05000251/FIN-2014003-01
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Finding | |
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Title | Failure to Implement a Surveillance Procedure to Perform a RCS Unidentified Leak Rate Statistical Calculation |
Description | The NRC identified a non-cited violation (NCV) of Technical Specification 6.8.1, Procedures, for the licensees failure to implement procedure 4-OSP-041.1, Reactor Coolant System (RCS) Leak Rate Calculation. Specifically, the licensee did not perform a Unit 4 reactor coolant system leak rate statistical calculation to determine the change in the average unidentified RCS leak rate which resulted in not performing a Level 3 RCS leak rate investigation. Corrective actions included performing the calculation, performing a detailed leak investigation, and entering the performance deficiency in their corrective action program as action request 01962745. The performance deficiency was determined to be more than minor because it was associated with the initiating events cornerstone attribute of human performance and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inspectors determined that the licensees failure to fully implement the procedure directly resulted in not performing an RCS Level 3 leak rate investigation. The finding was screened using IMC 0609, Significance Determination Process, Attachment 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1, 2012, and Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1 for Initiating Events , dated July 1, 2012. The inspectors determined the finding was of very low safety significance because after a reasonable assessment of the degradation, the inspectors determined the finding would not have likely affected other systems used to mitigate a Loss of Coolant Accident (LOCA) resulting in total loss of their function. This finding was associated with a cross-cutting aspect in the procedure adherence component in the human performance area because the licensee failed to fully implement the RCS leak rate calculation procedure (H.8). |
Site: | Turkey Point ![]() |
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Report | IR 05000251/2014003 Section 1R22 |
Date counted | Jun 30, 2014 (2014Q2) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.22 |
Inspectors (proximate) | A Butcavage J Munday M Endress R Williams T Hoeg |
Violation of: | Technical Specification - Procedures Technical Specification |
CCA | H.8, Procedure Adherence |
INPO aspect | WP.4 |
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Finding - Turkey Point - IR 05000251/2014003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Turkey Point) @ 2014Q2
Self-Identified List (Turkey Point)
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