LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl |
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GPU Nuclear Q
g7 P.O. Box 388 Forked River, New Jersey 08731 609-693-6000 Writer's Direct Dici Number:
March 4, 1983 Mr. Ronald C. Haynes, Administrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
Dear Mr. Haynes:
Subj ect: Oyster Creek Nuclear Generating Station Do cke t No. 50-219 Licensee Event Report Reportable Occurrence No. 50-219/83-06/03L This letter forwards three copies of a Licensee Event Report (LER) to report Reportable Occurrence No. 50-219/83-06/03L in compliance with paragraph 6.9.2.b.2 of the Technical Specifications.
Very truly yours, Pet'er B. Fiedler Vice President and Director Oyster Creek PBF:jal Enclosure s cc: Dire ctor (40 copies)
Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.
20555 Dire ctor (3)
Of fice of Management Information and Program Control U.S. Nuclear Regulatory Commission Washington, D.C.
20555 NRC Resident Inspector Oyster Creek Nuclear Generating Station Forked River, NJ 08731 8303160225 030304 PDR ADOCK 05000 s
y GPU Nuclear is a part of the General Pubhc Utilities System
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OYSTER CREEK NUCLEAR GENERATING STATION
. Forked River,' New Jersey 08731.
Licensee Event Report Reportable Occurrence No. 50-219/83-06/03L
- - Report Date March 4, 1983 Occurrence Date February 6,1983 Identification of Occurrence '
Operation in a degraded mode permitted by limiting condition for operation as specified in the Technical Specifications, paragraph 3.5.B.3, when the low flow switch for Standby Gas Treatment System fan 1-9 failed to sense a low flow condition therefore preventing system II valves from closing. This item is reportable per paragraph 6.9.2.b.2 of the Technical Specifications.
Conditions Frior to Occurrence The plant was operating at steady state power.
Mode Switch. Position Run Power:
Core 803.5 MWt Electrical 232 MWh Description of Occurrence On Sunday, February 6,1983 at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, during the execution of the Standby Gas Treatment System ten hour operability test in the system I preferential mode,' valves V-28-24, V-28-27 and V-28-30 failed to close af ter fan 1-9 tripped as part of the normal system line-up.. System I was declared out of sevice. At 2205 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br /> an operability and flow test was completed in the system II preferential mode with system II functioning normally.
Apparert Cause of Occurrence The apparent cause of this occurrence was moisture accumulation in fan 1-9 low flow switch sensing lines. This moisture and possible icing due to outdoor temperatures below freezing, prevented the flow switch from sensing a low flow Leondition with fan 1-9 off.
j During -normal system operation, valves V-28-24, V-28-27 and V-28-30 would close with a low flow condition sensed by fan 1-9 low flow switch.
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Licensee Event Report Page 2 Reportable Occurrence No. 50-219 /83-06/03L Analysis of Occurrence The Standby Gas Treatment System filters and exhausts the reactor building atmosphere to the stack during secondary containment isolation condition with a minimum release of radioactive materials from the reactor building to the environs.
The safety significance of this event is minimized as the Standby Gas Treatment System was operational in the system II preferential mode in the event that a demand for system operation had occurred.
Corrective Action
The low flow switch sensing lines for system I were blown out with nitrogen to remove existing moisture and the low flow switch was checked for proper operation. On Monday, February 7,1983 at 0220 hours0.00255 days <br />0.0611 hours <br />3.637566e-4 weeks <br />8.371e-5 months <br /> an operability and flow test was completed in the system I preferential mode with system I returned to servi ce.
As a preventative maintenance measure, st 0251 hours0.00291 days <br />0.0697 hours <br />4.150132e-4 weeks <br />9.55055e-5 months <br />, low flow switch sensing lines for system-II were blown out with nitrogen and the low flow switch was checked for proper operation., System II was returned to service following an operability and ficw test.
Failure Data Dwyer Instruments, Inc.
