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 SiteStart dateTitleDescription
05000220/LER-2017-003Nine Mile Point6 September 2017
2 November 2017
Automatic Reactor Scram due to Reactor Vessel Low Water Level
LER 17-003-00 for Nine Mile Point, Unit 1, Regarding Automatic Reactor Scram due to Reactor Vessel Low Water Level

On September 6, 2017 at 1157, Nine Mile Point Unit 1 experienced an 'automatic reactor scram due to reactor vessel low water level. The automatic Reactor Protection System (RPS) actuation and reactor scram is reportable per 10 CFR 50.72 (b)(2)(iv)(B) and 10 CFR 50.73(a)(2)(iv)(A) as any event or condition that resulted in a manual or automatic actuation of any of the systems listed in 10 CFR 50.73(a)(2)(iv)(B). Following the automatic scram all plant systems responded per design including High Pressure Coolant Injection (HPCI) System automatic initiation.

HPCI is a flow control mode of the normal feedwater systems, and is not an Emergency Core Cooling System.

The root cause of the scram was a failed power supply within the Proportional Amplifier, PAM-ID23E. This power supply failure resulted in the output from the module dropping out causing the #13 Feedwater Pump Flow Control Valve to close. The corrective action taken was the replacement of the failed Feedwater Level Control module, PAM- ID23E.

05000387/LER-2017-005Susquehanna8 June 2017
4 October 2017
Automatic Reactor Protection System Trip on High Neutron Flux
LER 17-005-01 for Susquehanna, Unit 1 Regarding Automatic Reactor Protection System Trip on High Neutron Flux

On June 8, 2017 at 1527 hours, the reactor automatically scrammed due to a loss of Main Turbine- Electro-Hydraulic Control (EHC) logic power causing a high neutron flux, Reactor Protection System (RPS) trip. The safety systems operated as expected. Secondary Containment differential pressure lowered to 0" WG due to a trip of the normal operation of the Reactor Building Ventilation system. The differential pressure was restored by the initiation of Standby Gas Treatment System.

The scram was caused directly by a DC+ (direct current, positive) test lead (Maxi Grabber) that inadvertently contacted with the grounding screw, causing a short and momentary loss of EHC logic power.

Immediate action was taken to validate that there was no damage to the +30 VDC (volts DC) EHC logic.

The root cause for this event is an insufficient focus on the High Risk Activity of adjusting the EHC power supply, and inadequate risk mitigating actions for that activity.

The condition is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an automatic actuation of the RPS, including reactor scram. Although no safety system functional failure occurred, this event is also reportable pursuant to 10CFR 50.73(a)(2)(v)(C) as a condition that could have prevented fulfillment of a safety function. There were no actual, or potential consequences to the health and safety of the public as a result of this event.

I

05000458/LER-2017-00818 August 2017Automatic Reactor Scram due to Failure of Main Feedwater Regulator Transfer Relay

On August 18, 2017, at 8:55 p.m. CDT, an automatic reactor scram occurred while the plant was operating at 100 percent power. The operators promptly established control of reactor water level and pressure, and a controlled plant cooldown was commenced. The initial scram signal was a flow-biased thermal power trip on the average power range monitors.

This action closely followed a planned shift of the master feedwater controller from channel "B" to channel "A.

Troubleshooting discovered that the feedwater level channel select relay had failed such that no signal was present on the "A" channel. When that channel was selected, the feedwater system erroneously sensed that reactor water level was low, and caused all three feedwater regulating valves to move fully open. At the same time, the false low water level signal was sensed in the control circuitry for the reactor recirculation system, resulting in an automatic shift of the recirculation pumps to slow speed. The resultant decrease in core flow caused the flow-biased thermal power trip in the average power range monitors, actuating the reactor scram. The failed feedwater system relay was replaced with an updated model with gold contacts. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(iv) as an event resulting in the automatic actuation of the reactor protection system.

05000440/LER-2017-002Perry27 June 2017Loss of Safety Function Due to Main Turbine Bypass Valve Opening
LER 17-002-00 for Perry Nuclear Power Plant Regarding Loss of Safety Function Due to Main Turbine Bypass Valve Opening

On April 30, 2017, at 1818 hours, while the plant was at 100 percent rated thermal power, main turbine steam bypass valve number 1 partially opened. Power was subsequently lowered in an attempt to close the bypass valve. While lowering power the bypass valve would shut and then reopen and power would again be lowered. When power was lowered to approximately 74 percent the bypass valve remained closed. During the transient the reactor protection system (RPS) trip functions for the main turbine stop valve closure and turbine control valve fast closure scram were declared inoperable due to the opening of the bypass valve, which changes the bypass setpoint for those RPS trips. With the loss of RPS trip capability. a loss of safety function existed intermittently for approximately 37 minutes. The manual reactor trip function and other RPS functions remained operable.

Both channels of the rod withdrawal limiter (RWL) and the end of cycle reactor recirculation pump trip (EOC-RPT) function were also declared inoperable. These functions are credited in accident analysis and this also resulted in a loss of safety function in accordance with the plants Technical Specification bases.

The direct cause of the bypass valve opening was degradation of the Primary Low Value Gate (PLVG) card in the main turbine speed control circuit.

The safety significance of this event is considered to be small. This event is not considered a safety system functional failure as the specific functions were maintained and never bypassed during the event. This event is being reported under 50.73(a)(2)(v)(A) and 50.73(a)(2)(v)(D) for a loss of safety function.

05000458/LER-2017-001River Bend31 January 2017
3 April 2017
Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open)
LER 17-001-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open)
During a refueling outage that commenced on January 28, 2017, there were occasions during which maintenance was performed without taking the required actions to comply with the applicable Technical Specifications. Specifically, operations with a potential to drain the reactor vessel (OPDRVs) were conducted without establishing primary containment integrity, and the provisions of NRC Enforcement Guidance Memorandum (EGM) 11-003, Rev. 3, were invoked instead. The first such operation was commenced on January 31, and the final OPDRV was completed on March 4. This condition is being reported in accordance with 10 CFR 50.73(a)(2) (i)(B) as operations prohibited by Technical Specifications. During all OPDRVs, the prerequisites specified by the EGM were enforced. All activities were completed with no transients in reactor cavity water level having occurred. This event was, thus, of minimal safety significance with regard to the health and safety of the public. On December 20, 2016, NRC approved a generic Technical Specification amendment that can be used by licensees to reconcile this condition. It is required by the EGM that applicable licensees (including River Bend Station) must submit a request for this amendment by December 20, 2017.
05000440/LER-2017-001Perry17 March 2017Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3The condition reported by this LER is the result of planned activities in support of Refueling Outage 1R16 at the Perry Nuclear Power Plant (PNPP) In Enforcement Guidance Memorandum (EGM) 11-003 Revision 3, the NRC provided enforcement guidance, applicable to boiling water reactor licensees, that addresses the reported condition Although this allowance is provided by the NRC's enforcement guidance, the planned activities are still considered reportable in accordance with 10CFR50 73(a)(2)(1)(B) as a condition prohibited by Technical Specifications From March 17, to March 24, 2017, PNPP conducted Operations with the Potential for Draining the Reactor Vessel (OPDRV) while in Mode 5 at zero percent power, without an operable Primary and Secondary Containment These activities were performed in accordance with the EGM 11-003, Revision 3, which allows the implementation of interim actions as an alternative to full compliance with Technical Specifications provided several conditions are met The OPDRV activities were planned activities that were completed following the guidance of the EGM and are considered to have low safety significance based on the interim actions taken Since these actions were preplanned, no cause determination was necessary As required by the EGM, a license amendment request will be submitted, based on the Technical Specifications Task Force traveler associated with generic resolution of this issue, by December 20, 2017
05000354/LER-2016-005Hope Creek5 November 2016
13 March 2017
Reactor Protection System Actuation While the Reactor Was Shutdown
LER 16-005-01 for Hope Creek, Unit 1, Regarding Reactor Protection System Actuation While the Reactor Was Shutdown

