LER-1982-045, Forwards LER 82-045/03L-0.Detailed Event Analysis Encl |
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GPU Nuclear h
gg gf P.O. Box 388 Forked River, New Jersey 08731 609-693-6000 Writer's Direct Dial Number:
November 11, 1982 Mr. Ronald C. Haynes, Administrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
Dear Mr. Haynes:
Subj ect: Oyster Creek Nuclear Generating Station Docket No. 50-219 Licensee Event Report Reportable Occurrence No. 50-219/82-45/03L This letter forwards three copies of a Licensee Event Report (LER) to report Reportable Occurrence No. 50-219/82-45/03L in compliance with paragraph 6.9.2.b.2 of the Technical Specifications. We recognize that the time limitation specified in the Technical Specifications, paragraph 6.9.2.b, for tne submittal of this LER, has been exceeded. The reason for the delay is as follows:
A deviation ruport is the administrative mechanism which initiates management review for corrective action and the determination of reportability of an event. Deviation Report No.82-201 was prepared for Emergency Service Water (ESW) pump 52A af ter it had failed an inservice test on September 9, 1982. The discharge pressure gauge on ESW pump 52A was checked and calibrated, the pump retested satisfactorily and was then declared operable. This was noted on the deviation report. Upon management review of the deviation report, it was determined that the event, which occorred on September 9,1982, was not reportable due to the fact that the gauge was calibra ted, the pump retested satisfactorily and was never removed f rom service, i.e., breakers and switches were not tagged out.
On the following day, September 10, 1982, the test was again performed on ESW pump 52A and it failed. The pump was subsequently declared inoperable, and was removed from service on September 11, 1982, to perform corrective ma i ntena nc e.
It appears that a deviation report was not written for the failure of the pump to pass the test on September 10, probably because the preparation of an additional report seemed redundant.
8211290575 821111 PDR ADOCK 05000219 S
PDR GPU Nuclear is a part of the General Pubhc Utihties System gW L
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1 Mr. Ronald C. Haynes Page 2 November 11, 1982 It was not until October 12, 1982, that it was realized that the event which occurred on September 10, constituted a reportable occurrence, when the Plant Operations Review Committee, during a review of the September Monthly Operating Report, noted the discrepancy. As a result, reportability of the event was not determined until a month af ter its occurrence.
Very truly yours, PeteF B. Tiedler Vice President and Director Oyster Creek PBF:PFC:Ise Enclosure s cc: Director (40 copies)
Of fice of Inspection and Enforcement U.S. Nuclear Regulatory Commission Was hington, D.C.
20555 Director (3 copies)
Of fice of Management Information and Program Control U.S. Nuclear Regulatory Commission Washington, D.C.
20555 NRC Resident Inspector Oyster Creek Nuclear Generating Station Forked River, NJ 08731
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OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/82-45/03L Report Date November 11, 1982 Occurrence Date September 10, 1982 Identification of Occurrence It was discovered on October 12, 1982, that Emergency Service Water pump 52A had been declared inoperable on September 10, 1982, and subsequently removed from service for maintenance on September 11, 1982. This constitutes operation in a degraded mode, permitted by a limiting condition for operation, as specified in the Technical Specifications, paragraph 3.4.C.4.
This event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b.2.
Conditions Prior to Occurrence The plant was operating at steady state power.
Major Plant Parameters:
Reactor Power - 1280 MWt Generator Load -
414 MWe Description of Occurrence During performance of the Containment Spray and Emergency Service Water (ESW) inservice test on September 9,1982, ESW pump 52A was found to have a discharge pressure below the acceptable limit. The pump was declared inoperable and the redundant ESW pump (52B) tested satisfactorily.
The discharge pressure gauge for ESW pump 52A was checked and calibrated, and the pump was retested. During the retest, discharge pressure was above the acceptable limit, and ESW pump 52A was declared operable.
On September 10, 1982, the test on ESW pump 52A was performed again at the request of operations management. The pump discharge pressure was again below the acceptable limit, and the pump was subsequently declared inoperable. The following day, ESW pimp 52A was removed from service and rendered inoperable in order to perform maintecance. The pump suction was cleaned and impeller j
clearance was adjusted. The pump was retested and was returned to service on l
September 13, 1982. During this time, the redundant ESW pump (52B) was demonstrated operable on a daily basis as required by the Technical S pecifications.
