill Fitting.Snubber Replaced | /03L-0:on 791023,during Routine Testing of Hydraulic Snubbers,Snubber S-6,located on Main Steam Line, Failed to Meet Test Acceptance Criteria.Caused by Loose Accumulator Oil Fill Fitting.Snubber Replaced | | | 05000255/LER-1980-002, Notifies That Current Main Steam Line Break Analysis Requested in NRC Cannot Be Completed Until Containment Spray Problem Identified in LER 80-002,is Resolved | Notifies That Current Main Steam Line Break Analysis Requested in NRC Cannot Be Completed Until Containment Spray Problem Identified in LER 80-002,is Resolved | | | 05000255/LER-1980-003-01, During Evaluation of SEP Topic VI-3,incorrect Assumptions for Initiation of Containment Spray Were Determined to Have Resulted in Lower Predicted Peak Pressures.Reanalysis Corrected Calculations | During Evaluation of SEP Topic VI-3,incorrect Assumptions for Initiation of Containment Spray Were Determined to Have Resulted in Lower Predicted Peak Pressures.Reanalysis Corrected Calculations | | | 05000255/LER-1980-003, Forwards Revised Page 3-36 to Basis of Tech Spec Section 3.4 Re Containment Cooling,Submitted in 861020 Change Request.Error in Original Submittal Resulted from LER 80-003 Re Description of Main Steam Line Break Results | Forwards Revised Page 3-36 to Basis of Tech Spec Section 3.4 Re Containment Cooling,Submitted in 861020 Change Request.Error in Original Submittal Resulted from LER 80-003 Re Description of Main Steam Line Break Results | | | 05000255/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000255/LER-1980-004-01, /01T-0:on 800327,during Review of Tech Spec Surveillance Procedures,Discovered Procedure MO-19 Requiring Isolation of Both Containment Spray Headers During Test Violated.Cause Not Stated.Procedure Rewritten | /01T-0:on 800327,during Review of Tech Spec Surveillance Procedures,Discovered Procedure MO-19 Requiring Isolation of Both Containment Spray Headers During Test Violated.Cause Not Stated.Procedure Rewritten | | | 05000255/LER-1980-005-01, /01T-0:on 800327,during Review of Tech Spec Surveillance Procedures,Discovered That Procedures QO-2 & MO-23 Require Stroking Sirw Tank Outlet Valves.Amend to OL or Clarification of Tech Spec Requirements Will Be Sought | /01T-0:on 800327,during Review of Tech Spec Surveillance Procedures,Discovered That Procedures QO-2 & MO-23 Require Stroking Sirw Tank Outlet Valves.Amend to OL or Clarification of Tech Spec Requirements Will Be Sought | | | 05000255/LER-1980-005, Forwards LER 80-005/01T-0 | Forwards LER 80-005/01T-0 | | | 05000255/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000255/LER-1980-006-03, Discovered That T-ring Air Supplies for 12-inch & 48-inch Purge Valves Had Leakage in Excess of Acceptance Criteria.Caused by Poor Fittings & Packings | Discovered That T-ring Air Supplies for 12-inch & 48-inch Purge Valves Had Leakage in Excess of Acceptance Criteria.Caused by Poor Fittings & Packings | | | 05000255/LER-1980-007-01, /01T-0:on 800407,during Maint on Control Room Ventilation Sys,Discovered Leakage Defects Through Shaft of Fan V-36.Fresh Air Damper D-1 Would Not Close.Caused by Inadequate pre-operational Testing of Ventilation Sys | /01T-0:on 800407,during Maint on Control Room Ventilation Sys,Discovered Leakage Defects Through Shaft of Fan V-36.Fresh Air Damper D-1 Would Not Close.Caused by Inadequate pre-operational Testing of Ventilation Sys | | | 05000255/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000255/LER-1980-008, Forwards