On November 5, 2016, at 0404, a Reactor Protection System (RPS) actuation occurred due to a valid scram discharge volume high water level signal. This actuation was the result of a Redundant Reactivity Control System (RRCS) Alternate Rod Insertion (ARI) signal that was inadvertently generated during testing. The reactor was in cold shutdown at the time of the RPS actuation, with all control rods inserted. The Reactor Coolant System (RCS) pressure was 830 psig to support excess flow check valve testing, and shutdown cooling was removed from service. When the RRCS/ARI actuated, the B reactor recirculation pump tripped as expected, and the scram air header depressurized as expected.

The depressurization of the scram air header is a design feature of the ARI. The ARI signal established the control rod drive (CRD) system scram flow path. This resulted in a high water level in the scram discharge volume (SDV), an expected response. High water level in the scram discharge volume is an actuation signal for the RPS.

This is a condition reportable under 10 CFR 50.73(a)(2)(iv)(A) as an event or condition that resulted in a manual or automatic actuation of a listed system. The cause of the RRCS/ARI actuation is inadequate procedural guidance which resulted in a personnel error associated with partial procedure performance.

05000354/LER-2016-004Hope Creek23 October 2016
20 December 2016
1 OF 3
LER 16-004-00 for Hope Creek Regarding Operations With a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment

On October 23, October 24, and October 31, 2016, with Hope Creek Generating Station (HCGS) in a planned refueling outage and the reactor cavity flooded in OPCON 5, HCGS performed operations with a potential to drain the reactor vessel (OPDRV) without an operable secondary containment. These operations are prohibited by Technical Specification (TS) 3.6.5.1; however, NRC guidance provided in Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, allowed the implementation of interim actions as an alternative to full compliance. These actions were compiled in a plant procedure for the OPDRV activities performed at HCGS during Refueling Outage (HR20) in October 2016.

These OPDRV activities were planned activities that were completed under the guidance of plant procedures and confirmed to have low safety significance based on the interim actions taken. Since these actions were deliberate, no cause determination was necessary. Consistent with the guidance provided in EGM 11-003, Revision 3, HCGS will submit a license amendment request to adopt a Technical Specification Task Force (TSTF) traveler associated with generic resolution of this issue within four months after the issuance of the Notice of Availability of the TSTF traveler.

These conditions are being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

05000298/LER-2016-005Cooper1 October 2016Implementation of Enforcement Guidance Memorandum 11-003, Revision 3, Causes Conditions Prohibited by Technical Specifications

During Refueling Outage 29 (RE-29), Cooper Nuclear Station implemented the guidance of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, "Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel," dated January 15, 2016. Consistent with EGM 11-003, Revision 3, secondary containment operability was not maintained during Operations with a Potential for Draining the Reactor Vessel activities, and Required Action C.2 of Technical Specification (TS) 3.6.4.1 was not completed.

EGM 11-003, Revision 3, was implemented four times during RE-29. These conditions are being reported as conditions prohibited by TS.

Implementation of EGM 11-003, Revision 3, during RE-29 was a planned activity. As such, there were no root cause evaluations of the events. Consistent with the guidance provided in EGM 11-003, Revision 3, Nebraska Public Power District will submit a license amendment request to adopt a Technical Specifications Task Force (TSTF) traveler associated with generic resolution of this issue within 12 months after issuance of the Notice of Availability of the TSTF traveler.

- 005 -00 Cooper Nuclear Station 05000- 298 2016 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

PLANT STATUS

Cooper Nuclear Station (CNS) was in Mode 5, Refueling, at 0 percent power, at the time of the events.

BACKGROUND

On January 15, 2016, the Nuclear Regulatory Commission issued Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, "Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel." EGM 11-003, Revision 3, provides generic enforcement discretion to allow implementation of specific interim actions as an alternative to full compliance with plant technical specifications related to Secondary Containment operability during Mode 5 Operations with a Potential for Draining the Reactor Vessel (OPDRV) activities. To ensure compliance with interim actions specified in the EGM, CNS added guidance to plant Procedure 0.50.5, "Outage Shutdown Safety.

EVENT DESCRIPTION

During Refueling Outage 29 (RE-29), CNS implemented the guidance of EGM 11-003, Revision 3, four times. Consistent with EGM 11-003, Revision 3, Secondary Containment operability was not maintained during OPDRV activities, and Required Action C.2 of Technical Specification (TS) 3.6.4.1 was not completed.

The following provides the dates which EGM 11-003 was implemented:

1. On October 1 and 2, 2016, the EGM was utilized to allow work on Reactor Recirculation Pump A (RR-P-A) and RR-P-B without the jet pump plugs installed while performing Surveillance Procedure 6.1SGT.401, "SGT A Fan Capacity Test, SGT B Cooling Flow Test and Check Valve 1ST (Div 1).

2. From October 2-5, 2016, the EGM was utilized to allow work on RR-P-A, RR-P-B, Control Rod Drive (CRD) withdrawal/bypass operations and Hydraulic Control Unit (HCU) 42-31 during repairs to Main Steam Air Operated Valve 86B.

3. On October 6, 2016, the EGM was utilized to work on RR-P-A and RR-P-B without the jet pump plugs installed while draining Reactor Core Isolation Cooling 12 Relief Valve and flushing Main Steam Isolation Valves (MSIV).

4. From October 19-25, 2016, the EGM was utilized to work on RR-P-A. While using the EGM, work was also performed on CRD-V-113s (freeze seal), CRD Drive Venting, and CRD-V-105 (10-43) (freeze seal). These OPDRVs were in progress while Secondary Containment was inoperable for MSIV 86A and 86B repair, Reactor Building (RB) personnel airlock seal repair, shift of RB ventilation, Service Water Valve 531 draining and Residual Heat Removal Valve 57/67 draining.

Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000- 298 Cooper Nuclear Station 2016 - 005 - 00

3. LER NUMBER

BASIS FOR REPORT

These events are reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as conditions prohibited by CNS TS 3.6.4.1, which prohibits performing activities identified as OPDRVs in MODE 5 while secondary containment is inoperable.

SAFETY SIGNIFICANCE

As discussed in EGM 11-003, Revision 3, enforcement discretion is appropriate because the issues have low safety significance since licensees must implement compensatory measures to provide an adequate level of safety when using the discretion. To ensure compliance with the interim actions specified in the EGM, CNS added guidance to plant Procedure 0.50.5. This procedure was implemented for the OPDRV activities during which Secondary Containment was not operable.