Catalog # 1637.25 Michigan City, Iniiana Switch was repaired and not replaced
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| 05000219/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-002-03, /03L-0:on 830123,startup Banks Removed from Svc Due to Dilution Plant Main Breaker Cable Termination Failure.Cause Under Investigation.Dilution Pump Power Feed Terminations Replaced | /03L-0:on 830123,startup Banks Removed from Svc Due to Dilution Plant Main Breaker Cable Termination Failure.Cause Under Investigation.Dilution Pump Power Feed Terminations Replaced | | | 05000219/LER-1983-003-03, /03L-0:on 830118,during Maint of Control Rod Drive Pump A,Pump Vent Line Broke Off.Core Spray Pump Nzoia Wetdown & B Pump Inadvertently Tripped.Cause Not Stated. Pump Removed from Svc & Motor Tested | /03L-0:on 830118,during Maint of Control Rod Drive Pump A,Pump Vent Line Broke Off.Core Spray Pump Nzoia Wetdown & B Pump Inadvertently Tripped.Cause Not Stated. Pump Removed from Svc & Motor Tested | | | 05000219/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-004-03, /03L-0:on 830331,during Preventive Maint,Control Rod Drive Feed Pump NC08A Circuit Breaker Mechanically Closed Per Procedure.Investigation Revealed Breaker Should Not Have Closed.Caused by Binding Trip Shaft | /03L-0:on 830331,during Preventive Maint,Control Rod Drive Feed Pump NC08A Circuit Breaker Mechanically Closed Per Procedure.Investigation Revealed Breaker Should Not Have Closed.Caused by Binding Trip Shaft | | | 05000219/LER-1983-005-03, /03L-0:on 830126,while Performing Containment Spray Sys Automatic Actuation Test,High Drywell Pressure Switches IP15A,B & C Tripped at Value Greater than Tech Spec Limit.Cause Not Determined.Pressure Switches Readjusted | /03L-0:on 830126,while Performing Containment Spray Sys Automatic Actuation Test,High Drywell Pressure Switches IP15A,B & C Tripped at Value Greater than Tech Spec Limit.Cause Not Determined.Pressure Switches Readjusted | | | 05000219/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-006-03, /03L-0:on 830206,all Automatic Valves Not Lined Up Properly During Execution of Standby Gas Treatment Sys 10 H Operability Test.Caused by Condensation in Fan 1-9 Low Flow Sensing Lines.Lines Cleaned | /03L-0:on 830206,all Automatic Valves Not Lined Up Properly During Execution of Standby Gas Treatment Sys 10 H Operability Test.Caused by Condensation in Fan 1-9 Low Flow Sensing Lines.Lines Cleaned | | | 05000219/LER-1983-007-03, /03L-0:on 830418,during Monthly 10 H Operability Test of Standby Gas Treatment Sys Ii,High Differential Pressure Across Both HEPA Filters Observed.Caused by Plugging of Filters.Filters Replaced | /03L-0:on 830418,during Monthly 10 H Operability Test of Standby Gas Treatment Sys Ii,High Differential Pressure Across Both HEPA Filters Observed.Caused by Plugging of Filters.Filters Replaced | | | 05000219/LER-1983-008-03, /03L-0:on 830314,incorrect Undervoltage Trip Coil Installed on Core Spray Booster Pump Breaker,Preventing Manual Start.Caused by Personnel Error.Coil Replaced | /03L-0:on 830314,incorrect Undervoltage Trip Coil Installed on Core Spray Booster Pump Breaker,Preventing Manual Start.Caused by Personnel Error.Coil Replaced | | | 05000219/LER-1983-008, Forwards LER 83-008/03L-0.Detailed Event Analysis Encl | Forwards LER 83-008/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-009, Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-010-01, /01T-0:on 830307,design Deficiency Discovered When Standby Gas Treatment Sys (SGTS) II Racked Out for Maint. SGTS II Inlet & Outlet Valves Opened,Allowing Recirculation During Sys I Operation.Procedures Revised | /01T-0:on 830307,design Deficiency Discovered When Standby Gas Treatment Sys (SGTS) II Racked Out for Maint. SGTS II Inlet & Outlet Valves Opened,Allowing Recirculation During Sys I Operation.Procedures Revised | | | 05000219/LER-1983-010, Forwards LER 83-010/01T-0.Detailed Event Analysis Encl | Forwards LER 83-010/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-011-03, /03L-0:on 830306,during Standby Gas Treatment Sys 10 H Operability Test in Sys II Preferential Mode,All Automatic Valves Not Lined Up Properly.Caused by Melted Sensing Line for Fan 1-9 Low Flow Switch.Lines Repaired | /03L-0:on 830306,during Standby Gas Treatment Sys 10 H Operability Test in Sys II Preferential Mode,All Automatic Valves Not Lined Up Properly.Caused by Melted Sensing Line for Fan 1-9 Low Flow Switch.Lines Repaired | | | 05000219/LER-1983-012, Forwards LER 83-012/01T-0.Detailed Event Analysis Encl | Forwards LER 83-012/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-012-01, /01T-0:on 