LER-1983-010, Forwards LER 83-010/01T-0.Detailed Event Analysis Encl |
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GPU Nuclear Q
g7 P.O. Box 388 Forked River, New Jersey 08731 609-693-6000 Writer's Direct Dial Number:
March 23, 1983 Mr. Ronald C. Haynes, Mministrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
Dear Mr. Haynes:
Subj ect: Oyster Creek Nuclear Generating Station Docket No. 50-219 Licensee Event Report Reportable Occurrence No. 50-219/83-10/0lT This letter forwards three copies of a Licensee Event Report (LER) to report Reportable Occurrence No. 50-219/83-10/0lT in compliance with paragraph 6.9.2. A.9 of the Technical Specifications.
Very truly yours, A
(
Peter B. Fiedler Vice President and Director Oyster Creek l
l PBF:jal l
Enclosure s cc: Dire ctor (40 copies)
Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.
20555 Dire c tor (3)
Of fice of Management Information and Program Control U.S. Nuclear Regulatory Commission Was hington, D.C.
20555 NRC Resident Inspector Oyster Creek Nuclear Generating Station Forked River, NJ 08731 l
F304110280 830323 PDR ADOCK 05000219 l
S PDR l
GPU Nuclear is a part of the General Public Utikties System ggt
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OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No 50-219 /83-10/OlT Report Date March 23, 1983 Occurrence Date March 7, 1983 Identification of Occurrence Discovery of a design deficiency which resulted in not meeting a Limiting Condition for Operation as defined in the Technical Specifications, paragraph 3.5.B.
This event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.A.9.
Conditions Prior to Occurrence Mode Switch Refuel Thermal Power 0 MWt Generator Load 0 MWh 0
Reactor Coolant Temperature dL212 F Description of Occurrence On Monday, March 7,1983, the circuit breaker for System II of the Standby Gas Treatment System (SGTS) was " racked out" for system maintenance. Plant operations personnel later recognized a system design deficiency.
When the circuit breaker is " racked out", the control power transformer (connected to the primary side of the circult breaker) de-energizes. When control power is lost to the solenoid valves, air supply to the diaphragm operated inlet and outlet valves is vented of f.
Since these diaphragm valves
.are " air to close" and fail open on a loss of air, this results in the af fected system being lef t unisolated.
If one (1) SGTS is out of service, by " racking out" the circuit breaker, and the remaining system is initiated under an accident condition, some portion of the discharge from the operating system would recirculate through the out of service system as the SGTS trains are situated in parallel and share a common discharge duct.
Licensee Event Report Page 2 Reportable Occurrerce No. 50-219/83-10/0lT Apparent Cause of Occurrence The apparent cause of the occurrence is attributed to the removal of an exhaust fan circuit breaker which unexpectedly removed control power from the inlet and outlet solenoid valves, resulting in the diaphragm valves failing open.
This occurrence is attributed to a design deficiency.
Analysis of Occurrence The Standby Gas Treatment System is provided to filter Reactor Building atmosphere to the stack in the event of certain accident situations, in order to minimize the release of radioactive materials to the environment.
The SGTS consists of two parallel full-flow systems of filters and fans, capable of maintaining a negative building pressure (-0.25" H O) and retaining 2
radioactive iodines and particulates that may be present in the Reactor Building during and af ter an accident.
For the condition presented in this occurrence, recirculation could possibly reduce the operating system's ability to provide sufficient system flow and suf ficient negative pressure in the Reactor Building.
Corrective Action
Immediate corrective action was to place the System II exhaust fan breaker back in service, which closed the inlet and outlet valves, allowing System I to operate independently.
Additional corrective action will be to add precautions and limitations to SGTS related procedures which will maintain operability of the redundant system when one system is removed from service.
Caution tags will be placed on the control switches and circuit breakers to alert the operator of this problem.
The SGTS control circuitry will be reviewed to determine if an improved methodology of maintaining continuous control power to the solenoid valves is prac tical.
