LER-1983-014, Forwards LER 83-014/01T-0.Detailed Event Analysis Encl |
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W' s
GPU Nuclear g
gf P.O. Box 388 Forked River, New Jersey 08731 609-693-6000 Writer's Direct Dial Number:
April 20, 1983 Regional Administrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19405
Dear Sir:
Subj ect: Oyster Creek Nuclear Generating Station Docket No. 50-219 Licensee Event Report Reportable Occurrence No. 50-219/83-14/01T This letter forwards three copies of a Licensee Event Report (LER) to report Reportable Occurrence No. 50-219/83-14/01T in compliance with paragraph 6.9.2.a.9 of the Technical Specifications.
Very truly yours, e
fyy, 2>J1,11 Peter B. Fiedler
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Vice President and Director Oyster Creek PBF:jal Enclosure s cc: Director (40 copies)
Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.
20555 Dire ctor (3)
Of fice of Management Information and Program Control U.S. Nuclear Regulatory Commission Washington, D.C.
20555 NRC Resident Inspector
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Oyster Creek Nuclear Generating Station Forked River, NJ 08731 8305030441 830420 PDR ADOCK 05000219 S
PDR GPU Nuclear is a part of the General Public Utilities Systern p
t-1 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportabir Occurrence No. 50-219/83-14/01T Report Date April 20, 1983 Occurrence Date April 6,1983 Identification of Occurrence Discovery of a design deficiency which would have resulted in not meeting a Limiting Condition for Operation as defined in the Technical Specificationn, paragraph 3.5.B.
This event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.a.9.
1 Conditions Prior to Occurrence 4
Mode Switch Refuel Thenmal Power 0 MWt Generator Load 0 MWe 0
Reactor Coolant Temperature 4212 F
- - Description of Occurrence On Wednesday, April 6,1983, af ter an investigation of the Standby Gas Treatment System (SGTS), a design deficiency was discovered.
Apparent Cause of Occurrence The cause of the occurrence is attributed to a design deficiency in the control power circuitry for the heating coils in the SGTS.
Analysis of Occurrence The SGTS filters and exhausts the Reactor Building atmosphere to the stack in the event of certain accident situations in order. to minimize the release of radioactive materials to the environment.
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1-Licensee Event Report Page 2 Reportable Occurrence No. 50-219/83-14/01T Heating coils are provided in each SGTS train. The heating coils are designed L
to reduce the humidity in the air stream to 70% relative humidity.
The SGTS consts,ts of two parallel trains of filters and fans, each designed to be capable of 99% efficiency in retaining radioactive iodine and particulates that may be present in the Reactor Building during and af ter an accident.
Presently, control circuitry for heating coils in both SGTS trains receive their 120V AC power from Motor Control Center (MCC) 1A24.
If, during an accident situation, the SCTS is called for and Diesel Genere. tor No.1 failed, while supplying the power to the heating coil control circuitry, SCTS charcoal filter efficiency would be reduced.
Corrective Action
As immediate corrective action, a temporary power feed will be installed which i
will supply SGTS II's heating coil f rom MCC IB24 and leave SGTS I's heating coil supplied by MCC 1A24 thus providing redundant power sources.
A permanent modification will be installed during the current refueling / maintenance outage.
