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an nei While reviewing containment isolation circuitry on January 14, 1987, plant engineering personnel discovered that four containment penetrations (PEN]
associated with the containment hydrogen monitoring system [IK;45] did not employ 'edundant isolation logic. Containment penetrations 21, 21A, 40A and 40B each contain two solenoid-operated isolation valves (IK;ISV]; however, both valves are operated by the same containment isolation channel. The Plant was in cold shutdown condition at the time of discovery.
A modification is being performed which'will provide redundant containment isolation to both independent channels of the containment hydrogen monitoring system, such that isolation of all eight solenoid valves is completed via an isolation signal from either the left or right channel containment high pressure or radiation signals.
In order to further eliminate the possibility of single mode failure, an additional auxiliary relay will be installed between the containment isolation contacts and the solenoids controlling the containment isolation valves. The modifications described above are scheduled to be complaced before the primary coolant system temperature is taken above 210 degrees.
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Description
While reviewing containment isolation circuitry on January 14, 1987, plant engineering personnel discovered that four containment penetrations [ PEN]
associated with the containment hydrogen monitoring system [1K;45] did not employ redundant isolation logic. Containment penetrations 21, 21A, 40A and 40B each contain two solenoid-operated isolation valves [IK;ISV); however, both valves are operated by the same containment isolation channel. The Plant was in cold shutdown condition at the time of discovery.
The containment hydrogen monitoring system consists of two independent channels which provide separate and redundant indication of containment hydrogen concentration. Presently, containment isolation initiated by the left channel of a containment high pressure or radiation signal closes both isolation valves on penetrations 21 and 21A, while containment isolation by the right channel closes both isolation valves on penetrations 40A and 40B.
Review of the records pertaining to the major modifications completed in 1983 indicate that system design criteria given to the architect / engineer (Gilbert / Commonwealth Associates) were not developed as prescribed.
Subsequently, the containment hydrogen monitoring system was installed as designed by the architect / engineer lacking redundant containment isolation logic, subject to single mode failure.
Cause of the Event
On June 24, 1982, the system design description for the containment hydrogen monitoring system was completed by architect / engineer (AE), Gilbert /
Commonwealth Associates. The system design description was prepared under system design criteria provided by the licensee; however, subsequent records review indicate that the AE did not wholly implement the design criteria as prescribed. Consequently, the containment hydrogen monitoring system was installed utilizing the system design description provided by the AE without redundant containment isolation logic, subject to single mode failure.
Analysis of the Event
The event is being reported under 10CFR50.73(a)(2)(vi) due to the subsequent discovery of a design inadequacy associated with the containment hydrogen monitoring system.
The resultant safety consequences discovered within this event are considered to be insignificant in that:
- 1. The piping associated with the containment hydrogen monitoring system has a combined area less than 0.5 square inches.
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- 2. The containment hydrogen monitoring system is a closed system (all supply air from the containment building is returned to the containment building).
- 3. In order to have fission products escape through one of the associated penetrations and not be returned to the containment building the following must occur concurrently:
a) an accident which breaches the primary coolant system b) core damage from that accident c) failure of containment isolation d) failure of the monitoring system piping
Corrective Actions
A modification is being performed which will provide redundant containment isolation to both independent channels of the containment hydrogen monitoring system, such that isolation of all eight solenoid valves is completed via an isolation signal from either the left or right channel containment high pressure or radiation signals.
In order to further eliminate the possibility of single mode failure, an additional auxiliary relay will be installed between the containment isolation contacts and the solenoids controlling the containment isolation valves.
The modifications described above are scheduled to be completed before the primary coolant system temperature is taken above 210 degrees.
Plant engineering is reviewing circuitry for all valves closed by containment isolation signals to assure proper system operation is achieved. Also, all other modifications in which the AE described above was involved will be i
reviewed to determine if similar design problems exist.
