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 Start dateReport dateSiteReporting criterionSystemEvent description
05000334/LER-2015-00115 April 201511 June 2015Beaver Valley10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Feedwater
Reactor Protection System
Auxiliary Feedwater
Control Rod

At 0411 EDT on April 15, 2015 the Beaver Valley Power Station (BVPS) Unit 1 reactor was manually tripped from approximately 85 percent power following a condensate pump trip. Prior to the manual reactor trip the unit was performing an emergent power reduction after the identification of a degrading condition on the "A" condensate pump motor. All control rods fully inserted into the core. The auxiliary feedwater system actuated as designed.

The unit was stabilized in Mode 3 with the normal main feedwater system in service and the auxiliary feedwater system properly secured.

The "A" condensate pump trip was caused by the failure of the inboard motor bearing due to lack of oil lubrication.

The root cause evaluation determined that responses to technical questions were provided without the appropriate technical rigor or validation of assumptions regarding acceptable oil level for the pump motor.

This event was reported (EN 50985) as an event or condition that results in the actuation of the reactor protection system when the reactor is critical, 10 CFR 50.72(b)(2)(iv)(B) and specified system actuation, 10 CFR 50.72(b)(2)(iv)(A). This event is reportable pursuant to 10 CFR 50.73(a)(2)(iv)(A) as a condition that resulted in the manual actuation of the Reactor Protection System, 10 CFR 50.73(a)(2)(iv)(B)(1), and the automatic actuation of the Auxiliary Feedwater System 10 CFR 50.73(a)(2)(iv)(B)(6).

05000412/LER-2014-00220 May 201421 July 2014Beaver Valley10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Reactor Coolant System
Feedwater
Reactor Protection System
Main Steam Isolation Valve
Auxiliary Feedwater
Main Steam Line
Control Rod

On May 20, 2014, at 0835 hours during a plant startup following the seventeenth refueling outage, Beaver Valley Power Station (BVPS) Unit 2 operations personnel manually tripped the reactor when it was recognized that the pre-determined trip criteria of 85 percent narrow range water level in the 'A' Steam Generator would be met. This manual trip criterion was reached after the steam generator water level began to oscillate following the start of the second condensate pump. Due to low decay heat input the main steam line isolation valves were shut in order to limit reactor coolant system cool down. Plant trip response was as expected without complications, and all control rods fully inserted in the core.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv)(A) as a condition that resulted in the valid manual or automatic actuation of any of the systems listed in (a)(2)(iv)(B) - (1) Reactor Protection System (RPS) and (2) Multiple Main Steam Isolation Valves (MSIVs). A 10 CFR 50.72 notification was made at 1052 hours on May 20, 2014, to report the manual reactor trip and main steam line isolation (EN# 50124).

The cause of this event has been determined to be the lack of an integrated secondary startup procedure.

Station operating procedures will be revised to prevent recurrence.

05000334/LER-2014-0026 January 20147 March 2014Beaver Valley10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Auxiliary Feedwater
Main Transformer
Main Steam Line

On January 6, 2014, the Beaver Valley Power Station (BVPS) Unit 1 tripped from full power due to a main transformer differential protection main unit generator trip as a result of a main unit transformer failure. All three Auxiliary Feedwater (AFW) pumps automatically started, as expected, due to lowering steam generator levels. The Turbine Driven Auxiliary Feedwater (TDAFW) pump ran for 1 hour and 49 minutes at which time the pump tripped due to governor oscillations. The TDAFW pump was declared inoperable. Subsequent investigation determined that the governor oscillations were due to a misadjusted governor needle valve that was last set during refueling outage 1R22 in October, 2013. Therefore the pump was inoperable from the time Mode 3 was entered on November 1, 2013 at 1006 hours. Technical Specifications (TS) require three trains of AFW to be operable in Modes 1 through 3. Entry into Mode 3 and operation with an inoperable pump, for longer than permitted by the TS, constitute conditions prohibited by TS. During this time each of the Motor Driven AFW pumps were rendered inoperable, separately, for maintenance and/or testing. This constitutes a condition that could have prevented the fulfillment of a Safety Function. The governor has been properly adjusted and the appropriate procedures will be revised.