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| 05000219/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-002-03, /03L-0:on 830123,startup Banks Removed from Svc Due to Dilution Plant Main Breaker Cable Termination Failure.Cause Under Investigation.Dilution Pump Power Feed Terminations Replaced | /03L-0:on 830123,startup Banks Removed from Svc Due to Dilution Plant Main Breaker Cable Termination Failure.Cause Under Investigation.Dilution Pump Power Feed Terminations Replaced | | | 05000219/LER-1983-003-03, /03L-0:on 830118,during Maint of Control Rod Drive Pump A,Pump Vent Line Broke Off.Core Spray Pump Nzoia Wetdown & B Pump Inadvertently Tripped.Cause Not Stated. Pump Removed from Svc & Motor Tested | /03L-0:on 830118,during Maint of Control Rod Drive Pump A,Pump Vent Line Broke Off.Core Spray Pump Nzoia Wetdown & B Pump Inadvertently Tripped.Cause Not Stated. Pump Removed from Svc & Motor Tested | | | 05000219/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-004-03, /03L-0:on 830331,during Preventive Maint,Control Rod Drive Feed Pump NC08A Circuit Breaker Mechanically Closed Per Procedure.Investigation Revealed Breaker Should Not Have Closed.Caused by Binding Trip Shaft | /03L-0:on 830331,during Preventive Maint,Control Rod Drive Feed Pump NC08A Circuit Breaker Mechanically Closed Per Procedure.Investigation Revealed Breaker Should Not Have Closed.Caused by Binding Trip Shaft | | | 05000219/LER-1983-005-03, /03L-0:on 830126,while Performing Containment Spray Sys Automatic Actuation Test,High Drywell Pressure Switches IP15A,B & C Tripped at Value Greater than Tech Spec Limit.Cause Not Determined.Pressure Switches Readjusted | /03L-0:on 830126,while Performing Containment Spray Sys Automatic Actuation Test,High Drywell Pressure Switches IP15A,B & C Tripped at Value Greater than Tech Spec Limit.Cause Not Determined.Pressure Switches Readjusted | | | 05000219/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-006-03, /03L-0:on 830206,all Automatic Valves Not Lined Up Properly During Execution of Standby Gas Treatment Sys 10 H Operability Test.Caused by Condensation in Fan 1-9 Low Flow Sensing Lines.Lines Cleaned | /03L-0:on 830206,all Automatic Valves Not Lined Up Properly During Execution of Standby Gas Treatment Sys 10 H Operability Test.Caused by Condensation in Fan 1-9 Low Flow Sensing Lines.Lines Cleaned | | | 05000219/LER-1983-007-03, /03L-0:on 830418,during Monthly 10 H Operability Test of Standby Gas Treatment Sys Ii,High Differential Pressure Across Both HEPA Filters Observed.Caused by Plugging of Filters.Filters Replaced | /03L-0:on 830418,during Monthly 10 H Operability Test of Standby Gas Treatment Sys Ii,High Differential Pressure Across Both HEPA Filters Observed.Caused by Plugging of Filters.Filters Replaced | | | 05000219/LER-1983-008-03, /03L-0:on 830314,incorrect Undervoltage Trip Coil Installed on Core Spray Booster Pump Breaker,Preventing Manual Start.Caused by Personnel Error.Coil Replaced | /03L-0:on 830314,incorrect Undervoltage Trip Coil Installed on Core Spray Booster Pump Breaker,Preventing Manual Start.Caused by Personnel Error.Coil Replaced | | | 05000219/LER-1983-008, Forwards LER 83-008/03L-0.Detailed Event Analysis Encl | Forwards LER 83-008/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-009, Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-010-01, /01T-0:on 830307,design Deficiency Discovered When Standby Gas Treatment Sys (SGTS) II Racked Out for Maint. SGTS II Inlet & Outlet Valves Opened,Allowing Recirculation During Sys I Operation.Procedures Revised | /01T-0:on 830307,design Deficiency Discovered When Standby Gas Treatment Sys (SGTS) II Racked Out for Maint. SGTS II Inlet & Outlet Valves Opened,Allowing Recirculation During Sys I Operation.Procedures Revised | | | 05000219/LER-1983-010, Forwards LER 83-010/01T-0.Detailed Event Analysis Encl | Forwards LER 83-010/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-011-03, /03L-0:on 830306,during Standby Gas Treatment Sys 10 H Operability Test in Sys II Preferential Mode,All Automatic Valves Not Lined Up Properly.Caused by Melted Sensing Line for Fan 1-9 Low Flow Switch.Lines Repaired | /03L-0:on 830306,during Standby Gas Treatment Sys 10 H Operability Test in Sys II Preferential Mode,All Automatic Valves Not Lined Up Properly.Caused by Melted Sensing Line for Fan 1-9 Low Flow Switch.Lines Repaired | | | 05000219/LER-1983-012, Forwards LER 83-012/01T-0.Detailed Event Analysis Encl | Forwards LER 83-012/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-012-01, /01T-0:on 