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Licensee Event Report Page 2 Reportable Occurrence No. 50-219/82-45/03L Apparent Cause of Occurrence The cause of the occurrence was attributed to improper impeller clearance adjustment af ter previous maintenance work on the pump. The procedure steps for impeller clearance adjustments were ambiguous.
Analysis of Occurrence The Containment Spray and Emergency Service Water Systems are engineered safety systems designed to remove fission product decay heat from the primary containment in the event of a loss of coolant accident. There are two independent systems used to accomplish this, with each system having redundant pumps, each capable of performing the safety function. The systems are designed so that a single containment spray pump and a single emergency service water pump can provide the necessary cooling.
In this case, the safety significarce is minimal, due to the fact that the redundant ESW pump in the system (52B) was operable. Based on this, the system would have performed its design function in the event of a LOCA.
Corrective Action
As required by the Technical Specifications, the redundant pump was demonstrated to be operable on a daily basis. The pump suction on ESW pump 52A was cleaned, the impeller clearance was adjusted, and the pump was tested satisfactorily and returned to service. In addition, the remaining three (3)
ESW pumps will have their impeller clearances checked and adjusted, if required. Procedure 708.1.002 was revised to more clearly detail how to adjust impeller clearance.
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| 05000219/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | Forwards LER 82-001/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-001-03, /03L-0:on 820128,during Testing,Containment Spray High Drywell Pressure Indicating Switches IP15A,IP15B & IP15C Found to Trip at Values Greater than Tech Spec Limits. Caused by Instrument Repeatability.Switches Reset | /03L-0:on 820128,during Testing,Containment Spray High Drywell Pressure Indicating Switches IP15A,IP15B & IP15C Found to Trip at Values Greater than Tech Spec Limits. Caused by Instrument Repeatability.Switches Reset | | | 05000219/LER-1982-002-03, /03L-0:on 820118,installation of Mod Could Have Led to Possible Failure to Maintain Primary Containment Integrity.Change Defeated Automatic Withdrawal Function 3 & 4 TIP Detectors.Caused by Inadequate Safety Review | /03L-0:on 820118,installation of Mod Could Have Led to Possible Failure to Maintain Primary Containment Integrity.Change Defeated Automatic Withdrawal Function 3 & 4 TIP Detectors.Caused by Inadequate Safety Review | | | 05000219/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | Forwards LER 82-002/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-003-03, /03L-0:on 820122,containment Spray High Drywell Pressure Indicating Switch IP25B Found to Trip at Value Greater than Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset | /03L-0:on 820122,containment Spray High Drywell Pressure Indicating Switch IP25B Found to Trip at Value Greater than Tech Spec Limits.Caused by Instrument Repeatability.Switch Reset | | | 05000219/LER-1982-004, Forwards LER 82-004/03L-0.Detailed Event Analysis Encl | Forwards LER 82-004/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-004-03, /03L-0:on 820121,reactor Bldg Closed Cooling Water Drywell Isolation Valve V-5-167 Failed to Fully Close.Caused by Lack of Stem/Stem Nut Lubrication &/Or Packing Problem. Stem,Stem Nut & Bearing Lubricated & Valve Repacked | /03L-0:on 820121,reactor Bldg Closed Cooling Water Drywell Isolation Valve V-5-167 Failed to Fully Close.Caused by Lack of Stem/Stem Nut Lubrication &/Or Packing Problem. Stem,Stem Nut & Bearing Lubricated & Valve Repacked | | | 05000219/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-005-03, /03L-0:on 820125,during Load