Updated LER 80-008/01X-1 | Forwards Updated LER 80-008/01X-1 | | | 05000255/LER-1980-008-01, Test Results of Type C Containment Leak Tests Indicated Local Leakage in Excess of Tech Specs.Caused by Deterioration of Valve Internals | Test Results of Type C Containment Leak Tests Indicated Local Leakage in Excess of Tech Specs.Caused by Deterioration of Valve Internals | | | 05000255/LER-1980-009-01, /01T-0:on 800424,during Walkdowns of safety- Related Sys Conducted to Verify P&ID Accuracy,Ventilation Supply Damper CV-1812 to West Safeguards Equipment Room Could Not Be Located.Cause Unknown | /01T-0:on 800424,during Walkdowns of safety- Related Sys Conducted to Verify P&ID Accuracy,Ventilation Supply Damper CV-1812 to West Safeguards Equipment Room Could Not Be Located.Cause Unknown | | | 05000255/LER-1980-010-01, /01T-0:on 800326,during Calibr of Sirw Tank Low Level Switches,Reactor Analysis & Safety Setpoint Were Determined to Have Exceeded Tech Specs Limit.Caused by Error in Acceptance Criteria.Reportability Determined 800428 | /01T-0:on 800326,during Calibr of Sirw Tank Low Level Switches,Reactor Analysis & Safety Setpoint Were Determined to Have Exceeded Tech Specs Limit.Caused by Error in Acceptance Criteria.Reportability Determined 800428 | | | 05000255/LER-1980-011-03, /03L-0:on 800416,following Mods to Power Operated Relief Valve Supplies,Valves Were Declared Operable Before Administrative Reviews Were Completed.Caused by Misunderstanding of Review Requirements | /03L-0:on 800416,following Mods to Power Operated Relief Valve Supplies,Valves Were Declared Operable Before Administrative Reviews Were Completed.Caused by Misunderstanding of Review Requirements | | | 05000255/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000255/LER-1980-012, Licensee Event Report 80-012 Regarding Bottom Half of the Barrier for Fire Penetration HO-12 Was Missing During Inspection of Fire Barriers | Licensee Event Report 80-012 Regarding Bottom Half of the Barrier for Fire Penetration HO-12 Was Missing During Inspection of Fire Barriers | | | 05000255/LER-1980-012-03, /03L-0:on 800417,during Insp of Fire Barriers, Discovered That Bottom Half of Barrier for Fire Penetration Was Missing.Cause Undetermined.Barrier Restored to Operable Status | /03L-0:on 800417,during Insp of Fire Barriers, Discovered That Bottom Half of Barrier for Fire Penetration Was Missing.Cause Undetermined.Barrier Restored to Operable Status | | | 05000255/LER-1980-013-01, /01T-0:on 800521,HPSI Flow Indication for Loop 2A Was Inoperable.Caused by Ruptured Bellows.Transmitter Was Replaced to Restore Operability | /01T-0:on 800521,HPSI Flow Indication for Loop 2A Was Inoperable.Caused by Ruptured Bellows.Transmitter Was Replaced to Restore Operability | | | 05000255/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000255/LER-1980-014, Licensee Event Reports 80-014, 80-015, and 80-016 Regarding Oil Level in Snubbers No. 5, 9, and 7 Were Found to Be Less than Zero During Routine Testing of Hydraulic Snubbers | Licensee Event Reports 80-014, 80-015, and 80-016 Regarding Oil Level in Snubbers No. 5, 9, and 7 Were Found to Be Less than Zero During Routine Testing of Hydraulic Snubbers | | | 05000255/LER-1980-014-03, /03L-0:on 800512,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 5 Found to Be Less than Zero.Caused by Rust Combined W/Vibrator,Accelerating Seal Failure.Rust Found Inside Accumalator | /03L-0:on 800512,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 5 Found