CAUSE

Implementation of EGM 11-003, Revision 3, during RE-29 was a planned activity. As such, there were no root cause evaluations of the events.

CORRECTIVE ACTIONS

CNS will submit a license amendment request to adopt the Technical Specifications Task Force (TSTF) traveler associated with generic resolution of this issue, within 12 months after issuance of the Notice of Availability of the TSTF traveler.

PREVIOUS EVENTS

During RE-28, CNS implemented EGM 11-003, Revision 2, seven times. These events were reported under one License Event Report, LER 2014-004-00.

05000353/LER-2016-001Limerick1 June 2016
27 July 2016
Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error
LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error
A manual actuation of the reactor protection system (RPS) when the reactor was critical was initiated during Plant Process Computer (PPC) modification testing at power. A modification wiring design error caused an actuation of both reactor recirculation pump (RRP) trip relays when a circuit isolation switch was closed. The direct cause of the event was a circuit wiring design error implemented in the field that caused energization of the RRP adjustable speed drive (ASD) trip coils. The root cause of the event was a failure of station personnel to appropriately apply Technical Human Performance (THU) error prevention techniques to identify the design error and prevent its installation and testing as part of the modification. The isolation switch for the mis-wired circuit was opened to enable reset of the ASD trip coils. The 2A and 2B ASDs were returned to service. The corrective actions are to change the circuit design to correct the design error. The human performance aspects of the event will be addressed through several management actions that include reinforcement of proper standards and behaviors related to THU error techniques with station personnel.
05000219/LER-2016-003Oyster Creek29 June 2016Manual SCRAM Inserted due to Leakage from the D' Reactor Recirculation Pump Seal
LER 16-003-00 for Oyster Creek, Unit 1, Regarding Manual SCRAM Inserted due to Leakage from the 'D' Reactor Recirculation Pump Seal

On April 30, 2016, at 1804 hours, during the plant startup following the 1M38 maintenance outage, a reactor SCRAM was manually inserted by the Control Room Operators during post maintenance testing following work on the 'D' Reactor Recirculation Pump (RRP) mechanical seal. The SCRAM was initiated since leakage was discovered by a rising trend in drywell unidentified leakage during plant startup. The seal had been replaced during the maintenance outage. The SCRAM was selected as the preferred method of shutting down the reactor due to low decay heat conditions following the outage.

ENS 51895 was submitted on April 30, 2016, as required by 10 CFR 50.72 (b)(2)(iv)(B). This issue is reportable under 10 CFR 50.73(a)(2)(iv)(A), for any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B).

05000397/LER-2016-001Columbia28 March 2016
24 May 2016
MANUAL REACTOR SCRAM FOLLOWING LOSS OF REACTOR CLOSED COOLING
LER 16-001-00 for Columbia Regarding Manual Reactor Scram Following Loss of Reactor Closed Cooling

At 1322 PDT on March 28, 2016, a manual reactor scram was initiated in response to a loss of Reactor Closed Cooling (RCC). The loss of RCC was due to the opening of a Service Water (SW) valve at the inlet side of the Fuel Pool Cooling heat exchanger during performance of a partial surveillance without proper isolation of the RCC system piping from the heat exchanger. The cross-connection of the two systems caused depressurization and loss of flow from the RCC system into the non-pressurized SW piping. The SW valve was closed and the reactor was scrammed. Safety system responses to the scram signal were normal, with all control rods being fully inserted. Reactor decay heat was removed via bypass valves to the Main Condenser. No safety relief valves lifted and no emergency core cooling systems injected following the reactor scram.

The root cause was determined to be that plant Operators did not properly evaluate plant configuration when performing a partial surveillance including the marking as "N/A" (not applicable) of procedural steps, in accordance with plant procedures. Human performance aspects of the event were quickly addressed and additional corrective actions include reinforcing and monitoring procedure standards, and updating work control procedures at the station.

26158 R6 NRC Form 366 (01-2014)

05000352/LER-2016-003Limerick20 March 2016
18 May 2016
Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak
LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak
Reactor coolant system pressure boundary leakage was identified by a drywell leak inspection team during a planned shutdown for a Unit 1 refueling outage. This event resulted in a plant shutdown required by Technical Specifications. The Unit 1 'A' RHR Shutdown Cooling Return Check Valve equalizing line developed a crack at the toe of a weld due to high cyclic fatigue induced by vibration from the reactor recirculation system. The Unit 1 welds were reworked to EPRI 2x1 at select locations on the "A" and "B" RHR Shutdown Cooling Return check valve equalizing lines for HV-051-1F050A and 50B. The similar Unit 2 welds on equalizing lines for HV-051-2F050A and 50B will be examined and reinforced. The scope will be added into the next refueling outage (2R14) currently scheduled for April 2017.
05000325/LER-2016-001Brunswick7 February 2016
6 April 2016
Electriqal Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
LER 16-001-00 for Brunswick, Unit 1, Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
On February 7, 2016, at 1312 Eastern Standard Time (EST), Unit 1 was in Mode 1 (i.e., Run) at 88 percent of rated power in end-of-cycle coastdown. At that time, an electrical fault occurred on a balance of plant 4160-volt bus, resulting in a lockout of the Startup Auxiliary Transformer (SAT) and a loss of both Reactor Recirculation pumps. Licensed personnel inserted a manual scram per procedure. Emergency Diesel Generators supplied emergency electrical busses until offsite power was restored at 1628 EST. The loss of power and reactor water level changes resulted in automatic closures of various Primary Containment Isolation Valves (PCIVs). The electrical fault resulted in an electrical explosion; therefore, an Alert was declared at 1326 EDT. The immediate cause of this event was a fault in a non-segregated electrical bus connected to the SAT. The root causes were insufficient detail in applicable maintenance instructions for inspecting the non-segregated bus housing and inadequate instructions for terminating electrical cables in a circuit breaker cubicle. Corrective actions include repairing equipment damaged by the electrical fault and revising the procedures and work instructions.
05000440/LER-2016-001Perry24 January 2016
23 March 2016
Pressure Boundary Leakage, Level 8 Automatic SCRAM, and APRM Loss of Safety Function
LER 16-001-00 for Perry Nuclear Power Plant Regarding Drywell Leakage, Level 8 Automatic SCRAM and APRM Loss of Safety Function

At 2100 hours, on January 23, 2016, the Perry Nuclear Power Plant (PNPP) commenced a reactor shutdown to investigate unidentified leakage in the drywell. At 2122 hours, drywell unidentified leakage exceeded Technical Specification (TS) limits necessitating a plant shutdown as required by TSs. At 0357 hours, on January 24, 2016, while performing the shutdown required by plant TSs, the average power range monitors (APRM) became inoperable due to a calibration setpoint being out of tolerance in the nonconservative direction following a transfer of the reactor recirculation pumps to slow speed. This resulted in a loss of safety function for the APRMs. At 1007 hours, on January 24, 2016, with the plant at 8 percent power, during a feedwater shift to place the motor feed pump in service, reactor water level rose to the level 8 setpoint and the reactor protection system (RPS) automatically initiated, shutting down the reactor. Following the shutdown, a small leak was identified on the reactor recirculation loop "A" pump discharge valve vent line. The recirculation loop is part of the reactor coolant system; this resulted in a degraded condition and a condition prohibited by TS due to pressure boundary leakage.