This event is being reported under 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications and under 10 CFR 50.73(a)(2)(v)(B) as a condition that could have prevented the fulfillment of a Safety Function - Remove Residual Heat.

05000338/LER-2013-00321 November 201316 January 2014North Anna10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On November 21, 2013, at 2006 hours with Units 1 and 2 operating at 100 percent power (Mode 1), Engineering personnel determined that the Casing Cooling tank low level setpoint does not account for vortexing. During a review of the Channel Statistical Allowance (CSA), it was identified that the final Casing Cooling tank level would be below the top of the pump suction nozzle when accounting for the full CSA on the low level bistable and closure time for tank isolation motor operated valves. This condition could have allowed air entrainment and caused a reduction in Recirculation Spray system flow during a Containment Depressurization Actuation.

As a result, the Outside Recirculation Spray (ORS) pumps for both units were declared inoperable and Technical Specification (TS) 3.0.3 was entered for each unit. A prompt report was made to the NRC and an Operability Determination was completed with actions to isolate the Casing Cooling tank on a low level at less than or equal to 10% versus the current setpoint of 4%. This change restored operability of the ORS pumps and TS 3.0.3 was exited at 2217 hours, prior to ramping the units. This event is reportable pursuant to 10CFR50.73(a)(2)(v)(D) for a condition that could have prevented the fulfillment of a safety function. The health and safety of the public were not affected by this event.

05000395/LER-2013-00516 October 201311 December 2013Summer10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

As a result of recent industry operating experience (OE 305419, EN 49411, EN 49419) regarding the impact of unfused Direct Current (DC) ammeter circuits in the Control Room, Virgil C. Summer Nuclear Station (VCSNS) performed a review of ammeter circuitry. On October 16, 2013, the review determined the described condition to be applicable to VCSNS resulting in an unanalyzed condition with respect to 10CFR50 Appendix R analysis requirements.

The wiring design for the ammeters contains a shunt in the current flow from each DC battery or charger. The ammeter wiring attached to the shunt does not contain fuses. It is postulated that a fire could cause one of the ammeter wires to hot short to ground. Concurrently, the fire could cause another DC wire from the opposite polarity on the same battery or the same battery charger to also short to ground. This would cause a ground loop through the unfused ammeter cable. The potential exists that the cable could heat up causing a secondary fire in the ammeter raceway. The secondary fire could adversely affect safe shutdown equipment and potentially cause the loss of the ability to safely shutdown per 10CFR50 Appendix R.

The apparent cause of this event is double short to ground faults of opposite polarity were not considered during the design process of the Battery System. A corrective action has been added to the National Fire Protection Association (NFPA) 805 implementation to provide a permanent solution to address this unanalyzed Appendix R condition. As an interim action, roving fire watches have been established for the affected areas.

05000338/LER-2013-00211 October 20136 December 2013North Anna10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Reactor Coolant System
Reactor Protection System
Auxiliary Feedwater
Main Transformer
Main Condenser
Control Rod
Main Steam

On October 11, 2013, at 1319 hours with Unit 1 operating at 48 percent power (Mode 1), an automatic turbine trip and subsequent reactor trip occurred due to a lockout relay actuation for the 1C Station Service Transformer (1-EP-SST-1C). The lockout occurred simultaneously with the start of the 1C Condensate Pump (1-CN-P-1C). The direct cause of the 1-EP-SST-1C lockout is that current transformer terminal block shorting screws were left installed inside the 1- EP-BKR-15C2 breaker cubicle. The root cause of the event was less than adequate written instructions for documenting the installation and removal of the terminal block shorting screws.