to Be Less than Zero.Caused by Rust Combined W/Vibrator,Accelerating Seal Failure.Rust Found Inside Accumalator | | | 05000255/LER-1980-015-03, /03L-0:on 800512,during Routine Testing of Hydraulic Snubber,Oil Level in Snubber 9 Found to Be Less than Zero.Cause of Seal Damage Unknown;Normal Wear Suspected.Accumulator Plunger Seal Found to Be Damaged | /03L-0:on 800512,during Routine Testing of Hydraulic Snubber,Oil Level in Snubber 9 Found to Be Less than Zero.Cause of Seal Damage Unknown;Normal Wear Suspected.Accumulator Plunger Seal Found to Be Damaged | | | 05000255/LER-1980-016-03, /03L-0:on 800515,during Testing of Hydraulic Snubber,Oil Level in Snubber 7 Found to Be Less than Zero. Caused by Seal Degradation.Snubber Will Be Disassembled to Confirm Cause | /03L-0:on 800515,during Testing of Hydraulic Snubber,Oil Level in Snubber 7 Found to Be Less than Zero. Caused by Seal Degradation.Snubber Will Be Disassembled to Confirm Cause | | | 05000255/LER-1980-017-03, Ps Testing Procedures Review Revealed Setpoint of PS-1801 Through 1804 to Be Lower than Permitted by Tech Specs.Caused by Faulty Procedure. Procedures Revised to Conform W/Tech Specs | Ps Testing Procedures Review Revealed Setpoint of PS-1801 Through 1804 to Be Lower than Permitted by Tech Specs.Caused by Faulty Procedure. Procedures Revised to Conform W/Tech Specs | | | 05000255/LER-1980-017, Forwards Updated LER 80-017/03X-1 | Forwards Updated LER 80-017/03X-1 | | | 05000255/LER-1980-018-03, /03L-0:on 800522,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 2 Was Found to Be Less than Zero & Was Declared Inoperable.Apparently Caused by Seal Degradation | /03L-0:on 800522,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 2 Was Found to Be Less than Zero & Was Declared Inoperable.Apparently Caused by Seal Degradation | | | 05000255/LER-1980-018, Licensee Event Report 80-018 Regarding Oil Level in Snubber No. 2 Found to Be Less than Zero During Routine Testing of Hydraulic Snubbers | Licensee Event Report 80-018 Regarding Oil Level in Snubber No. 2 Found to Be Less than Zero During Routine Testing of Hydraulic Snubbers | | | 05000255/LER-1980-019-01, /01T-0:on 800609,during Tech Spec Review,Tech Spec 3.3 Determined to Provide Too Little Borated Water for Safety Injection.Caused by Imprecise Wording of Tech Spec. Low Level Alarm Setpoint Changed,Tech Spec Under Evaluation | /01T-0:on 800609,during Tech Spec Review,Tech Spec 3.3 Determined to Provide Too Little Borated Water for Safety Injection.Caused by Imprecise Wording of Tech Spec. Low Level Alarm Setpoint Changed,Tech Spec Under Evaluation | | | 05000255/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000255/LER-1980-020-01, /01T-0:on 800711,control Rod Drive Mechanism Failed to Operate Properly,Resulting in Rod Being Misaligned for Approx Five Minutes.Caused by Dirty Control Relay Armatures & Contractor Interlock Which Resulted in Sticking | /01T-0:on 800711,control Rod Drive Mechanism Failed to Operate Properly,Resulting in Rod Being Misaligned for Approx Five Minutes.Caused by Dirty Control Relay Armatures & Contractor Interlock Which Resulted in Sticking | | | 05000255/LER-1980-020, Forwards LER 80-020/01T-0 | Forwards LER 80-020/01T-0 | | | 05000255/LER-1980-021-01, /01X-1:on 800725,during Valve Inservice Insp, Operator Opened Containment Sump Valve CV-3030.Valve Stayed Open 36-h.Caused by Operator Error.Valve Closed,Operator Counseled & Shift Turnover Checklist Revised | /01X-1:on 800725,during Valve Inservice