Surveillance Test, Diesel Generator 1-1 Tripped on Engine Fault.Caused by Reduction of Water Inventory in Cooling Sys as Result of Radiator Tube Leak.Leaky Tubes Plugged | /03L-0:on 820125,during Load Surveillance Test, Diesel Generator 1-1 Tripped on Engine Fault.Caused by Reduction of Water Inventory in Cooling Sys as Result of Radiator Tube Leak.Leaky Tubes Plugged | | | 05000219/LER-1982-006, Forwards LER 82-006/01T-0.Detailed Event Analysis Encl | Forwards LER 82-006/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-006-01, /01T-0:on 811203,one Trip Sys in Automatic Depressurization Sys Rendered Inoperable by Removal of Dc Control Power Fuses.Caused by Nonrating of Microswitches Inside IA83-A Replacement.All EMRV Switches Replaced | /01T-0:on 811203,one Trip Sys in Automatic Depressurization Sys Rendered Inoperable by Removal of Dc Control Power Fuses.Caused by Nonrating of Microswitches Inside IA83-A Replacement.All EMRV Switches Replaced | | | 05000219/LER-1982-007-03, /03L-0:on 820126,main Steam Line High Flow Sensor RE-22H Tripped at Greater Value than Given in Tech Specs. Caused by Instrument Repeatability & Drift.Sensor Reset & Setpoints Lowered | /03L-0:on 820126,main Steam Line High Flow Sensor RE-22H Tripped at Greater Value than Given in Tech Specs. Caused by Instrument Repeatability & Drift.Sensor Reset & Setpoints Lowered | | | 05000219/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Encl | Forwards LER 82-007/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-008-03, /03L-0:on 820210,monthly Channel Check of Secondary (Thermocouples) Safety & Relief Valve Position Monitoring Sys Not Performed as Required by Tech Spec. Caused by Lack of Administrative & Procedural Controls | /03L-0:on 820210,monthly Channel Check of Secondary (Thermocouples) Safety & Relief Valve Position Monitoring Sys Not Performed as Required by Tech Spec. Caused by Lack of Administrative & Procedural Controls | | | 05000219/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-009-03, /03L-0:on 820210,overload Trip Occurred on Standby Gas Treatment Sys Exhaust Fan 1-8.Apparently Caused by Change in Breaker Trip Setpoint.Further Testing Underway | /03L-0:on 820210,overload Trip Occurred on Standby Gas Treatment Sys Exhaust Fan 1-8.Apparently Caused by Change in Breaker Trip Setpoint.Further Testing Underway | | | 05000219/LER-1982-010, Forwards LER 82-010/01T-0.Detailed Event Analysis Encl | Forwards LER 82-010/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-010-01, /01T-0:on 820218,deluge Sys for Reactor Bldg Elevation 51 Ft Actuated Due to Smoke from Overheated Bearing in Cleanup Sys Auxiliary Pump Motor.Caused by Inadequate Electrical Sealing Techniques | /01T-0:on 820218,deluge Sys for Reactor Bldg Elevation 51 Ft Actuated Due to Smoke from Overheated Bearing in Cleanup Sys Auxiliary Pump Motor.Caused by Inadequate Electrical Sealing Techniques | | | 05000219/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-011-03, /03L-0:on 820208,three Hydraulic Snubbers Were Inoperable & Accelerated Surveillance of Tech Spec 4.5.0.3 Was Not Performed.Caused by Component Failure.Snubbers Replaced W/Certified Operable Snubbers | /03L-0:on 820208,three Hydraulic Snubbers Were Inoperable & Accelerated Surveillance of Tech Spec 4.5.0.3 Was Not Performed.Caused by Component Failure.Snubbers Replaced W/Certified Operable Snubbers | | | 05000219/LER-1982-012, Forwards LER 82-012/01P-0.Detailed Event Analysis Encl | Forwards LER 82-012/01P-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-012-01, /01P-0:on 820226,air Operated Vacuum Breaker V-26-18 Exceeded Allowable Leak Rate.Caused by Improper Alignment of Valve Shaft & Operator Due to Inadequate Maint Instructions.Valve Realigned & Procedures Will Be Revised | /01P-0:on 820226,air Operated Vacuum Breaker V-26-18 Exceeded Allowable Leak Rate.Caused by Improper Alignment of Valve Shaft & Operator