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Additional Information
, Containment Penetration Associated Isolation Valves 21 SV-2415A SV-2415B 21A SV-2413A SV-2413B 40A SV-2414A SV-2414B 40B SV-2412A SV-2412B l
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- - t Consumers Power rewaums AMENIEAAr5 MISERE55 General Offices: 1946 West Pernali Road, Jackson, MI 49201 + (517) 788-0550 February 26, 1987 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 DOCKET 50-255 - LICENSE DPR PALISADES PLANT -
LICENSEE EVENT REPORT 87-001, REVISION 1 - NON-REDUNDAN2 CONTAINMENT ISOLATION ASSOCIATED WITH H MONITORING SYSTEM 2
Licensee Event Report (LER) 87-01, Revision 1 (Non-Redundant Containment Isolation Associated with H Monitoring System) is attached. This event is 2
reportable to the NRC per IUCFR50.73(a)(2)(v). The revision is necessary to update the Corrective Action section as indicated by vertical bars in the margin.
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J Brian D Johnson Staff Licensing Engineer CC Administrator, Region III, USNRC NRC Resident Inspector - Palisades Attachment i l i
OC0287-0055-NLO4
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| 05000255/LER-1987-001, :on 870114,plant Engineering Personnel Discovered Four Containment Penetrations Did Not Employ Redundant Isolation Logic.Caused by Architect/Engineer Error.Mod Being Performed |
- on 870114,plant Engineering Personnel Discovered Four Containment Penetrations Did Not Employ Redundant Isolation Logic.Caused by Architect/Engineer Error.Mod Being Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vi) | | 05000255/LER-1987-001-01, :on 870114,containment Penetrations Associated W/Containment Hydrogen Monitoring Sys Did Not Employ Redundant Isolation Logic.Caused by Sys Design Description Not Being Implemented as Prescribed |
- on 870114,containment Penetrations Associated W/Containment Hydrogen Monitoring Sys Did Not Employ Redundant Isolation Logic.Caused by Sys Design Description Not Being Implemented as Prescribed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vi) | | 05000255/LER-1987-002, :on 870115,noise Spike in Nuclear Instrumentation Resulted in Inadvertent Reactor Protection Sys Actuation.Caused by Corroded Cable Connector Pin at Interface of Detector Element.Element Replaced |
- on 870115,noise Spike in Nuclear Instrumentation Resulted in Inadvertent Reactor Protection Sys Actuation.Caused by Corroded Cable Connector Pin at Interface of Detector Element.Element Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-003, :on 870119,discovered Seven Valve Operators Lacked T-drains in End Bell of Motor Housing.Caused by Motor T-drains Improperly Installed.Procedure Established to Provide Administrative Controls Over Equipment |
- on 870119,discovered Seven Valve Operators Lacked T-drains in End Bell of Motor Housing.Caused by Motor T-drains Improperly Installed.Procedure Established to Provide Administrative Controls Over Equipment
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000255/LER-1987-004, :on 870123,charging Pump P-55A Declared Inoperable.Caused by Sporadic Mechanical Operation of Circuit Breaker.On 870205,ITE Circuit Breaker Models K225 & K600 Found Not Functionally Interchangeable |
- on 870123,charging Pump P-55A Declared Inoperable.Caused by Sporadic Mechanical Operation of Circuit Breaker.On 870205,ITE Circuit Breaker Models K225 & K600 Found Not Functionally Interchangeable
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(1) | | 05000255/LER-1987-005, :on 860216,lifted Relief Valve on Steam Generator Secondary Manway Identified,Constituting Failed Containment Penetration.Caused by Failure of Inner Manway Gasket & Improper Valve Installation |
- on 860216,lifted Relief Valve on Steam Generator Secondary Manway Identified,Constituting Failed Containment Penetration.Caused by Failure of Inner Manway Gasket & Improper Valve Installation
| 10 CFR 50.73(a)(2)(1) | | 05000255/LER-1987-006, :on 870213,inadvertent Low Temp Overpressure Protection Sys Actuation Occurred.Caused by Electrical Spike in Channel a Pressure Indication Circuitry.Procedural Controls Instituted to Prevent Recurrence |