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| 05000219/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | Forwards LER 83-001/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | Forwards LER 83-002/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-002-03, /03L-0:on 830123,startup Banks Removed from Svc Due to Dilution Plant Main Breaker Cable Termination Failure.Cause Under Investigation.Dilution Pump Power Feed Terminations Replaced | /03L-0:on 830123,startup Banks Removed from Svc Due to Dilution Plant Main Breaker Cable Termination Failure.Cause Under Investigation.Dilution Pump Power Feed Terminations Replaced | | | 05000219/LER-1983-003-03, /03L-0:on 830118,during Maint of Control Rod Drive Pump A,Pump Vent Line Broke Off.Core Spray Pump Nzoia Wetdown & B Pump Inadvertently Tripped.Cause Not Stated. Pump Removed from Svc & Motor Tested | /03L-0:on 830118,during Maint of Control Rod Drive Pump A,Pump Vent Line Broke Off.Core Spray Pump Nzoia Wetdown & B Pump Inadvertently Tripped.Cause Not Stated. Pump Removed from Svc & Motor Tested | | | 05000219/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-004-03, /03L-0:on 830331,during Preventive Maint,Control Rod Drive Feed Pump NC08A Circuit Breaker Mechanically Closed Per Procedure.Investigation Revealed Breaker Should Not Have Closed.Caused by Binding Trip Shaft | /03L-0:on 830331,during Preventive Maint,Control Rod Drive Feed Pump NC08A Circuit Breaker Mechanically Closed Per Procedure.Investigation Revealed Breaker Should Not Have Closed.Caused by Binding Trip Shaft | | | 05000219/LER-1983-005-03, /03L-0:on 830126,while Performing Containment Spray Sys Automatic Actuation Test,High Drywell Pressure Switches IP15A,B & C Tripped at Value Greater than Tech Spec Limit.Cause Not Determined.Pressure Switches Readjusted | /03L-0:on 830126,while Performing Containment Spray Sys Automatic Actuation Test,High Drywell Pressure Switches IP15A,B & C Tripped at Value Greater than Tech Spec Limit.Cause Not Determined.Pressure Switches Readjusted | | | 05000219/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-006-03, /03L-0:on 830206,all Automatic Valves Not Lined Up Properly During Execution of Standby Gas Treatment Sys 10 H Operability Test.Caused by Condensation in Fan 1-9 Low Flow Sensing Lines.Lines Cleaned | /03L-0:on 830206,all Automatic Valves Not Lined Up Properly During Execution of Standby Gas Treatment Sys 10 H Operability Test.Caused by Condensation in Fan 1-9 Low Flow Sensing Lines.Lines Cleaned | | | 05000219/LER-1983-007-03, /03L-0:on 830418,during Monthly 10 H Operability Test of Standby Gas Treatment Sys Ii,High Differential Pressure Across Both HEPA Filters Observed.Caused by Plugging of Filters.Filters Replaced | /03L-0:on 830418,during Monthly 10 H Operability Test of Standby Gas Treatment Sys Ii,High Differential Pressure Across Both HEPA Filters Observed.Caused by Plugging of Filters.Filters Replaced | | | 05000219/LER-1983-008-03, /03L-0:on 830314,incorrect Undervoltage Trip Coil Installed on Core Spray Booster Pump Breaker,Preventing Manual Start.Caused by Personnel Error.Coil Replaced | /03L-0:on 830314,incorrect Undervoltage Trip Coil Installed on Core Spray Booster Pump Breaker,Preventing Manual Start.Caused by Personnel Error.Coil Replaced | | | 05000219/LER-1983-008, Forwards LER 83-008/03L-0.Detailed Event Analysis Encl | Forwards LER 83-008/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-009, Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | Forwards LER 83-009/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-010-01, /01T-0:on 830307,design Deficiency Discovered When Standby Gas Treatment Sys (SGTS) II Racked Out for Maint. SGTS II Inlet & Outlet Valves Opened,Allowing Recirculation During Sys I Operation.Procedures Revised | /01T-0:on 830307,design Deficiency Discovered When Standby Gas Treatment Sys (SGTS) II Racked Out for Maint. SGTS II Inlet & Outlet Valves Opened,Allowing Recirculation During Sys I Operation.Procedures Revised | | | 05000219/LER-1983-010, Forwards LER 83-010/01T-0.Detailed Event Analysis Encl | Forwards LER 83-010/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | Forwards LER 83-011/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-011-03, /03L-0:on 830306,during Standby Gas Treatment Sys 10 H Operability Test in Sys II Preferential Mode,All Automatic Valves Not Lined Up Properly.Caused by Melted Sensing Line for Fan 1-9 Low Flow Switch.Lines Repaired | /03L-0:on 830306,during Standby Gas Treatment Sys 10 H Operability Test in Sys II Preferential Mode,All Automatic Valves Not Lined Up Properly.Caused by Melted Sensing Line for Fan 1-9 Low Flow Switch.Lines Repaired | | | 05000219/LER-1983-012, Forwards