The cause of the recirculation loop vent line leak was that the weld connecting the root appendage was not performed per the design drawing. The APRM calibration issue was caused by a change to the feedwater flow input to the heat balance. The cause of the reactor level rise and subsequent high water level scram was due to operator error in monitoring and manipulating feedwater system indications and controls.

The safety significance of this event is considered to be small. These events are being reported under; 50.73(a)(2)(i)(A), for completion of any plant shutdown required by the plant's TS; 50.73(a)(2)(ii)(A) for a condition resulting in the plant's principle safety barrier being seriously degraded; 50.73(a)(2)(i)(B) for a violation of Technical Specifications; 50.73(a)(2)(iv)(A) for actuation of the RPS while critical; and 50.73(a)(2)(v)(A) for a loss of safety function.

05000458/LER-2016-002River Bend9 January 2016
7 March 2016
Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient
LER 16-002-00 for River Bend, Unit 1, Regarding Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient
On January 9, 2016, at approximately 2:37 a.m. CST, with the plant operating at 100 percent power, an automatic reactor scram occurred concurrent with the closure of all main steam isolation valves (MSIVs). That action was the result of an electrical transient caused by a phase-to-phase fault on a nearby 230kV transmission line. The transient caused a momentary decrease in the voltage on both reactor protection system busses, which also power the MSIV control solenoids. The Division 2 primary containment isolation logic was also actuated, causing the Division 2 valves in balance-of-plant systems to close. Both divisions of the standby gas treatment system automatically started due to the shutdown of the normal annulus pressure control system. Both reactor recirculation pumps downshifted to slow speed. The company's transmission department investigated the event. Although no definite source of the fault was found, it was concluded that a lightning strike likely caused the transient. The fault occurred on a 230kV transmission line approximately three miles from the station. The fault lasted for 5.4 cycles before it was isolated by automatic breaker action, and caused the voltage on the switchgear supplying the RPS busses to decrease to approximately 34 percent of normal. This transient was sufficient to trip the scram solenoids and the MSIV solenoids. No plant parameter limits requiring the automatic actuation of any of the emergency core cooling systems or the emergency diesel generators were exceeded. This event, thus, was of minimal significance to the health and safety of the public. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv) as an actuation of the reactor ( protection system and the primary containment isolation logic. .
05000458/LER-2015-009River Bend27 November 2015
26 January 2016
1 OF 3
LER 15-009-00 for River Bend Station, Unit 1 Regarding Automatic Reactor Scram Due to Partial Loss of Offsite Power Caused by Fault in Local 230K Switchyard
On November 27,2015, at 4:31 a.m. CST, with the plant operating at 100 percent power, an automatic reactor scram occurred following the loss of power to both divisions of the reactor protection system (RPS). This condition resulted from a single-phase fault in the local 230kV switchyard. The initial response of the protective relays for the switchyard caused the breakers connected to the north 230kV bus in the switchyard to trip. The fault caused a voltage transient on the in-plant switchgear sufficient to trip the scram relays in the Division 2 RPS, resulting in a half-scram. The action of the protective relays continued, eventually causing the de-energization of reserve station service line no. 1. This lead to the loss of Division 1 RPS and a full reactor scram. The Division 1 and 3 emergency diesel generators started as designed to restore power to their respective safety-related onsite electrical distribution subsystems. No safety-related systems were out of service at the time of the scram, and reactor pressure and water level were promptly stabilized. All reactor control rods inserted properly. Multiple actuations of the main steam safety-relief valves (SRVs) occurred during the event. The nuclear steam supply system vendor reported this action was likely due to a localized pressure transient in the SRV instrumentation lines. SRV tailpipe temperature recorders indicated that all valves re-seated correctly following the initial transient. The cause of the event was an animal-induced fault in the 230kV switchyard that resulted in the automatic trip of the north bus feeder breaker to the RSS No. 1. The fault also caused the south bus feeder breaker to trip, de-energizing RSS No. 1.
05000263/LER-2015-007Monticello24 November 2015
21 January 2016
Loss of Residual Heat Removal Capability
LER 15-007-00 for Monticello Regarding Loss of Residual Heat Removal Capability

On November 24, 2015 at 0534 hours, the Monticello Nuclear Generating Plant was at 0% power in Mode 3 (Hot Shutdown) for a forced outage. While initially placing Shutdown Cooling (SDC) in service, the 12 Residual Heat Removal (RHR) pump tripped approximately 8-10 seconds after start due to the closure of the RHR SDC suction isolation valves. When placing SDC in service, flow rapidly increased after opening the RHR Division 2 Low Pressure Coolant Injection (LPCI) outboard injection valve causing a localized pressure transient in the reactor recirculation pump suction piping that resulted in an isolation of the SDC suction line. Reactor pressure vessel (RPV) pressure remained stable at approximately 30 psig.

Prior to attempting to place 'B' SDC in service, the Condensate system and the 'F' Safety Relieve Valve were in service providing decay heat removal. Immediate actions were taken to restore 'B' RHR SDC to operable status, thus an alternative method of decay heat removal was already established by the Condensate system and `F' Safety Relief Valve.

05000263/LER-2015-006Monticello23 November 2015
21 January 2016
- Reactor Scram due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line
LER 15-006-00 for Monticello Regarding Reactor Scram due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line

On November 23, 2015, a trip of the # 11 Reactor Recirculation Pump occurred, followed by a Group 1 isolation which resulted in a reactor scram. A post scram troubleshooting investigation determined a large spike in differential pressure occurred in the 'C' main steam flow instrumentation line at the time of the Group 1 initiation event.

The root cause of this event was determined to be legacy foreign material present in the 'C' main steam flow instrumentation line. This foreign material obstructed the instrumentation line and resulted in the momentary sensed high steam flow. The sensed high steam flow was not due to an actual high steam flow condition in the 'C' main steam line.

Since the presence of foreign material in the instrument line is a legacy issue, the corrective action for the root cause was to remove the foreign material. The corrective action for the trip of the reactor recirculation pump, will be to revise the fleet procedure to require verification of torque on accessible electrical connections for critical components which are bench tested and also to ensure that accessible soldered and crimped electrical terminations are inspected for sians of dearadation durina bench testina.

05000387/LER-2015-009Susquehanna11 January 2016Pressure Boundary Leakage From an Inadequate Weld Repair in Small Bore Pump Seal Vent Piping
LER 15-009-00 for Susquehanna, Unit 1, Regarding Pressure Boundary Leakage From an Inadequate Weld Repair in Small Bore Pump Seal Vent Piping

On November 13, 2015, at 1745 hours during drywell entry, a leak was reported on the "B" Reactor Reactor Recirculation (RXR) Pump Lower Seal Cavity Vent piping. The leak was identified at the inboard pipe-to-union weld and required a weld repair prior to returning to service. The affected piping weld is for 3/4-inch piping, schedule 80 SA-479 TP304 or TP316, union 3000# SA-182 Gr F304 or F316. The affected piping had been in service for approximately 11 months following a previous repair of the weld at this location during the December 2014 forced outage, (e.g., LER 2014-011-00, issued February 11, 2015).