- on 870213,inadvertent Low Temp Overpressure Protection Sys Actuation Occurred.Caused by Electrical Spike in Channel a Pressure Indication Circuitry.Procedural Controls Instituted to Prevent Recurrence
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-007, :on 870216,max Hypothetical Accident Safety Analysis Discrepancy Identified.Caused by Incorrectly Identified Calculational Assumptions Re Time for Introduction of Hydrazine Spray Water |
- on 870216,max Hypothetical Accident Safety Analysis Discrepancy Identified.Caused by Incorrectly Identified Calculational Assumptions Re Time for Introduction of Hydrazine Spray Water
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(B) | | 05000255/LER-1987-008, :on 870311,reactor Trip Occured While Performing Reactor Protection Matrix Relay Test.Caused by Dirty Contacts on Matrix Relay Test Switch Not Allowing Full Current to Test Coils.Switches to Be Replaced |
- on 870311,reactor Trip Occured While Performing Reactor Protection Matrix Relay Test.Caused by Dirty Contacts on Matrix Relay Test Switch Not Allowing Full Current to Test Coils.Switches to Be Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-009, :on 870325,auxiliary Feedwater Sys Actuation Signal Received Due to Low Water Level in Steam Generator. Caused by Shrinkage of Steam Generator Level During Testing. Personnel Informed of Circumstances of Event |
- on 870325,auxiliary Feedwater Sys Actuation Signal Received Due to Low Water Level in Steam Generator. Caused by Shrinkage of Steam Generator Level During Testing. Personnel Informed of Circumstances of Event
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-010, :on 870322 & 0426,water Flow Switch Fire Detectors Identified Inoperable.Caused by Eroded Flow Sensing Mechanism.Two Detectors Replaced & Remaining Units Will Be Replaced |
- on 870322 & 0426,water Flow Switch Fire Detectors Identified Inoperable.Caused by Eroded Flow Sensing Mechanism.Two Detectors Replaced & Remaining Units Will Be Replaced
| | | 05000255/LER-1987-011, :on 870412,manual Reactor Trip Initiated by Operations Personnel.Caused by Tooth Breaking Off Electric Hydraulic Control Fluid Pump Rotor.Pump B Disassembled & Sent to Corporate Lab for Further Analysis |
- on 870412,manual Reactor Trip Initiated by Operations Personnel.Caused by Tooth Breaking Off Electric Hydraulic Control Fluid Pump Rotor.Pump B Disassembled & Sent to Corporate Lab for Further Analysis
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-012, :on 870417,turbine Generator Trip on Reverse Power Caused Actuation of Standby Diesel Generator 1-1. Caused by electro-hydraulic Control Sys Fluid Leak from Turbine Interface Valve.Adjustments Made |
- on 870417,turbine Generator Trip on Reverse Power Caused Actuation of Standby Diesel Generator 1-1. Caused by electro-hydraulic Control Sys Fluid Leak from Turbine Interface Valve.Adjustments Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-013, :on 870322,personnel Identified That Water Flow Switch Fire Detector WFS-262 (Kp;Fis) Inoperable.Caused by Failure to Perform 1 H Fire Watch.Quarterly Test Revised to Include Refs to Appropriate Tech Specs |
- on 870322,personnel Identified That Water Flow Switch Fire Detector WFS-262 (Kp;Fis) Inoperable.Caused by Failure to Perform 1 H Fire Watch.Quarterly Test Revised to Include Refs to Appropriate Tech Specs
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-014, :on 870427,primary Data Logger Computer Memory Failed Causing in-core Alarm Sys to Be Inoperable.Caused by Operator Misinterpreting Tech Spec Action Statement.Tech Spec Revised |
- on 870427,primary Data Logger Computer Memory Failed Causing in-core Alarm Sys to Be Inoperable.Caused by Operator Misinterpreting Tech Spec Action Statement.Tech Spec Revised
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-015-01, :on 870322,during Performance of Fire Suppression Sys Flow Operability Test,Water Flow Switch Fire Detector Found Inoperable & Fire Watch Not Begun,Per Tech Specs.Caused by Personnel Error.Test Revised |