All safety system responded as expected. The Auxiliary Feedwater Pumps actuated as designed following the reactor trip and provided makeup flow to the Steam Generators. 1-EP- SST-1C was inspected and no signs of damage or abnormal conditions were observed. At 1507 hours, a 4 hour report was made to the NRC in accordance with 10CFR50.72(b)(2)(iv)(B) for a Reactor Protection System (RPS) actuation and a 8 hour report in accordance with 10CFR50.72(b)(3)(iv)(A) for a Auxiliary Feedwater system actuation. The event is reportable pursuant to 10CFR50.73(a)(2)(iv)(A) for a condition that resulted in the automatic actuation of the RPS and AFW Systems. The health and safety of the public were not affected by the event.

05000334/LER-2013-0024 October 201314 February 2014Beaver Valley10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator

During the Beaver Valley Power Station (BVPS) Unit 1 1R22 Refueling Outage, a through wall defect was discovered during a planned visual examination of the Reactor Containment Building (RCB) steel liner. The BVPS Unit 1 containment design consists of an internal steel liner that is surrounded by reinforced concrete.

Investigation and laboratory analysis determined that there were indications of two through wall penetrations with a possible third penetration slightly off-set from the second. The total combined area of the three penetrations was calculated to be 0.395 square inches. A visual inspection of 100 percent of the accessible liner area was completed. No additional significant indications of corrosion were identified. Prior to startup from 1R22, the RCB steel liner was repaired and tested satisfactory.

The direct cause of this event was determined to be pitting type corrosion, originating from foreign material introduced during the original construction of the containment wall.

An evaluation determined that there is reasonable assurance that the containment was operable during the period of time that the plant was operated with the small areas of through wall corrosion on the steel liner.

Therefore, there was no loss of safety function and the safety significance is considered to be very low. This event is being reported under 10 CFR 50.73(a)(3)(ii)(A) as a condition resulting in a principal safety barrier being degraded.

05000334/LER-2013-00130 September 201327 November 2013Beaver Valley10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(iv), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Feedwater
Service water
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal

At approximately 0228 hours on September 30, 2013, during a planned shutdown of Beaver Valley Power Station (BVPS) Unit 1 for a refueling outage, the "B" motor driven Auxiliary Feedwater (AFW) pump was manually started, while in Mode 3, due to lowering levels in the steam generators.

The condensate pump recirculation flow control valve opened to approximately 40 percent, which resulted in a reduction of the condensate flow to the steam generators and a decrease in the steam generator levels.

The operators recognized that adequate feedwater flow was not available using the normal flow path of the condensate pump through the bypass feedwater regulating valves to the steam generators. In response to the lowering steam generator levels, the operators manually started the "B" motor driven AFW pump to restore the steam generator water levels. Following the start of the AFW pump, the steam generator levels were returned to their normal operating control band. The apparent cause of this event was that the condensate flow control valve opened when it was not intended due to the associated flow controller being out of calibration. The controller was repaired and functionally checked during the refueling outage.

This event is being reported under 10 CFR 50.73(a)(2)(iv) as a condition that resulted in the valid manual start of a system listed in (a)(2)(iv)(B)(6) - Auxiliary Feedwater. The safety significance associated with the manual start of the AFW pump is considered to be very low.

05000323/LER-2013-00510 July 201321 November 2013Diablo Canyon10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Reactor Coolant System
Reactor Protection System
Auxiliary Feedwater

On July 10, 2013, at 09:50 PDT, while performing the periodic hot-washing of the 500 kV insulators, a flashover of the Phase A 500 kV to ground across the Phase A lightning arrestor occurred and actuated the 500 kV differential relay. The actuation of the 500 kV differential relay opened the Unit 2 generator output breakers to isolate the generator, which then actuated a turbine trip. Since Unit 2 was operating above the 50 percent power permissive, the reactor protection system initiated a Unit 2 reactor trip. All plant equipment responded as designed.