The condition was reported on November 13, 2015 in accordance with 10 CFR 50.72(b)(3)(ii)(A) as a principal safety barrier degradation (EN 51538). This Licensee Event Report (LER) is written in accordance with 10 CFR 50.73(a)(ii)(A) and 10 CFR 50.73(a)(2)(i)(B) as a condition that resulted in a principal safety barrier degradation with evidence of reactor coolant pressure boundary leakage, which is a condition prohibited by the Technical Specifications.

The previous December 2014 weld repair did not fully excavate the weld and remove the J-groove, and thereby eliminate the presence of the crack.

Repair of the cracked weld was performed prior to the restart of Unit 1. The safety significance of this condition is minimal. Given the size of the leak, there were no consequences to the health and safety of the public.

05000354/LER-2015-005Hope Creek28 September 2015
5 January 2016
Reactor Scram Due to Invalid RRCS Actuation
LER 15-005-01 for Hope Creek, Unit 1, Regarding Reactor Scram Due to Invalid RRCS Actuation

On September 28, 2015, at 20:46, with the Hope Creek reactor operating at 100% power, a human error during surveillance testing resulted in the actuation of the Redundant Reactivity Control System (RRCS), and subsequently, an automatic reactor scram on a valid low water level signal. At the time of the transient, a surveillance test of division 1 of the RRCS system was in progress. The test simulates a high reactor pressure signal. Plant data show the signal was entered in both channels of division 1 of the RRCS system. The resulting system actuation caused a trip of both Reactor Recirculation Pumps, and the actuation of the Alternate Rod Insertion (ARI) function of the RRCS system. As a result of these two actuations, reactor power lowered, causing reactor water level to lower to the Reactor Protection System (RPS) trip set point of +12.5 inches. The RPS initiated an automatic reactor scram. Reactor operators recovered water level to within the desired band using the feedwater system. Reactor pressure was maintained using turbine bypass valves discharging to the main condenser.

This report is being submitted under 10 CFR 50.73(a)(2)(iv)(A), as an event or condition that resulted in the actuation of the Reactor Protection System.

05000220/LER-2015-004Nine Mile Point4 September 2015Automatic Reactor Scram Due to Main Steam Isolation Valve Closure

On Friday September 4th, 2015 at 09:16:04, Nine Mile Point Unit 1 automatically scrammed from approximately 100% rated power due to an inadvertent Main Steam Isolation Valve (MSIV) isolation. This event is reportable under 10 CFR 50.72 (b)(2)(iv)(B) and 10 CFR 50.73(a)(2)(iv)(A) as any event or condition that resulted in a manual or automatic actuation of any of the systems listed in 10 CFR 50.73(a)(2)(iv)(B). During quarterly surveillance testing, the MSIV failed to stop its close stroke and reopen automatically per design, due to a failed MSIV pilot test valve. The root cause of the event was an inadequate application of the designed pilot test valve for MSIV control, resulting in the pilot test valve internals binding during the surveillance test. The failed pilot valve spool and cage assembly were replaced.

The corrective action to prevent recurrence is to replace the MSIV pilot valveS with an industry proven design.

The event described in this LER is documented in the plant's corrective action program.

05000397/LER-2015-003Columbia13 May 2015Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 2

The condition reported by this LER was an expected condition, which was the result of planned activities in support of a routine refueling outage. As described in the LER, the U.S. Nuclear Regulatory Commission (NRC) provided enforcement guidance, applicable to boiling water reactor licensees, that allows the reported condition.

Although this allowance is provided by the NRC's enforcement guidance, the planned activities are still reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications (TS).

Between May 13, 2015 and June 13, 2015, Columbia Generating Station (Columbia) performed Operations with the Potential for Draining the Reactor Vessel (OPDRV) activities while in Mode 5 without an operable secondary containment, as expected and allowed by NRC Enforcement Guidance Memorandum (EGM) 11-003, Revision 2.

Although EGM 11-003, Revision 2, allows implementation of interim actions as an alternative to full compliance, this condition is still considered a condition prohibited by Technical Specification (TS) 3.6.4.1. The OPDRV activities were planned activities that were completed under the guidance of plant procedures and work instructions and are considered to have low safety significance based on the interim actions taken. Since these actions were deliberate, no cause determination was necessary. A license amendment request will be submitted following NRC approval of the Technical Specification Task Force (TSTF) traveler associated with generic resolution of this issue.

26158 R6 NRC Form 366 (01-2014) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017 Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Inf000llects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000354/LER-2015-002Hope Creek14 April 2015Operations With A Potential To Drain The Reactor Vessel (OPDRV) Without Secondary Containment

On April 14, April 15, April 17, April 20, April 27, and April 29, 2015, with Hope Creek Generating Station (HCGS) in a planned refueling outage and the reactor cavity flooded in OPCON 5, HCGS performed operations with a potential to drain the reactor vessel (OPDRV) without an operable secondary containment. These operations are prohibited by Technical Specification (TS) 3.6.5.1; however, recent NRC guidance provided in Enforcement Guidance Memorandum (EGM) 11-003, Revision 2, allowed the implementation of interim actions as an alternative to full compliance. These actions were compiled in a plant procedure for the OPDRV activities performed at HCGS during Refueling Outage (H1R19) in April 2015.

These OPDRV activities were planned activities that were completed under the guidance of plant procedures and confirmed to have low safety significance based on the interim actions taken. Since these actions were deliberate, no cause determination was necessary. Consistent with the guidance provided in EGM 11-003, Revision 2, HCGS will submit a license amendment request to adopt a Technical Specifications Task Force (TSTF) traveler associated with generic resolution of this issue within four months after the issuance of the Notice of Availability of the TSTF traveler.

These conditions are being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

05000388/LER-2015-003Susquehanna10 April 2015Unit 2 Automatic Reactor Scram Caused by Main Turbine Trip Due to Loss of Main Condenser Vacuum

On April 10, 2015, at 2100 hours, a planned shutdown for the Susquehanna Unit 2 refueling outage commenced. With shutdown in progress and at approximately 37% power for balance of plant operations, a pre-job brief was conducted in preparation for placing an Auxiliary Boiler in service and placing the Main Turbine Steam Seals on Auxiliary Steam.

At 2129 hours, the 'A' Auxiliary Boiler was placed in service per procedure OP-027-001, "Aux Boiler System," and the Main Turbine Steam Seals were placed on auxiliary steam via valve 221008, "SJAE and Steam Seal Aux Supply !so Vlv." At approximately 2330 hours, the procedure was resumed which directed closure of valve 221008 when Auxiliary Boiler temporary load is no longer needed. At this point, temporary load was no longer needed but auxiliary steam was still flowing through valve 221008, supplying steam to the Unit 2 Main Turbine Steam Seals. The valve was subsquenty closed, which isolated steam to the U2 Main Turbine Steam Seals, allowing air in-leakage into the Main Condenser, causing condenser vacuum to degrade. At 2346 hours, Unit 2 automatically scrammed from approximately 37 percent power due to a the Main Turbine trip on loss of condenser vacuum.