830319,door to Main Steam Line Trunnion Room Found Open During Refueling Checkoff.Caused by Design Deficiency,Personnel Error & Failure to Post Sign Identifying Door as Secondary Containment.Door Closed | /01T-0:on 830319,door to Main Steam Line Trunnion Room Found Open During Refueling Checkoff.Caused by Design Deficiency,Personnel Error & Failure to Post Sign Identifying Door as Secondary Containment.Door Closed | | | 05000219/LER-1983-013, Forwards LER 83-013/01T-0.Detailed Event Analysis Encl | Forwards LER 83-013/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-013-01, /01T-0:on 830327,both Doors of Reactor Bldg Personnel Access Airlock Opened Simultaneously.Caused by Personnel Error.Incident Reviewed W/Personnel & Appropriate Disciplinary Action Taken | /01T-0:on 830327,both Doors of Reactor Bldg Personnel Access Airlock Opened Simultaneously.Caused by Personnel Error.Incident Reviewed W/Personnel & Appropriate Disciplinary Action Taken | | | 05000219/LER-1983-014, Forwards LER 83-014/01T-0.Detailed Event Analysis Encl | Forwards LER 83-014/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-014-01, /01T-0:on 830406,design Deficiency Discovered in Heating Coil Control Circuitry for Standby Gas Treatment Sys Trains.Temporary Redundant Power Feed Provided Until Permanent Mod Installed During Current Maint Outage | /01T-0:on 830406,design Deficiency Discovered in Heating Coil Control Circuitry for Standby Gas Treatment Sys Trains.Temporary Redundant Power Feed Provided Until Permanent Mod Installed During Current Maint Outage | | | 05000219/LER-1983-015-03, /03L-0:on 830609,electricians Found Wire Wrapped Around Armature of Undervoltage Trip Device.Caused by Personnel Error in Installation of Wire Gag.Tripcoil,Blown Fuses & Static Time Delay Box Replaced | /03L-0:on 830609,electricians Found Wire Wrapped Around Armature of Undervoltage Trip Device.Caused by Personnel Error in Installation of Wire Gag.Tripcoil,Blown Fuses & Static Time Delay Box Replaced | | | 05000219/LER-1983-017-01, /01T-0:on 830826,arming Relay for Diesel Generator Protective Relay Set at Value Possibly Causing Breaker to Open During Fast Start.Caused by Design Deficiency.Setting Changed | /01T-0:on 830826,arming Relay for Diesel Generator Protective Relay Set at Value Possibly Causing Breaker to Open During Fast Start.Caused by Design Deficiency.Setting Changed | | | 05000219/LER-1983-018-03, /03L Submittal Delayed Due to Need for Plant Operations Review Committee Investigation Into Cause & Corrective Actions.Ro Will Be Submitted by 831108 | /03L Submittal Delayed Due to Need for Plant Operations Review Committee Investigation Into Cause & Corrective Actions.Ro Will Be Submitted by 831108 | | | 05000219/LER-1983-019-03, /03L-0:on 831114,during Surveillance of Standby Gas Treatment Sys,Reactor Bldg Ventilation Valve V-28-22 Failed to Close on Isolation Initiation Signal.Caused by Piece of Piston Breaking Off.Piston Repaired | /03L-0:on 831114,during Surveillance of Standby Gas Treatment Sys,Reactor Bldg Ventilation Valve V-28-22 Failed to Close on Isolation Initiation Signal.Caused by Piece of Piston Breaking Off.Piston Repaired | | | 05000219/LER-1983-020-03, /03L-0:on 830916,svc Water Pump 1-2 Breaker Failed to Trip When Undervoltage Device Deenergized.Caused by Component Failure Due to Burr on Latch Surface.Preventive Maint Done on Breaker & Burr removed.w/831019 Ltr | /03L-0:on 830916,svc Water Pump 1-2 Breaker Failed to Trip When Undervoltage Device Deenergized.Caused by Component Failure Due to Burr on Latch Surface.Preventive Maint Done on Breaker & Burr removed.w/831019 Ltr | | | 05000219/LER-1983-021-03, /03L-0:on 831012,loss of Main Bus 1A & Emergency Bus 1C Rendered One Standby Gas Treatment Sys Train Inoperable.Stack Gas Sampling Capability Lost for Approx 3 Had Pump a Shutdown Due to Loss of Power | /03L-0:on 831012,loss of Main Bus 1A & Emergency Bus 1C Rendered One Standby Gas Treatment Sys Train Inoperable.Stack Gas Sampling Capability Lost for Approx 3 Had Pump a Shutdown Due to Loss of Power | | | 05000219/LER-1983-025-03, /03L-0:on 831201,maint & Surveillance Procedures Identified as Not Adequately Verifying Excess Flow Check Valves Open Following Operations.Caused by Inadequate Maint & Surveillance Procedures.Procedures Revised | /03L-0:on 831201,maint & Surveillance Procedures Identified as Not Adequately Verifying Excess Flow Check Valves Open Following Operations.Caused by Inadequate Maint & Surveillance Procedures.Procedures Revised | |
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