05000250/FIN-2014008-01
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Finding | |
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Title | Failure to Properly Program the Turbine Generator Digital Control System Load Drop Anticipatory Circuit Results in a Manual Reactor Trip |
Description | A self-revealing finding was identified for the failure to establish new digital software set points for the load drop anticipatory (LDA) logic circuit associated with an extended power uprate (EPU) digital turbine electro-hydraulic control (EHC) system design modification. Specifically, the software for the LDA logic circuit was programmed to reset at a value that would not be reached during a normal reactor plant shutdown before the turbine control system sensed a loss of load condition and closed the turbine control valves. As a result, during a planned Unit 3 reactor plant shutdown, the LDA control logic unexpectedly closed the turbine control valves at 25 percent reactor power. The operators then manually tripped the unit based on the indication of loss of turbine load in the control room. Licensee Unit 3 software engineering change (EC) package 246849 change request notice (CRN) 253 Attachment 5, Turbine Control Initial Values, instructed the programmer to set the LDA disarm value to 50 percent turbine load. Contrary to this instruction, the programmer set the disarm value to 50 pounds per square inch gauge (psig) steam pressure. The failure of the programmer to establish the proper set point value in the LDA reset logic was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment reliability attribute of the initiating events cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during power operations. The finding was determined to be of very low safety significance (Green) based on Exhibit 1, Initiating Events Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process for Findings At-Power (dated June 19, 2012). This was due to the fact that the finding did not result in a loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. The inspectors determined the cause of this finding was associated with a cross cutting aspect of procedure adherence. Specifically, the licensee set the turbine control valve LDA reset point to 50 psig instead of 50 percent turbine load as prescribed in EC 246849. |
Site: | Turkey Point ![]() |
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Report | IR 05000250/2014008 Section 4OA3 |
Date counted | Mar 31, 2014 (2014Q1) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | D Rich M Endress T Hoeg W Deschaine |
CCA | H.8, Procedure Adherence |
INPO aspect | WP.4 |
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Finding - Turkey Point - IR 05000250/2014008 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Turkey Point) @ 2014Q1
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