Root Cause: Personnel involved with auxiliary boiler startup did not adhere to Operator Fundamentals and effectively apply appropriate Human Performance error-reduction tools specific to understanding and anticipating the impact of component operation prior to its operation. Completed Action: Procedure OP-027-001, "Auxiliary Boiler System," was revised to caution operators of the potential for isolating auxiliary steam to the Main steam seals and/or Steam Jet Air Ejectors when securing temporary loading of the auxiliary boilers. Key Planned Action: Provide initial licensed and non-licensed operator classroom and job performance measure or dynamic learning activity training with focus on: STAR, Questioning Attitude, Pre job Brief, and understand and anticipate the impact of component operation prior to its operation. Safety Significance: There were no actual consequences to the health and safety of the public as a result of this event.

05000341/LER-2015-003Fermi19 March 2015Oscillation Power Range Monitor Upscale Reactor Scram during Single Loop Operation

On March 19, 2015 at 0702 EST the reactor protection system at Fermi 2 initiated an automatic reactor scram on Oscil ation Power Range Monitor (OPRM) Upscale following the manual trip of the north reactor recirculation pump due to a cooling water leak. The reactor protection system performed as expected and all control rods were fully inserted into the core. Reactor water level reached a low of approximately 126 inches above top of active fuel and was restored and maintained in the normal operating band by the feedwater and control rod drive systems. No safety relief valves actuated and reactor pressure was controlled by the main turbine bypass valves. Plant systems responded to the scram as designed and all reactor parameters were maintained within design limits following the event.

The cause of the automatic reactor protection system scram on OPRM Upscale was the neutron flux oscillations following the large core flow reduction and lowering feedwater temperature after the trip of a reactor recirculation pump. This event was documented and evaluated in the Fermi 2 Corrective Action Program. The associated root cause evaluation is in progress and may identify additional corrective actions which will be tracked and implemented by the corrective action program.

This event is reportable in accordance with 10 CFR.50.73(a)(2)(iv)(A) as a critical reactor scram.

05000298/LER-2014-004Cooper3 October 2014Implementation of Enforcement Guidance Memorandum 11-003, Revision 2, Causes Conditions Prohibited by Technical Specifications

During Refueling Outage 28 (RE-28), Cooper Nuclear Station implemented the guidance of Enforcement Guidance Memorandum (EGM) 11-003, Revision 2, "Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel," dated December 13, 2013. Consistent with EGM 11-003, Revision 2, secondary containment operability was not maintained during Operations with a Potential for Draining the Reactor Vessel activities, and Required Action C.2 of Technical Specification 3.6.4.1 was not completed.

EGM 11-003, Revision 2, was implemented seven times during RE-28. These conditions are being reported as conditions prohibited by Technical Specifications.

Implementation of EGM 11-003, Revision 2, during RE-28 was a planned activity. As such, there were no root cause evaluations of the events. Consistent with the guidance provided in EGM 11-003, Revision 2, Nebraska Public Power District will submit a license amendment request to adopt a Technical Specifications Task Force (TSTF) traveler associated with generic resolution of this issue within 12 months after the issuance of the Notice of Availability of the TSTF traveler.

05000265/LER-2014-002Quad Cities2 April 2014Cable Tray Fire Caused by Non-Conforming Cable Routing

On April 2, 2014, at 1228 hours, a Fire Alarm System (FAS) alarm was received for the Unit 2 D heater bay area. Although entry into the room at the time identified only a steam leak, subsequently various spurious alarms and electrical system anomalies occurred.

At 1303 hours, Unit 2 was manually scrammed, the turbine was tripped, and the main steam isolation valves (MSIVs) were closed to ensure the steam leak was isolated. A fire was identified to have occurred in the D heater bay (an area of the plant containing the high pressure (final stage) D feedwater heaters, and several Unit 2 cable trays and risers). The fire was extinguished by the automatic wet pipe sprinkler fire suppression system.

At 1340 hours, due to the manual de-energizing of safety-related motor control center (MCC) 29-1 in the reactor building in response to notification that smoke had been observed, an ALERT level Emergency Action Level classification was declared as HA3 (fire in a vital area affecting safety system equipment). The emergency was terminated at 2132 hours.

The cause of the event was an existing cable flaw that was caused by cable routing that exceeded the required minimum static bend radius.

Corrective actions included repairing impacted cables, replacing the failed steam seal expansion joint, operating procedure revisions, and additional inspections/tests.

The safety significance of this event was minimal. Given the impact on multiple systems, this report is submitted in accordance with 10 CFR 50.73 (a)(2)(iv)(A) for manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B); in accordance with 10 CFR 50.73 (a)(2)(v)(D) for an event that could have prevented the fulfillment of the safety function of systems needed to mitigate the consequences of an accident; and in accordance with 10 CFR 50.73(a)(2)(i)(A), for the completion of a nuclear plant shutdown required by the plant's Technical Specifications.

05000410/LER-2014-007Nine Mile Point2 April 2014Secondary Containment Inoperable Due to Simultaneous Opening of Airlock Doors

(NMP2) Reactor Building was breached when workers opened both inner and outer airlock doors, R261-1 and R261-2, simultaneously while passing through. The integrity of the airlock was re-established within 4 to 5 seconds when one of the doors was closed and latched. A second opening of both airlock doors occurred at 1140 that same day. Secondary containment differential pressure never exceeded the minimum Technical Specification limit of 0.25 inch of vacuum water gauge. These events are significant in that the secondary containment was momentarily breached during replacement of the Reactor Recirculation Pump "B" seal, an activity which had the potential for draining the reactor vessel (OPDRV).

The causal analysis identified that workers did not use their human performance verification tools to ensure the opposing outer door of the airlock was closed prior to opening the inner door. Corrective actions taken include coaching and counseling for workers involved in the event on the importance of applying their human performance tools of self-checking and peer-checking when passing through secondary containment doors. A previous LER submitted on a similar event could not be identified.

05000410/LER-2014-004Nine Mile Point10 March 2014Actuation of the Alternate Rod Insertion System and Subsequent Reactor Scram

On Monday March 10, 2014 at 1628 hours, Nine Mile Point Unit 2 (NMP2) experienced an actuation of the Alternate Rod Insertion (ARI) system which resulted in an automatic reactor scram from 99.2% thermal power.

An inadvertent Reactor Water Low-Low Level 2 signal from transmitters 2ISC*LT8A and 2ISC*LT8B initiated the Division I ARI which resulted in a Reactor Recirculation Pump trip and a full reactor scram. The event was caused by instrument perturbation while Maintenance I&C technicians were performing minor maintenance associated with changing labels on instrument drain valves in the vicinity of trip sensitive equipment. Safety related and other important equipment functioned properly during and after the scram. This event is reportable under 10 CFR 50.73(a)(2)(iv)(A). The causal analysis identified that station personnel have not adequately internalized the risk and implemented rigorous process and behavioral barriers to mitigate the vulnerabilities associated with work on or near trip sensitive equipment. Corrective actions taken or planned include:

1) Protect the trip sensitive equipment and 2) Implementing new fleet procedures/processes for work around trip sensitive equipment. A similar event was documented in NMP2 LER 2010-001.