Diablo Canyon Power Plant (DCPP) staff determined the root cause of this event to be the hot-washing of the Phase A transmission line string insulators (500 kV dead-end insulators) with inadequate controls for oversight of supplemental PG&E transmission line personnel and on-line maintenance risk analysis that resulted in a conductive overspray, which induced an external arc around the lightning arrester insulation resulting in flashover. The corrective action to prevent reoccurrence involves the development and implementation of a maintenance strategy for 500 kV dead-end insulators to ensure they remain adequately contamination free, structurally sound, and minimize risk to DCPP.

There were no personnel injuries, no offsite radiological releases, and no damage to safety-related equipment associated with this condition. This condition did not have an adverse effect on the health and safety of the public.

05000339/LER-2013-0034 July 201330 August 2013North Anna10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

annunciator, 2G-B5 "Station Service Busses 2A-2B-2C UV Relay Trouble" alarmed and locked in. Troubleshooting indicated that the under voltage (UV) relay monitoring B-C phase for Station Service Bus 2A had actuated. The 2A UV channel was placed into trip on July 3, 2013, per Technical Specification 3.3.1 Condition L, but the 2A under frequency (UF) channel was not placed into trip. On July 3, 2013, a multidiscipline team, including the vendor, determined that the UF relay would remain operable with the degraded voltage. An Operability Determination was developed and approved to document the conclusion. However, on July 10, 2013, it was revealed through additional testing that the operability determination contained inaccurate information and the 2A UF relay would not operate within the required time frame. The 2A UF relay channel was subsequently placed in trip on July 10, 2013. A potential transformer blown fuse was replaced and the UV and UF channels were restored to operable on July 22, 2013.

This event is reportable pursuant to 10CFR50.73(a)(2)(i)(B) for a condition prohibited by Technical Specifications (TS) when the inoperable UF channel was not placed into trip within the time limits of TS. The health and safety of the public were not affected by the event.

05000395/LER-2013-00325 June 201321 August 2013Summer10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Control Room Emergency Filtration System

On June 25, 2013 with the plant in Mode 1, the "A" Chiller (XHX0001A) shut down during a fast bus transfer of its 7.2 kV bus power supply due to the tripping of two molded case circuit breakers (MCCBs) located on the "A" Chiller skid. The "A" Chiller was running prior to a planned fast transfer of its 7.2 kV bus power supply from the normal power source (115kV) to the alternate source (230kV). Troubleshooting found both compressor motor MCCBs in the tripped condition.

The instantaneous trip calibration of the MCCBs was designed to trip the breakers with an incoming current greater than the nominal value of 2000A, and a current greater than this magnitude was experienced during this event. Trips of the MCCBs require local operator action to restart the chiller. A subsequent restart attempt resulted in both compressor motors not starting. The "A" Chiller has peen considered to be inoperable since being placed into service August 5, 2011 due to the inability of the chiller to respond to Engineered Safety Features (ESF) sequencer demand following a grid perturbation similar to the bus voltage transient that occurred with a "fast transfer" scenario. The Chilled Water System is an attendant cooling water system that supports the Control Room Emergency Filtration System (CREFS). VCSNS Technical Specifications (TS) 3.7.6 requires two trains of CREFS to be operable while in Mode one through four.

The MCCBs on the Chiller skid have been adjusted to trip at higher amperage. The instantaneous trip setting for the MCCBs has been changed from 2000A to an instantaneous trip range of 3063A to 3938A.