Insp, Operator Opened Containment Sump Valve CV-3030.Valve Stayed Open 36-h.Caused by Operator Error.Valve Closed,Operator Counseled & Shift Turnover Checklist Revised | | | 05000255/LER-1980-021, Forwards Corrected App C, Calculations of Radiological Effects as Results of Hypothetical Accident W/CV-3030 Open, to 800820 LER 80-021,Revision 1.Corrected Apps E & F Also Encl | Forwards Corrected App C, Calculations of Radiological Effects as Results of Hypothetical Accident W/CV-3030 Open, to 800820 LER 80-021,Revision 1.Corrected Apps E & F Also Encl | | | 05000255/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000255/LER-1980-022-03, /03L-0:on 800710,2-h After Reactor Criticality, Channel NI-03 Not Declared Operable Prior to Reactor Startup.Caused by Failure of Shift Supervisor to Check Control Mechanism | /03L-0:on 800710,2-h After Reactor Criticality, Channel NI-03 Not Declared Operable Prior to Reactor Startup.Caused by Failure of Shift Supervisor to Check Control Mechanism | | | 05000255/LER-1980-023-03, Containment High Radiation Detectors Re 1805 & 1807 Determined Inoperable.No Apparent Cause for Failure.Detectors Disassembled,Cleaned & Recoated & Are Now Functional | Containment High Radiation Detectors Re 1805 & 1807 Determined Inoperable.No Apparent Cause for Failure.Detectors Disassembled,Cleaned & Recoated & Are Now Functional | | | 05000255/LER-1980-023, Forwards Updated LER 80-023/03X-1 | Forwards Updated LER 80-023/03X-1 | | | 05000255/LER-1980-024, Forwards LER 80-024/01T-0 | Forwards LER 80-024/01T-0 | | | 05000255/LER-1980-024-01, /01T-0:on 800731,w/diesel Generator & Charging Pump P-55A Inoperable,Backup Pump P-55B Failed.Diesel Generator Restored in One Hour.Caused by Pump Packing Failure on P-55B.Pump Repacked & Restored to Svc | /01T-0:on 800731,w/diesel Generator & Charging Pump P-55A Inoperable,Backup Pump P-55B Failed.Diesel Generator Restored in One Hour.Caused by Pump Packing Failure on P-55B.Pump Repacked & Restored to Svc | | | 05000255/LER-1980-025, Forwards LER 80-025/01T-0 | Forwards LER 80-025/01T-0 | | | 05000255/LER-1980-025-01, /01T-0:on 800801,during Vol Control Tank Venting, Unplanned Gaseous Release Occurred W/O 15-day Min Holdup. Caused by Either Dirt Trapped in Head Plate & Diaphragm or Uneven Tightening of Compressor Head Bolts | /01T-0:on 800801,during Vol Control Tank Venting, Unplanned Gaseous Release Occurred W/O 15-day Min Holdup. Caused by Either Dirt Trapped in Head Plate & Diaphragm or Uneven Tightening of Compressor Head Bolts | | | 05000255/LER-1980-026, Forwards LER 80-026/03L-0 | Forwards LER 80-026/03L-0 | | | 05000255/LER-1980-026-03, /03L-0:on 800719,during Refilling of Safety Injection tanks,FT-0313 Found Inoperable.Caused by Failure to Close Instrument Equalizing Valve During Recent Calibr | /03L-0:on 800719,during Refilling of Safety Injection tanks,FT-0313 Found Inoperable.Caused by Failure to Close Instrument Equalizing Valve During Recent Calibr | | | 05000255/LER-1980-027-01, During Venting of Quench Tank to Waste Gas Surge Tank,Gaseous Release Occurred W/O 15 Day Min Holdup.Caused by Leaking Isolation Valve & Valve Pin Disassembly.Pin Replaced | During Venting of Quench Tank to Waste Gas Surge Tank,Gaseous Release Occurred W/O 15 Day Min Holdup.Caused by Leaking Isolation Valve & Valve Pin Disassembly.Pin Replaced | | | 05000255/LER-1980-027, Forwards Updated LER 80-027/01X-1 | Forwards Updated LER 80-027/01X-1 | |
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