05000410/LER-2014-003Nine Mile Point4 March 2014Uninterruptible Power Supply Failure and Subsequent Manual ScramOn March 4, 2014, at approximately 0143, Nine Mile Point Unit 2 (NMP2) was manually scrammed because of rising reactor recirculation pump (RRP) seal and motor temperatures. Prior to the scram, a failure of the Uninterruptible Power Supply, 2VBB-UPS3B, to provide uninterruptible power occurred. The malfunction of the Uninterruptible Power Supply (UPS) resulted in the inboard Primary Containment cooling water isolation valves closing and a Reactor Protection System (RPS) half scram. The closing of the inboard isolation valves resulted in the loss of cooling flow to the RRP seals and motors. The cause of the UPS malfunction was a degraded subcomponent associated with the UPS. The causal analysis for this event identified that it resulted from inadequate vendor and industry guidance/operating experience associated with the maintenance of a UPS related subcomponent. Corrective actions planned or taken include replacing degraded UPS subcomponents, revising preventative maintenance strategy, and working with the vendor to identify a list of single point of vulnerability (SPV) components that can prohibit the UPS from transferring to its alternate source when needed. The reportable condition described in this LER is documented in the plant's corrective action program as CR-2014-001725.
05000220/LER-2014-001Nine Mile Point12 February 2014Reportable Conditions Not Reported During the Previous 3 Years Involving Average Power Range Monitors InoperabilityThis LER is submitted to acknowledge that Nine Mile Point (NMP) missed providing LERs for past occurrences reportable in accordance with10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.73(a)(2)(v)(A) as conditions that could have prevented the fulfillment of the safety function of a structure or system needed to shutdown the reactor and maintain it in a safe shutdown condition. This condition was discovered on February 12, 2014. The reportable conditions occurred twice within the past three years when APRMs were declared inoperable as a result of reactor recirculation pump (RRP) trips. In each occurrence, the APRM flow-biased control rod block and scram function remained available, though, non- conservative. The cause of Operations personnel not recognizing the APRM conditions as reportable was due to ineffective training of Operations personnel. Corrective actions taken or planned include briefings and detailed training on reporting requirements and revisions to procedures that clarify event reporting requirements.
05000263/LER-2014-001Monticello17 January 2014Primary System Leakage Found in Recirculation Pump Upper Seal Heat Exchanger

On January 17, 2014, leakage into the Reactor Building Closed Cooling Water (RBCCW) System was determined to be Reactor Coolant Pressure Boundary (RCPB) leakage as identified by the Monticello Nuclear Generating Plant (MNGP) Technical Specifications (TS). Based on this, the TS limiting condition for operation was not met and a plant shutdown was required. The plant shutdown commenced at 2029 on January 17, 2014. There was no radioactive release from the plant. The plant was shut down without incident to repair the source of the inleakage.

The apparent cause for the RCPB leak was the lack of an established maintenance strategy in place to periodically check the condition of the heat exchanger or replace it. A crack formed in the #12 Recirculation Pump Upper Seal Heat Exchanger coil due to intergranular stress corrosion cracking.

The leaking # 12 Recirculation Pump Upper Seal Heat Exchanger was removed and the system was modified to operate without this heat exchanger by utilizing the excess capacity of the #12 Recirculation Pump Lower Seal Heat Exchanger.

05000354/LER-2013-009Hope Creek5 December 2013Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip

On December 5, 2013, at 03:25 EST, Hope Creek Unit 1 automatically scrammed from approximately 75 percent rated thermal power due to a main turbine trip that was caused by a high level in the 'A' moisture separator (MS).

The MS high level control loop was in the process of being tuned when the dump valve cycled repeatedly and subsequently failed closed. The main turbine trip automatic reactor scram resulted in a trip of both reactor recirculation pumps. The plant was stabilized in hot shutdown Operational Condition 3. During the recovery of the recirculation pumps, the digital electro-hydraulic control system was mis-operated which caused the turbine bypass valves to cycle. This caused reactor level to swell above Level 8 then shrink below Level 3 resulting in a second actuation of the reactor protection system.

A root cause evaluation determined the cause of the MS dump valve failure was thermal binding.

MS dump valve control has been modified from a modulating function to a full open function on high level to prevent valve cycling. The root cause determined that the MS dump valve clearances need to be modified to prevent thermal binding.

This is an event reportable under 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an automatic actuation of the reactor protection system.

05000410/LER-2013-004Nine Mile Point2 December 2013Manual Reactor Protection System Actuation due to Loss of Reactor Recirculation Flow

On December 2, 2013, at 0903, Nine Mile Point Unit 2 (NMP2) was lowering reactor power level to remove the main turbine from service to support maintenance. During the power reduction, the Low Frequency Motor Generators (LFMGs) did not start automatically. Attempts to manually start the recirculation system pumps in slow speed were unsuccessful and a manual reactor scram was inserted due to the sudden reduction in core flow.

This event is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A) as a condition that resulted in manual or automatic actuation of any of the systems listed in 10 CFR 50.73(a)(2)(iv)(B). The Reactor Protection System is listed in 10 CFR 50.73(a)(2)(iv)(B).

The root cause of this event is a failure to identify that the switches in the auto transfer circuits for the reactor recirculation pumps to shift from high speed to low speed are single point vulnerable (SPV) components because they were exempted from the AP-913 classification process. Since the switches were not classified as SPV components, no mitigation strategies were developed.

Corrective actions include revision of the operating procedures to manually start the LFMG sets and not rely on the auto transfer circuitry.

There are no similar Licensee Event Reports for NMP2.

05000353/LER-2013-001Limerick16 April 2013Valid Manual Actuation of the Reactor Protection System During Refuel Outage Testing

A valid manual actuation of the reactor protection system (RPS) occurred during a refueling outage with all control rods inserted.

The manual actuation of the RPS system was initiated when the mode switch was placed in the "Shutdown" position following an automatic actuation of RPS. The event was initiated by an unplanned automatic actuation of the turbine stop valve closed trip logic during an RPS surveillance test. The automatic RPS' system actuation was caused by a failure to follow the existing procedure change processes. A corrective action was completed which reinforced the requirements for partial procedure use and temporary procedure changes. The corrective action also established expectations for the review and approval of partial procedures and temporary procedure changes.

05000293/LER-2013-001Pilgrim10 January 2013Inadvertent Trip of Both Recirculation Pumps and Subsequent Manual Scram

On Thursday, January 10, 2013 at 1534 hour (EST), with the reactor at 100% core thermal power, both reactor recirculation pumps unexpectedly tripped and a manual reactor scram was inserted as required by station procedures. Following the reactor scram, all rods were verified to be fully inserted and the Primary Containment Isolation System Group II (Reactor Building) and Group VI (Reactor Water Cleanup System) actuations occurred as designed due to the expected reactor water level shrink associated with the scram signal. All other plant systems responded as designed. The scram was uncomplicated and decay heat was released to the main condenser via the turbine by-pass valves.