El

05000412/LER-2013-00124 June 201323 August 2013Beaver Valley10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Emergency Core Cooling System

On 6/24/2013, Beaver Valley Power Station (BVPS) Unit No. 2 was at 100 percent power. At 0836 hours, the Control Room was notified of a void in the suction piping of the "A" train High Head Safety Injection (HHSI) pump. During a routine performance of a void monitoring procedure, a void of approximately 0.62 cubic feet was discovered at the suction of the "C" HHSI pump which was aligned to the "A" train. The pump was declared inoperable and Technical Specification (TS) LCO 3.5.2, ECCS Operating, was entered. The "B" HHSI pump, aligned to the "B" train, was operable and in service. The "A" HHSI pump was inoperable, due to planned maintenance.. Following venting and verification that the suction piping of the "C" HHSI pump was sufficiently full of water, the "A" train of HHSI was declared operable and TS LCO 3.5.2 was exited at 1623 hours on 6/24/2013. It was subsequently determined that the gas void had existed prior to the "C" pump being credited as the stand-by HHSI pump on the "A" train eight days previously. The "C" HHSI pump was inoperable during the eight day time frame. TS LCO 3.5.2, ECCS Operating, requires two trains of ECCS to be operable. As this condition existed for greater than the allowed restoration and shut down completion times of this LCO, a condition prohibited by technical specifications had existed. At no time during this event were both trains of ECCS inoperable simultaneously.

The void source was determined to be from an inadequate fill and vent of the reactor coolant pumps seal return line.

The root cause of this event is the minimum flow required to move entrained air through the seal water return piping was not present. The procedure used to fill and vent the seal return lines did not ensure a minimum flow was obtained that would move the entrained air to the vent location. The plant risk associated with this event was evaluated to be very low.

05000382/LER-2013-00522 May 20137 November 2013Waterford10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Emergency Diesel Generator
HVAC

Waterford 3 declared Emergency Diesel Generator B (EDG-B) inoperable on May 22, 2013 due to inability to maintain room temperature within design limits. Subsequent trouble shooting revealed that the variable pitch room exhaust fan had failed due to separation of the fan hub from the hub sleeve. Examination of recent operating data showed that the first evidence of fan failure had been during a surveillance test the previous month. An apparent cause evaluation determined the probable cause of the failure to be the result of repairs made during a previous (1999) fan motor replacement. These repairs caused additional stresses on the fan hub components which eventually resulted in fan hub separation from the hub sleeve. The EDG-B room exhaust fan was repaired and EDG-B operability was restored on May 26, 2013. Safety significance for the event is characterized as low to moderate. This condition is reportable under the following criteria:

10 CFR 50.73(a)(2)(i)(B), 10 CFR 50.73(a)(2)(ii)(B), and 10 CFR 50.73(a)(2)(v)(D).

05000339/LER-2013-00110 May 20132 July 2013North Anna Power Station Unit 210 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Reactor Protection System
Auxiliary Feedwater
Permanent Magnet Generator
Main Condenser
Control Rod
On May 10, 2013, at 0612 hours with Unit 2 in Mode 1, 60 percent power following a refueling outage, a manual reactor trip was initiated as a result of increased vibrations on the number 9 main turbine/generator bearing and a report of a luminous discharge in the main generator exciter enclosure. All systems responded as expected following the manual trip. The auxiliary feedwater (AFW) pumps received an automatic start signal due to the resulting low-low level in "C" Steam Generator (SG). The AFW System operated as designed with no abnormalities noted and was subsequently returned to automatic operation. The SG levels were restored to normal operating level. When resetting AMSAC, a second AFW system automatic start occurred due to a procedure sequence error and was determined to be an invalid signal. At 0820 hours, a 4 hour report was made in accordance with 10CFR50.72(b)(2)(iv)(B) for Reactor Protection System (RPS) actuation and 8 hour report in accordance with 10CFR50.72(b)(3)(iv)(A) for the first AFW pump automatic start. This event is reportable per 10 CFR 50.73(a)(2)(iv)(A) for a condition that resulted in automatic actuation of the RPS and AFW System. The health and safety of the public were not affected by the event since the equipment responded as designed.
05000382/LER-2013-00429 April 20133 September 2013Waterford10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Reactor Coolant System

A review of plant reactor coolant temperature trends from a planned outage shows that on April 29, 2013, reactor coolant temperature was raised from approximately 135 degrees F to approximately 180 degrees F as a planned evolution. On April 30, 2013, RCS temperature was raised from approximately 180 degrees F to approximately 345 degrees F as a planned evolution. Additionally, on April 30, 2013, plant operations involving water additions to the Volume Control Tank were conducted. A review of the Station Log shows that only one ENI log channel was operable during these evolutions. These evolutions were prohibited by the plant's Technical Specifications under these conditions.