Due to Inadequate Maint Instructions.Valve Realigned & Procedures Will Be Revised | | | 05000219/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-013-03, /03L-0:on 820128,low Voltage Annunciator Relay Setting for Main Station Batteries B & C & Diesel Generator 2 Battery Relay & Setting Found Below Tech Specs Limit. Caused by Annunciation Setpoints Out of Spec | /03L-0:on 820128,low Voltage Annunciator Relay Setting for Main Station Batteries B & C & Diesel Generator 2 Battery Relay & Setting Found Below Tech Specs Limit. Caused by Annunciation Setpoints Out of Spec | | | 05000219/LER-1982-014-01, /01T-0:on 820410,local Leak Rate Testing Found That Five Containment Isolation Valves & One Gasket Did Not Meet 11.9 Scfh Acceptance Criteria.Caused by 1-8 Sump Discharge Seats Degrading.Valves Repaired & Gasket Replaced | /01T-0:on 820410,local Leak Rate Testing Found That Five Containment Isolation Valves & One Gasket Did Not Meet 11.9 Scfh Acceptance Criteria.Caused by 1-8 Sump Discharge Seats Degrading.Valves Repaired & Gasket Replaced | | | 05000219/LER-1982-015-03, /03L-0:on 820315,during Offgas Holdup Valve Isolation Test,Timer RN28 Timed Out 28-s in Excess of Tech Spec Limit.Caused by Instrument Drift.Timer Reset. Surveillance Test Will Be Performed Prior to Every Startup | /03L-0:on 820315,during Offgas Holdup Valve Isolation Test,Timer RN28 Timed Out 28-s in Excess of Tech Spec Limit.Caused by Instrument Drift.Timer Reset. Surveillance Test Will Be Performed Prior to Every Startup | | | 05000219/LER-1982-015, Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | Forwards LER 82-015/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-016, Forwards LER 82-016/03L-0.Detailed Event Analysis Encl | Forwards LER 82-016/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-016-03, /03L-0:on 820611,during Transfer of Spent Resin, Svc Air Piping Became Cross Contaminated W/Water,Resulting in Three Leaks to Environ.Caused by Blocked Vent Lines on Tank.Affected Sys Isolated | /03L-0:on 820611,during Transfer of Spent Resin, Svc Air Piping Became Cross Contaminated W/Water,Resulting in Three Leaks to Environ.Caused by Blocked Vent Lines on Tank.Affected Sys Isolated | | | 05000219/LER-1982-017-03, /03L-0:on 820325,normal Auxiliary Power Bus 1C Relay Failed Totally & Svc Water Pump Trip Time Delay Relay SK8A Failed to Operate within Tech Spec Limits.Power Bus Failure Caused by Normal End of Life | /03L-0:on 820325,normal Auxiliary Power Bus 1C Relay Failed Totally & Svc Water Pump Trip Time Delay Relay SK8A Failed to Operate within Tech Spec Limits.Power Bus Failure Caused by Normal End of Life | | | 05000219/LER-1982-017, Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | Forwards LER 82-017/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-018-03, /03L-0:on 820527,main Steam Line Drain Valve V-1-106 Operated & Failed to Close Fully.Caused by High Torque Trip.Repair or Replacement of Valve Will Be Accomplished During Next Shutdown | /03L-0:on 820527,main Steam Line Drain Valve V-1-106 Operated & Failed to Close Fully.Caused by High Torque Trip.Repair or Replacement of Valve Will Be Accomplished During Next Shutdown | | | 05000219/LER-1982-018, Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | Forwards LER 82-018/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-019-01, /01T-0:on 820331,local Leak Rate Test for Valves V-1-106 & V-1-111 Found Leakage Exceeding Tech Spec Limit. Caused by Deterioration of Valve Internals.Valves Repaired | /01T-0:on 820331,local Leak Rate Test for Valves V-1-106 & V-1-111 Found Leakage Exceeding Tech Spec Limit. Caused by Deterioration of Valve Internals.Valves Repaired | | | 05000219/LER-1982-019, Forwards LER 82-019-/01T-0.Detailed Event Analysis Encl | Forwards LER 82-019-/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-020, Forwards LER 82-020/01T-0.Detailed Event Analysis Encl | Forwards LER 