- on 870322,during Performance of Fire Suppression Sys Flow Operability Test,Water Flow Switch Fire Detector Found Inoperable & Fire Watch Not Begun,Per Tech Specs.Caused by Personnel Error.Test Revised
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-015, :on 840804,turbine Trip Occurred,Resulting in Automatic Reactor Trip Due to Loss of Load.Caused by Loss of Electrohydraulic Control Fluid Pressure.Breaker Contacts for Feedwater Breakers Cleaned & Adjusted |
- on 840804,turbine Trip Occurred,Resulting in Automatic Reactor Trip Due to Loss of Load.Caused by Loss of Electrohydraulic Control Fluid Pressure.Breaker Contacts for Feedwater Breakers Cleaned & Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-016, :on 870522,reactor Manually Tripped Following Errant Closure of Main Feedwater Pump Turbine Driver Exhaust Valve MV-159FW.Caused by Poor Communication Between Operators While Performing Valve Lineup |
- on 870522,reactor Manually Tripped Following Errant Closure of Main Feedwater Pump Turbine Driver Exhaust Valve MV-159FW.Caused by Poor Communication Between Operators While Performing Valve Lineup
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-017, Forwards Semiannual Radioactive Effluent Release Rept... Jan-June 1987 & Corrected Semiannual Rept for Jul-Dec 1986. LER 87-017 Also Encl Due to Corrective Action Taken Re Failure to Make Flow Rate Estimates During Release | Forwards Semiannual Radioactive Effluent Release Rept... Jan-June 1987 & Corrected Semiannual Rept for Jul-Dec 1986. LER 87-017 Also Encl Due to Corrective Action Taken Re Failure to Make Flow Rate Estimates During Release | | | 05000255/LER-1987-018, :on 870620,primary Coolant Sys Temp Dropped Below 525 F Due to Improper Valve Operation.Caused by Plugged Close Port in Valve Positioner.Sys Mod Completed & Carbon Manifolds Replaced W/Copper |
- on 870620,primary Coolant Sys Temp Dropped Below 525 F Due to Improper Valve Operation.Caused by Plugged Close Port in Valve Positioner.Sys Mod Completed & Carbon Manifolds Replaced W/Copper
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-019-02, :on 870621,diesel Generator 1-1 & 1-2 Inadvertently Actuated While Personnel Attempted to Latch Turbine Generator.Caused by Failure of Autostop Oil Pressure Switch.Sop 8 Revised to Instruct Operations |
- on 870621,diesel Generator 1-1 & 1-2 Inadvertently Actuated While Personnel Attempted to Latch Turbine Generator.Caused by Failure of Autostop Oil Pressure Switch.Sop 8 Revised to Instruct Operations
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-020, :on 870708,gases Contained in Waste Gas Decay Tank T-68A Released to Atmosphere W/O Being Held for Min of 15 Days.Caused by Maint Personnel Removing Flange from Relief Valve Not Tagged Out of Svc |
- on 870708,gases Contained in Waste Gas Decay Tank T-68A Released to Atmosphere W/O Being Held for Min of 15 Days.Caused by Maint Personnel Removing Flange from Relief Valve Not Tagged Out of Svc
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-021, :on 870710,reactor Manually Tripped from 14% of Rated Power.Caused by Oil Leak from Upper Reservoir of Primary Coolant Pump P-50D.Cracked Discharge Line Associated W/Backstop Lube Oil Pump Removed & Replaced |
- on 870710,reactor Manually Tripped from 14% of Rated Power.Caused by Oil Leak from Upper Reservoir of Primary Coolant Pump P-50D.Cracked Discharge Line Associated W/Backstop Lube Oil Pump Removed & Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-022, :on 870712,primary Coolant Sys Temp Dropped Below 525 F Thus Violating Tech Spec 3.1.3(c).Caused by Main Feedwater Regulating Valve CV-0701 Being Placed in Open Position.Valve Closed & Procedures Revised |
- on 870712,primary Coolant Sys Temp Dropped Below 525 F Thus Violating Tech Spec 3.1.3(c).Caused by Main Feedwater Regulating Valve CV-0701 Being Placed in Open Position.Valve Closed & Procedures Revised