LER 83-012/01T-0.Detailed Event Analysis Encl | Forwards LER 83-012/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-012-01, /01T-0:on 830319,door to Main Steam Line Trunnion Room Found Open During Refueling Checkoff.Caused by Design Deficiency,Personnel Error & Failure to Post Sign Identifying Door as Secondary Containment.Door Closed | /01T-0:on 830319,door to Main Steam Line Trunnion Room Found Open During Refueling Checkoff.Caused by Design Deficiency,Personnel Error & Failure to Post Sign Identifying Door as Secondary Containment.Door Closed | | | 05000219/LER-1983-013, Forwards LER 83-013/01T-0.Detailed Event Analysis Encl | Forwards LER 83-013/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-013-01, /01T-0:on 830327,both Doors of Reactor Bldg Personnel Access Airlock Opened Simultaneously.Caused by Personnel Error.Incident Reviewed W/Personnel & Appropriate Disciplinary Action Taken | /01T-0:on 830327,both Doors of Reactor Bldg Personnel Access Airlock Opened Simultaneously.Caused by Personnel Error.Incident Reviewed W/Personnel & Appropriate Disciplinary Action Taken | | | 05000219/LER-1983-014, Forwards LER 83-014/01T-0.Detailed Event Analysis Encl | Forwards LER 83-014/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1983-014-01, /01T-0:on 830406,design Deficiency Discovered in Heating Coil Control Circuitry for Standby Gas Treatment Sys Trains.Temporary Redundant Power Feed Provided Until Permanent Mod Installed During Current Maint Outage | /01T-0:on 830406,design Deficiency Discovered in Heating Coil Control Circuitry for Standby Gas Treatment Sys Trains.Temporary Redundant Power Feed Provided Until Permanent Mod Installed During Current Maint Outage | | | 05000219/LER-1983-015-03, /03L-0:on 830609,electricians Found Wire Wrapped Around Armature of Undervoltage Trip Device.Caused by Personnel Error in Installation of Wire Gag.Tripcoil,Blown Fuses & Static Time Delay Box Replaced | /03L-0:on 830609,electricians Found Wire Wrapped Around Armature of Undervoltage Trip Device.Caused by Personnel Error in Installation of Wire Gag.Tripcoil,Blown Fuses & Static Time Delay Box Replaced | | | 05000219/LER-1983-017-01, /01T-0:on 830826,arming Relay for Diesel Generator Protective Relay Set at Value Possibly Causing Breaker to Open During Fast Start.Caused by Design Deficiency.Setting Changed | /01T-0:on 830826,arming Relay for Diesel Generator Protective Relay Set at Value Possibly Causing Breaker to Open During Fast Start.Caused by Design Deficiency.Setting Changed | | | 05000219/LER-1983-018-03, /03L Submittal Delayed Due to Need for Plant Operations Review Committee Investigation Into Cause & Corrective Actions.Ro Will Be Submitted by 831108 | /03L Submittal Delayed Due to Need for Plant Operations Review Committee Investigation Into Cause & Corrective Actions.Ro Will Be Submitted by 831108 | | | 05000219/LER-1983-019-03, /03L-0:on 831114,during Surveillance of Standby Gas Treatment Sys,Reactor Bldg Ventilation Valve V-28-22 Failed to Close on Isolation Initiation Signal.Caused by Piece of Piston Breaking Off.Piston Repaired | /03L-0:on 831114,during Surveillance of Standby Gas Treatment Sys,Reactor Bldg Ventilation Valve V-28-22 Failed to Close on Isolation Initiation Signal.Caused by Piece of Piston Breaking Off.Piston Repaired | | | 05000219/LER-1983-020-03, /03L-0:on 830916,svc Water Pump 1-2 Breaker Failed to Trip When Undervoltage Device Deenergized.Caused by Component Failure Due to Burr on Latch Surface.Preventive Maint Done on Breaker & Burr removed.w/831019 Ltr | /03L-0:on 830916,svc Water Pump 1-2 Breaker Failed to Trip When Undervoltage Device Deenergized.Caused by Component Failure Due to Burr on Latch Surface.Preventive Maint Done on Breaker & Burr removed.w/831019 Ltr | | | 05000219/LER-1983-021-03, /03L-0:on 831012,loss of Main Bus 1A & Emergency Bus 1C Rendered One Standby Gas Treatment Sys Train Inoperable.Stack Gas Sampling Capability Lost for Approx 3 Had Pump a Shutdown Due to Loss of Power | /03L-0:on 831012,loss of Main Bus 1A & Emergency Bus 1C Rendered One Standby Gas Treatment Sys Train Inoperable.Stack Gas Sampling Capability Lost for Approx 3 Had Pump a Shutdown Due to Loss of Power | | | 05000219/LER-1983-025-03, /03L-0:on 831201,maint & Surveillance Procedures Identified as Not Adequately Verifying Excess Flow Check Valves Open Following Operations.Caused by Inadequate Maint & Surveillance Procedures.Procedures Revised | /03L-0:on 831201,maint & Surveillance Procedures Identified as Not Adequately Verifying Excess Flow Check Valves Open Following Operations.Caused by Inadequate Maint & Surveillance Procedures.Procedures Revised | |
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