TS 3.3.1 Action 4 requires, with only one log power channel operable in Mode 5 or Mode 4, suspending "all operations involving positive reactivity changes," and is clarified by an applicable note which states, "Limited plant cooldown or boron dilution is allowed provided the change is accounted for in the calculated shutdown margin.

Planned corrective action is to revise the TS bases for TS 3.3.1 to emphasize the limitations for usage of the note applicable to Action 4.

The planned heatup and dilution evolutions had no discernable effect on nuclear safety.

05000395/LER-2013-00124 March 201319 November 2013Summer10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Emergency Diesel Generator1.0 ABSTRACT On 3/24/2013 at 0458, a grid disturbance caused an undervoltage relay actuation on the "A" train 7200 Volt Switchgear Bus and the automatic start of the standby "A" Emergency Diesel Generator (EDG). At the time of the event, the "A" train Switchgear Bus was aligned to its normal offsite 115 kV power source. The grid disturbance was longer in duration than the associated undervoltage relay delay time. However the undervoltage event did not exist long enough to trip open the normal incoming breaker or initiate the Engineered Safety Features Load Sequencer (ESFLS). The EDG came up to the rated frequency and voltage, but the output breaker did not close, which was as expected. At 0520 the EDG was secured and restored to standby. The station was in Mode 5 for a mid cycle outage. All station equipment and all transmission system equipment operated as designed. Corrective actions to minimize the probability of reoccurrence have been added to the station's corrective action program. The event is reportable per 10CFR50.73(a)(2)(iv)(A), and 10CFR50.73(a)(2)(iv)(B)(8).
05000323/LER-2013-00212 March 201322 August 2013Diablo Canyon10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Control Rod

Refueling Outage Cycle 17, Unit 2 source range (SR) instrument N-32 experienced an unexpected increase in indicated counts per second (cps). Other available SR indications showed no rise in cps. At the time, SR instrument N-31 was inoperable. Since operators considered N-32 inoperable while N-31 was already inoperable, the audible count rate in the control room was no longer reliable. DCPP determined this condition constituted a loss of a safety function required to maintain the reactor in a safe shutdown condition and was reportable in accordance with 10 CFR 50.73(a)(2)(v)(A).

Following a vendor failure analysis, DCPP determined that a discontinuity in the cable insulation shield caused the N-32 high count rate readings. DCPP replaced the faulted cable. This condition did not adversely affect the health and safety of the public.

05000382/LER-2013-00316 November 201222 July 2013Waterford10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(ii)(b)
10 CFR 50.73(a)(2)(ix)
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Reactor Coolant System
Feedwater
Shutdown Cooling
On November 16, 2012 at 03:29 CST, it was identified that periodic testing had not been established for the local manual handwheel function on twenty-four safety related Air Operated Valves (AOV) that are required by design to operate after their associated air supply accumulator is exhausted. Additionally, license basis documents had not been updated to reflect an accumulator mission time. An inadequate evaluation had been performed of the substitution of manual operator action for automatic action by the AOV. Testing revealed that three AOVs would not operate by manual handwheel. There was one inoperable AOV in each of the Emergency Feedwater (EFW) flow paths to the Steam Generators, which made both EFW trains inoperable. There was an inoperable AOV manual override in the Auxiliary Component Cooling Water System, which made and the Train B Ultimate Heat Sink (UHS) inoperable. Since testing of the three AOV's handwheels had not been performed, it is indeterminate how long the condition existed; however, the condition had recently existed where both trains of EFW and UHS were required to be OPERABLE. At the time of discovery, Waterford 3 was defueled in a no mode condition and was in compliance with Technical Specification requirements. Actions were completed to restore the three valves' manual handwheels to an operable status.
05000336/LER-2011-0033 September 201126 October 2011Millstone10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
Steam Generator
Reactor Coolant System
Service water
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal