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-023, :on 870621 & 0712,diesel Generators 1-1 & 1-2 Inadvertently Actuated.Caused by Operator Error.Sop 8 Revised to Include Precautionary Statements & Operator Guidance Re Potential for Actuation |
- on 870621 & 0712,diesel Generators 1-1 & 1-2 Inadvertently Actuated.Caused by Operator Error.Sop 8 Revised to Include Precautionary Statements & Operator Guidance Re Potential for Actuation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-024, :on 870714,unusual Event Declared Based on Loss of Offsite Power.Caused by Fault on 1-2 Startup Transformer Due to Contaminants in Deluge Sys Water.Deluge Sys Will Be Flushed Quarterly |
- on 870714,unusual Event Declared Based on Loss of Offsite Power.Caused by Fault on 1-2 Startup Transformer Due to Contaminants in Deluge Sys Water.Deluge Sys Will Be Flushed Quarterly
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-025, :on 870817,electro-hydraulic Control Sys Supply Line Failed.Caused by Rupture of Flexible Fluid Supply Hose to Governor Valve.Manual Reactor Trip Initiated.Flexible Hose Replaced W/Rigid Tubing |
- on 870817,electro-hydraulic Control Sys Supply Line Failed.Caused by Rupture of Flexible Fluid Supply Hose to Governor Valve.Manual Reactor Trip Initiated.Flexible Hose Replaced W/Rigid Tubing
| 10 CFR 50.73(a)(2) | | 05000255/LER-1987-026, :on 870821,audible Air Leakage Identified from Containment Into Airlock Through Closed Inner Airlock Door, in Violation of Tech Specs.Caused by Procedural Deficiency. Sealing Surface Adjusted Into Continuous Bead |
- on 870821,audible Air Leakage Identified from Containment Into Airlock Through Closed Inner Airlock Door, in Violation of Tech Specs.Caused by Procedural Deficiency. Sealing Surface Adjusted Into Continuous Bead
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-027, :on 870823,automatic Reactor Trip Occurred Due to Loss of Field in Main Generator.Caused by Failure of Main Generator Voltage Regulator Output.Failed Bias Supply Potentiometer Replaced & Tested |
- on 870823,automatic Reactor Trip Occurred Due to Loss of Field in Main Generator.Caused by Failure of Main Generator Voltage Regulator Output.Failed Bias Supply Potentiometer Replaced & Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-028, :on 870825,primary Coolant Sys Temp Dropped Below 525 F.Caused by Starting of Main Feedwater Pump P-1B After Boron Addition to Primary Coolant Sys.Control Rods Withdrawn & Tech Spec Section 3.1.3c Changed |
- on 870825,primary Coolant Sys Temp Dropped Below 525 F.Caused by Starting of Main Feedwater Pump P-1B After Boron Addition to Primary Coolant Sys.Control Rods Withdrawn & Tech Spec Section 3.1.3c Changed
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-029-02, :on 870901,auxiliary Feedwater Actuation Sys Inadvertently Actuated.Caused by Personnel Error.Tech Spec Surveillance Procedure MI-39 Being Reviewed to Determine If Required Actions Can Be More Clearly Defined |
- on 870901,auxiliary Feedwater Actuation Sys Inadvertently Actuated.Caused by Personnel Error.Tech Spec Surveillance Procedure MI-39 Being Reviewed to Determine If Required Actions Can Be More Clearly Defined
| | | 05000255/LER-1987-030, :on 870903,QA Personnel Identified That Safety Injection tank,T-82B (Bp;Tk),Not Being Sampled for Boron Concentration at Frequency Specified in Facility Tech Specs. Tech Spec Change Request Submitted on 870911 |
- on 870903,QA Personnel Identified That Safety Injection tank,T-82B (Bp;Tk),Not Being Sampled for Boron Concentration at Frequency Specified in Facility Tech Specs. Tech Spec Change Request Submitted on 870911
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-031, :on 870903,diesel Generator Declared Inoperable.Caused by Slow Voltage Regulator Response. Adjustments Made to Diesel Generator Ref Voltage & Voltage Stability Feedback Circuit |
- on 870903,diesel Generator Declared Inoperable.Caused by Slow Voltage Regulator Response. Adjustments Made to Diesel Generator Ref Voltage & Voltage Stability Feedback Circuit