82-020/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-020-01, /01T-0:on 820328,MSIV Leak Rate Testing Disclosed Deterioration of Valve Internals on NS03-A & Packing Leak on Outboard Valve NS04-A.Caused Not stated.NS03-A Disassembled & repaired.NS04-A Repacked | /01T-0:on 820328,MSIV Leak Rate Testing Disclosed Deterioration of Valve Internals on NS03-A & Packing Leak on Outboard Valve NS04-A.Caused Not stated.NS03-A Disassembled & repaired.NS04-A Repacked | | | 05000219/LER-1982-021, Forwards LER 82-021/01T-0.Detailed Event Analysis Encl | Forwards LER 82-021/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-021-01, /01P:on 820416,primary Containment Atmosphere Not Reduced to Less than 5% Oxygen within 24-h After Reactor Mode Selector Switch Placed in Run Position.Caused by Insufficient Nitrogen & Blown Rupture Disc | /01P:on 820416,primary Containment Atmosphere Not Reduced to Less than 5% Oxygen within 24-h After Reactor Mode Selector Switch Placed in Run Position.Caused by Insufficient Nitrogen & Blown Rupture Disc | | | 05000219/LER-1982-022, Forwards LER 82-022/03L-0.Detailed Event Analysis Encl | Forwards LER 82-022/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-022-03, /03L-0:on 820416,after 1B Breaker Closed & Startup Transformer S1B Breaker Failed to Operate,Operator Determined That Fuse Had Blown.Caused by Mild Momentary Overload.Fuse Replaced & Breaker Reset & Returned to Svc | /03L-0:on 820416,after 1B Breaker Closed & Startup Transformer S1B Breaker Failed to Operate,Operator Determined That Fuse Had Blown.Caused by Mild Momentary Overload.Fuse Replaced & Breaker Reset & Returned to Svc | | | 05000219/LER-1982-023-03, /03L-0:on 820418,during Normal Operation,Control Rod Drive Pump a Failed,Resulting in Operation in Degraded Mode.Cause Undetermined.Rotating Assembly Replaced | /03L-0:on 820418,during Normal Operation,Control Rod Drive Pump a Failed,Resulting in Operation in Degraded Mode.Cause Undetermined.Rotating Assembly Replaced | | | 05000219/LER-1982-023, Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | Forwards LER 82-023/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-024-03, /03L-0:on 820414,while Performing Surveillance on Electromatic Relief Valve Pressure Switches,Three of Five Switches Tripped Below Tech Spec Limit.Caused by Instrument Repeatability & Drift.Instruments Reset | /03L-0:on 820414,while Performing Surveillance on Electromatic Relief Valve Pressure Switches,Three of Five Switches Tripped Below Tech Spec Limit.Caused by Instrument Repeatability & Drift.Instruments Reset | | | 05000219/LER-1982-024, Forwards LER 82-024/03L-0.Detailed Event Analysis Encl | Forwards LER 82-024/03L-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-025, Forwards LER 82-025/01T-0.Detailed Event Analysis Encl | Forwards LER 82-025/01T-0.Detailed Event Analysis Encl | | | 05000219/LER-1982-026-03, /03L-0:on 820507,thermocouple for Safety Valve NR28J Found Open During Surveillance Testing.Caused by Broken Lead Wire at Thermocouple.One of Adjacent Valve Acoustic Monitor Setpoints Reduced.Thermocouple Replaced | /03L-0:on 820507,thermocouple for Safety Valve NR28J Found Open During Surveillance Testing.Caused by Broken Lead Wire at Thermocouple.One of Adjacent Valve Acoustic Monitor Setpoints Reduced.Thermocouple Replaced | | | 05000219/LER-1982-027-03, /03L-0:on 820512,during Routine Visual Insp,Oil Puddle Discovered Below Liquid Poison Pump B.Caused by Plugged Stuffing Box 1-inch Drain.Pump Tagged Out,Oil Changed & Drain Cleared | /03L-0:on 820512,during Routine Visual Insp,Oil Puddle Discovered Below Liquid Poison Pump B.Caused by Plugged Stuffing Box 1-inch Drain.Pump Tagged Out,Oil Changed & Drain Cleared | | | 05000219/LER-1982-027, Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | Forwards LER 82-027/03L-0.Detailed Event Analysis Encl | |
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