830319,door to Main Steam Line Trunnion Room Found Open During Refueling Checkoff.Caused by Design Deficiency,Personnel Error & Failure to Post Sign Identifying Door as Secondary Containment.Door Closed | /01T-0:on 830319,door to Main Steam Line Trunnion Room Found Open During Refueling Checkoff.Caused by Design Deficiency,Personnel Error & Failure to Post Sign Identifying Door as Secondary Containment.Door Closed | | | 05000219/LER-1983-013, Forwards LER 83-013/01T-0.Detailed Event Analysis Encl | Forwards LER 83-013/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-013-01, /01T-0:on 830327,both Doors of Reactor Bldg Personnel Access Airlock Opened Simultaneously.Caused by Personnel Error.Incident Reviewed W/Personnel & Appropriate Disciplinary Action Taken | /01T-0:on 830327,both Doors of Reactor Bldg Personnel Access Airlock Opened Simultaneously.Caused by Personnel Error.Incident Reviewed W/Personnel & Appropriate Disciplinary Action Taken | | | 05000219/LER-1983-014, Forwards LER 83-014/01T-0.Detailed Event Analysis Encl | Forwards LER 83-014/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-014-01, /01T-0:on 830406,design Deficiency Discovered in Heating Coil Control Circuitry for Standby Gas Treatment Sys Trains.Temporary Redundant Power Feed Provided Until Permanent Mod Installed During Current Maint Outage | /01T-0:on 830406,design Deficiency Discovered in Heating Coil Control Circuitry for Standby Gas Treatment Sys Trains.Temporary Redundant Power Feed Provided Until Permanent Mod Installed During Current Maint Outage | | | 05000219/LER-1983-015-03, /03L-0:on 830609,electricians Found Wire Wrapped Around Armature of Undervoltage Trip Device.Caused by Personnel Error in Installation of Wire Gag.Tripcoil,Blown Fuses & Static Time Delay Box Replaced | /03L-0:on 830609,electricians Found Wire Wrapped Around Armature of Undervoltage Trip Device.Caused by Personnel Error in Installation of Wire Gag.Tripcoil,Blown Fuses & Static Time Delay Box Replaced | | | 05000219/LER-1983-017-01, /01T-0:on 830826,arming Relay for Diesel Generator Protective Relay Set at Value Possibly Causing Breaker to Open During Fast Start.Caused by Design Deficiency.Setting Changed | /01T-0:on 830826,arming Relay for Diesel Generator Protective Relay Set at Value Possibly Causing Breaker to Open During Fast Start.Caused by Design Deficiency.Setting Changed | | | 05000219/LER-1983-018-03, /03L Submittal Delayed Due to Need for Plant Operations Review Committee Investigation Into Cause & Corrective Actions.Ro Will Be Submitted by 831108 | /03L Submittal Delayed Due to Need for Plant Operations Review Committee Investigation Into Cause & Corrective Actions.Ro Will Be Submitted by 831108 | | | 05000219/LER-1983-019-03, /03L-0:on 831114,during Surveillance of Standby Gas Treatment Sys,Reactor Bldg Ventilation Valve V-28-22 Failed to Close on Isolation Initiation Signal.Caused by Piece of Piston Breaking Off.Piston Repaired | /03L-0:on 831114,during Surveillance of Standby Gas Treatment Sys,Reactor Bldg Ventilation Valve V-28-22 Failed to Close on Isolation Initiation Signal.Caused by Piece of Piston Breaking Off.Piston Repaired | | | 05000219/LER-1983-020-03, /03L-0:on 830916,svc Water Pump 1-2 Breaker Failed to Trip When Undervoltage Device Deenergized.Caused by Component Failure Due to Burr on Latch Surface.Preventive Maint Done on Breaker & Burr removed.w/831019 Ltr | /03L-0:on 830916,svc Water Pump 1-2 Breaker Failed to Trip When Undervoltage Device Deenergized.Caused by Component Failure Due to Burr on Latch Surface.Preventive Maint Done on Breaker & Burr removed.w/831019 Ltr | | | 05000219/LER-1983-021-03, /03L-0:on 831012,loss of Main Bus 1A & Emergency Bus 1C Rendered One Standby Gas Treatment Sys Train Inoperable.Stack Gas Sampling Capability Lost for Approx 3 Had Pump a Shutdown Due to Loss of Power | /03L-0:on 831012,loss of Main Bus 1A & Emergency Bus 1C Rendered One Standby Gas Treatment Sys Train Inoperable.Stack Gas Sampling Capability Lost for Approx 3 Had Pump a Shutdown Due to Loss of Power | | | 05000219/LER-1983-025-03, /03L-0:on 831201,maint & Surveillance Procedures Identified as Not Adequately Verifying Excess Flow Check Valves Open Following Operations.Caused by Inadequate Maint & Surveillance Procedures.Procedures Revised | /03L-0:on 831201,maint & Surveillance Procedures Identified as Not Adequately Verifying Excess Flow Check Valves Open Following Operations.Caused by Inadequate Maint & Surveillance Procedures.Procedures Revised | |
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