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-032, :on 870910,LPSI Pump P-67B Inadvertently Actuated During Preventive Maint to Contacts of DBA Sequencer.Caused by Personnel Slipping Screwdriver Off Head of Cam Screw.Cam & Sequencer Will Be Replaced |
- on 870910,LPSI Pump P-67B Inadvertently Actuated During Preventive Maint to Contacts of DBA Sequencer.Caused by Personnel Slipping Screwdriver Off Head of Cam Screw.Cam & Sequencer Will Be Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1987-033, :on 870903,high-range Noble Gas Stack Monitor Declared Inoperable When Detector Output Values Fell Below Tech Spec Requirements.Caused by Failure of Anode Insulator. Detector Will Be Refurbished by 871115 |
- on 870903,high-range Noble Gas Stack Monitor Declared Inoperable When Detector Output Values Fell Below Tech Spec Requirements.Caused by Failure of Anode Insulator. Detector Will Be Refurbished by 871115
| | | 05000255/LER-1987-034, :on 871002,normal Range Gas Stack Effluent & Particulate Stack Effluent Monitors Found Inoperable Due to Low Flow Condition.Caused by Inadequate Tech Spec Procedure. Alarm Window Will Be Modified |
- on 871002,normal Range Gas Stack Effluent & Particulate Stack Effluent Monitors Found Inoperable Due to Low Flow Condition.Caused by Inadequate Tech Spec Procedure. Alarm Window Will Be Modified
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-035, :on 871015,LPSI Pump P-67A Manually Secured from Operation Due to Erratic Discharge Pressure & Flow. Caused by Improperly Placed Jumper.Review of Requirements & Controls on Work Planning Process in Progress |
- on 871015,LPSI Pump P-67A Manually Secured from Operation Due to Erratic Discharge Pressure & Flow. Caused by Improperly Placed Jumper.Review of Requirements & Controls on Work Planning Process in Progress
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000255/LER-1987-036, :on 871019,waste Gas Decay Tank Released to Atmosphere After Isolation on Same Day.Caused by Data Transposition Error in Completion of Batch Card.Procedure Rev in Progress.Trip Function Tested |
- on 871019,waste Gas Decay Tank Released to Atmosphere After Isolation on Same Day.Caused by Data Transposition Error in Completion of Batch Card.Procedure Rev in Progress.Trip Function Tested
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-037, :on 871106,licensee Failed to Take Compensatory Measures During Temporary Loss of Fire Suppression Sys. Caused by Misleading Plant Diagram.Change Request Initiated to Correct Misleading Diagram |
- on 871106,licensee Failed to Take Compensatory Measures During Temporary Loss of Fire Suppression Sys. Caused by Misleading Plant Diagram.Change Request Initiated to Correct Misleading Diagram
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-038, :on 871022,auxiliary Operator Had Worked 28 H in 48 H Period,Exceeding Work Hour Limitations.Caused by Operator Unfamiliarity W/Overtime Limitation Criteria.Memo Issued as Part of Required Reading Program |
- on 871022,auxiliary Operator Had Worked 28 H in 48 H Period,Exceeding Work Hour Limitations.Caused by Operator Unfamiliarity W/Overtime Limitation Criteria.Memo Issued as Part of Required Reading Program
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1987-039, :on 871030,discovered That Charging Pump P-55B Would Not Automatically Actuate.Caused by Failure to Fully Comply W/Charging Needs Due to Misidentification.Pump P-55B Declared Administratively Inoperable |
- on 871030,discovered That Charging Pump P-55B Would Not Automatically Actuate.Caused by Failure to Fully Comply W/Charging Needs Due to Misidentification.Pump P-55B Declared Administratively Inoperable
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000255/LER-1987-040, :on 871122,level in Diesel Oil Storage Tank T-10 Below Tech Specs Limit.Caused by Erroneous Readings on Indicator LIA-1400.Diesel Oil Added to Fill Tank & Level Verified Manually |
- on 871122,level in Diesel Oil Storage Tank T-10 Below Tech Specs Limit.Caused by Erroneous Readings on Indicator LIA-1400.Diesel Oil Added to Fill Tank & Level Verified Manually
| 10 CFR 50.73(a)(2)(i) |
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