The cause of the two reactor recirculation pumps tripping was due to the inadvertent seal-in of a relay (pump trip interlock) in the Low Pressure Coolant Injection (LPCI) Loop Select Logic circuitry within the Residual Heat Removal (RHR) System during surveillance testing. When the logic was reset at completion of testing, a normally open relay contact (which was inadvertently closed) interlocked with the recirculation pumps circuit, sent a trip signal to their drive motor breakers.

Corrective action has been taken to revise the subject surveillance procedure with steps to reinstall relay covers and added a verifier to observe relay status/ state prior to resetting the relay logic circuit.

This event had no impact on the health and/or safety of the public.

05000388/LER-2012-004Susquehanna19 December 2012Unit 2 Automatic Scram Due to Low Reactor Pressure Vessel Level

At approximately 1731 hours on December 19, 2012, with the unit operating at approximately 18% power, Susquehanna Steam Electric Station Unit 2 automatically scrammed on low reactor pressure vessel (RPV) level (Level 3, +13 inches) while transitioning the 'A' reactor feed pump from discharge pressure mode to flow control mode. All control rods inserted and both reactor recirculation pumps tripped. Reactor water level lowered to approximately -29 inches causing Level 3 (+13 inches) isolations.

There were no automatic Emergency Core Cooling System initiations. No steam relief valves opened during the event. All safety systems operated as expected.

The scram and associated actuations were reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A) in EN 48607 at 2029 on December 19, 2012. These events are also reportable as an LER in accordance with 10 CFR 50.73(a)(2)(iv)(A).

The root causes of the event were: 1) decision making without a formal evaluation of impacts that reflected a conditioned operator response and inadequate risk evaluation of activities and 2) missed opportunities to identify and provide compensation for the design of the integrated control system logic interface with the valve breaker power.

Key corrective actions included: 1) providing operator training, 2) providing an equipment reliability update to crews, 3) issuing an Operations directive to minimize the knowledge based decisions, 4) revising the Units 1 and 2 reactor feed pump operating procedures, and 5) placing caution signs on the applicable valve breakers indicating that opening the breakers impacts Integrated Control System (ICS) logic. Key corrective actions planned include: 1) defining operator specific skill of the craft work activity actions in an Operations administrative procedure, 2) implementing changes to the station procedure use and adherence procedure, and 3) creating new or revised guidance on the need to identify actions to respond to or compensate for single point vulnerabilities.

There were no adverse consequences to the health and safety of the public as a result of this event.

FORM 366 (10-2010) X JB ISV Yes (10-2010) LICENSEE EVENT REPORT (LER)

05000325/LER-2012-006Brunswick19 September 2012Licensee Event Report
U.S.
ATTN: Mr. Victor M. McCree, Regional Administrator
Nuclear Regulatory Commission
Page 2 of 2
cc (with enclosure):
U. S. Nuclear Regulatory Commission, Region II
245 Peachtree Center Ave, NE, Suite 1200
Atlanta, GA 30303-1257
U. S. Nuclear Regulatory Commission
ATTN: Ms. Michelle P. Catts, NRC Senior Resident Inspector
8470 River Road
Southport, NC 28461-8869
U. S. Nuclear Regulatory Commission (Electronic Copy Only)
ATTN: Mrs. Farideh E. Saba (Mail Stop OWFN 8G9A)
11555 Rockville Pike
Rockville, MD 20852-2738
Chair - North Carolina Utilities Commission
P.O. Box 29510
Raleigh, NC 27626-0510
NRC FORM 366U U.S. NUCLEAR REGULATORY COMMISSION
(10-2010)
LICENSEE EVENT REPORT (LER)
(See reverse for required number of
digits/characters for each block)
1. FACILITY NAME
Brunswick Steam Electric Plant (BSEP), Unit 1
4. TITLE
APPROVED BY OMB: NO. 3150-0104EEXPIRES: 10/31/2013
Estimated burden per response to comply with this mandatory
collection request: 80 hours. Reported lessons learned are
incorporated into the licensing process and fed back to industry. Send
comments regarding burden estimate to the FOIA/Privacy Section (T-5
F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555
0001, or by internet e-mail to infocollects.resource@nrc.gov, and to
the Desk Officer, Office of Information and Regulatory Affairs, NEOB
10202, (3150-0104), Office of Management and Budget, Washington,
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not display a currently valid OMB control number, the NRC may not
conduct or sponsor, and a person is not required to respond to, the
information collection.
2. DOCKET NUMBER 3. PAGE
05000325 1 of 3
Operation Prohibited by Technical Specifications due to Operation With a Potential for Draining the
Reactor Vessel (OPDRV)

On September 15, 2012, Unit 1 began a forced outage to replace a 1B recirculation pump seal. On September 17, with the unit in Mode 4, a clearance was hung on the 1B recirculation loop and the recirculation pump suction and discharge isolation valves were isolated to provide the reactor coolant system boundary. After the valves were isolated, there was approximately 10 gpm of leakage by the seats.

On September 19, 2012, at approximately 0330 hours Eastern Daylight Time (EDT), secondary containment airlock doors were opened to facilitate additional ventilation flow to the reactor building, thereby improving working conditions. The decision to open the secondary containment airlock doors was based on BSEP established guidance that leakage through mechanical joints (e.g., valve or flange packing leaks, seat leakage through an isolation valve, flange leakage) is not an Operation with a Potential for Draining the Reactor Vessel (OPDRV). The NRC Senior Resident Inspector questioned this position and, ultimately, the NRC concluded that the activity did constitute an OPDRV. Conducting an OPDRV activity coincident with secondary containment being inoperable constituted operation prohibited by Technical Specification (TS) 3.6.4.1 and is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B).

The cause of this event was inappropriate application of guidance in plant procedure 001-01.01, "BNP Conduct of Operations Supplement." The immediate corrective action was to re-establish secondary containment.

05000352/LER-2012-005Limerick18 July 2012Valid Actuation of the Reactor Protection System With the Reactor Critical and Unusual Event Declared

A valid manual actuation of the reactor protection system was initiated due to an automatic trip of both reactor recirculation pumps. T The reactor recirculation pumps tripped due to a loss of stator cooling water following a failure of a connection in a 13 kV/480 VAC non-safeguard load center air termination cabinet. T An Unusual Event was declared due to flash-over damage on the failed transformer air termination cabinet which was classified as an explosion within the protected area boundary. T The cause of the failed transformer was a high voltage connection clamp that was larger than the 13 kV cable size and the cable was not installed properly. T The cable in use was a solid conductor and the clamp used was designed for stranded cable. T This resulted in overheating and subsequent failure of the connection which damaged the cable and the load center transformer. T The investigation determined that this connection is not disturbed during routine maintenance. T Therefore, this is believed to be a manufacturing issue. T The 124A load center transformer supply cable was upgraded to a stranded cable with a crimped lug connection. T The faulted 124A load center transformer was replaced and returned to service.

Similar load center transformers will be upgraded to stranded cable with crimped lug connections.