At 09:31 on September 3, 2011, with Millstone Power Station Unit 2 operating at 100 percent power in Mode 1, the "A" train service water loop was declared inoperable when leakage from a degraded service water spool piece degraded beyond pre-established limits. Plant Technical Specification 3.7.4.1 stipulates with one service water loop inoperable, restore the inoperable loop to operable status within 72 hours or be in cold shutdown (Mode 5) within the next 36 hours. Since the leak was unisolable, operators commenced a plant shutdown.

Cold Shutdown Mode 5 was entered at 17:03 on September 4, 2011.

The direct cause of the service water leak was a degraded coating on the piping flange located in the "A" train 10-inch service water line to the emergency diesel generator heat exchangers. The degradation mechanism of the flange is attributed to galvanic corrosion of the carbon steel material. Carbon steel is anodic to the adjacent alloy surfaces.

The pipe spool flange was replaced.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(i)(A) as completion of a nuclear plant shutdown required by the plant's Technical Specifications.

05000338/LER-2011-0013 February 20111 April 2011North Anna10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On February 3, 2011, at 0345 hours, with Unit 1 at 100 percent power, Mode 1, annunciator 1H-G4, Annunciator System DC Ground was received in the Main Control Room (MCR).

At 0348 hours annunciator 1B-D3, Boric Acid Tank 1B Hi-Lo Level CH I-II was received which, when acknowledged, locked in and annunciator 1H-G4 cleared. While investigating, an acrid smell was noticeable in the MCR. At 0353, upon entry into the annunciator system cabinet room, adjacent to the MCR, the door of the cabinet, 1-EI-CB-21, was opened and flames approximately 2 - 4 inches long were observed coming from an annunciator circuit card. Operations personnel entered fire contingency action procedure 0-FCA-0, Fire Protection - Operations Response. At 0354 hours, a two second discharge of a portable CO2 fire extinguisher put out the fire and a re-flash fire watch was established. At 0437 hours the fire contingency action procedure was exited. This event posed no significant safety implications since the fire was small, extinguished quickly, did not pose an actual threat to the safety of the nuclear power plant and it did not affect equipment required for safe operation of the plant. Therefore, the health and safety of the public were not affected by this event. This event is being reported voluntarily to share information and lessons learned.

05000498/LER-2004-0046 April 20047 June 2004South Texas10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On the morning of April 6, 2004, a Tornado Warning was issued for the South Texas Project. Unit 1 was in Mode 1 at 100% power. Unit 2 was in Mode 5 in a refueling outage. The Unit 1 Control Room directed all plant personnel to seek shelter over the public address system at 1140. Security Officers in elevated and ground positions were relocated inside the Mechanical Electrical Auxiliary buildings. Officers at the station checkpoints were relocated to the East Gate House and the Nuclear Support Center. At 1143 a Security Alert was declared by the Security Force Supervisor as defined in the Safeguards Contingency Plan.

Since the requirements of 10 CFR 73.55(e) and (h) were not met, the Unit 1 Shift Supervisor invoked 10CFR50.54(x) at 1151 for the protection of security personnel. The declaration of a Security Alert is an entry condition into the site Emergency Plan at the Unusual Event level. In accordance with site procedures the Unit 1 Shift Supervisor declared an Unusual Event at 1151.

The Owner Controlled Area and Protected Area patrols were secured at 1151 for their safety. At 1300, after the weather subsided, the security force began recovery by returning to the pre-tornado warning positions. At 1319, the site exited the Security Alert and the Unusual Event. The intrusion detection and threat assessment equipment were tested and compensatory measures established if appropriate. A search of the Protected Area was conducted and completed satisfactorily at 1422.

z NRC FORM 366 (7-2001