01-21-2016 | On November 24, 2015 at 0534 hours0.00618 days <br />0.148 hours <br />8.829365e-4 weeks <br />2.03187e-4 months <br />, the Monticello Nuclear Generating Plant was at 0% power in Mode 3 (Hot Shutdown) for a forced outage. While initially placing Shutdown Cooling ( SDC) in service, the 12 Residual Heat Removal ( RHR) pump tripped approximately 8-10 seconds after start due to the closure of the RHR SDC suction isolation valves. When placing SDC in service, flow rapidly increased after opening the RHR Division 2 Low Pressure Coolant Injection ( LPCI) outboard injection valve causing a localized pressure transient in the reactor recirculation pump suction piping that resulted in an isolation of the SDC suction line. Reactor pressure vessel ( RPV) pressure remained stable at approximately 30 psig.
Prior to attempting to place 'B' SDC in service, the Condensate system and the 'F' Safety Relieve Valve were in service providing decay heat removal. Immediate actions were taken to restore 'B' RHR SDC to operable status, thus an alternative method of decay heat removal was already established by the Condensate system and `F' Safety Relief Valve. |
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Category:Letter
MONTHYEARML24025A9362024-01-31031 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0055 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) IR 05000263/20230042024-01-31031 January 2024 Integrated Inspection Report 05000263/2023004 ML24024A0722024-01-24024 January 2024 Independent Spent Fuel Storage Installation, Onticello, Supplement to Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation IR 05000263/20244012024-01-22022 January 2024 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection 05000263/2024401 L-MT-23-054, Subsequent License Renewal Application Supplement 82024-01-11011 January 2024 Subsequent License Renewal Application Supplement 8 L-MT-23-047, License Amendment Request: Revision to the MNGP Pressure Temperature Limits Report to Change the Neutron Fluence Methodology and Incorporate New Surveillance Capsule Data2023-12-29029 December 2023 License Amendment Request: Revision to the MNGP Pressure Temperature Limits Report to Change the Neutron Fluence Methodology and Incorporate New Surveillance Capsule Data L-MT-23-056, Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 1 Part 22023-12-18018 December 2023 Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 1 Part 2 ML23349A0572023-12-15015 December 2023 and Independent Spent Fuel Storage Installation, Revision to Correspondence Service List for Northern States Power - Minnesota IR 05000263/20234022023-12-13013 December 2023 Security Baseline Inspection Report 05000263/2023402 L-MT-23-042, 2023 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.462023-12-11011 December 2023 2023 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.46 L-MT-23-052, Subsequent License Renewal Application Supplement 72023-11-30030 November 2023 Subsequent License Renewal Application Supplement 7 L-MT-23-051, Update to the Technical Specification Bases2023-11-28028 November 2023 Update to the Technical Specification Bases L-MT-23-049, Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 12023-11-21021 November 2023 Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 1 ML23319A3182023-11-15015 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation IR 05000263/20230032023-11-13013 November 2023 Integrated Inspection Report 05000263/2023003 and 07200058/2023001 L-MT-23-043, 10 CFR 50.55a(z)(1) Request Regarding OMN-17, Revision 1. VR-092023-11-13013 November 2023 10 CFR 50.55a(z)(1) Request Regarding OMN-17, Revision 1. VR-09 L-MT-23-038, License Amendment Request to Revise Monticello Technical Specification Surveillance Requirement 3.8.6.62023-11-10010 November 2023 License Amendment Request to Revise Monticello Technical Specification Surveillance Requirement 3.8.6.6 L-MT-23-046, Subsequent License Renewal Application Response to Request for Additional Information Round 2 - Set 12023-11-0909 November 2023 Subsequent License Renewal Application Response to Request for Additional Information Round 2 - Set 1 ML23291A1102023-10-23023 October 2023 Environmental Audit Summary and RCIs and RAIs ML23285A3062023-10-12012 October 2023 Implementation of the Fleet Standard Emergency Plan for the Monticello Nuclear Generating Plant and the Prairie Island Nuclear Generating Plant L-MT-23-041, Subsequent License Renewal Application Response to Request for Confirmation of Information Set 22023-10-0303 October 2023 Subsequent License Renewal Application Response to Request for Confirmation of Information Set 2 L-MT-23-037, Subsequent License Renewal Application Response to Request for Additional Information Set 32023-09-22022 September 2023 Subsequent License Renewal Application Response to Request for Additional Information Set 3 ML23262B0372023-09-19019 September 2023 Response to NRC Request for Additional Information Regarding the 2023 Monticello and Prairie Island Plant Decommissioning Funding Status Reports ML23248A2092023-09-18018 September 2023 Proposed Alternative VR-11 to the Requirements of the ASME OM Code Associated with Periodic Verification Testing of MO-2397, Reactor Water Cleanup Inboard Isolation Valve ML23256A1682023-09-13013 September 2023 Independent Spent Fuel Storage Installation and Monticello Nuclear Generating Plant - Voluntary Security Clearance Program 2023 Insider Threat Program Self-Inspection IR 05000263/20230102023-09-0707 September 2023 Commercial Grade Dedication Inspection Report 05000263/2023010 L-MT-23-036, Subsequent License Renewal Application Response to Request for Additional Information Set 2 and Supplement 62023-09-0505 September 2023 Subsequent License Renewal Application Response to Request for Additional Information Set 2 and Supplement 6 ML23214A2412023-08-31031 August 2023 Letter: Aging Management Audit - Monticello Unit 1 - Subsequent License Renewal Application IR 05000263/20230052023-08-30030 August 2023 Updated Inspection Plan for Monticello Nuclear Generating Plant (Report 05000263/2023005) L-MT-23-035, Subsequent License Renewal Application Supplement 52023-08-28028 August 2023 Subsequent License Renewal Application Supplement 5 ML23241A9732023-08-21021 August 2023 Request for Scoping Comments Concerning the Environmental Review of Monticello Nuclear Generating Plant, Unit 1, Subsequent License Renewal Application (Docket No. 50-263) L-MT-23-034, Subsequent License Renewal Application Response to Request for Additional Information Set 12023-08-15015 August 2023 Subsequent License Renewal Application Response to Request for Additional Information Set 1 ML23222A0122023-08-10010 August 2023 Independent Spent Fuel Storage Installation and Monticello Nuclear Generating Plant - Changes in Foreign Ownership, Control or Influence ML23215A1312023-08-0909 August 2023 License Renewal Regulatory Audit Regarding the Environmental Review of the Subsequent License Renewal Application IR 05000263/20230022023-08-0707 August 2023 Plantintegrated Inspection Report 05000263/2023002 L-MT-23-028, 2023 Refueling Outage 90-Day Inservice Inspection (ISI) Summary Report2023-07-31031 July 2023 2023 Refueling Outage 90-Day Inservice Inspection (ISI) Summary Report L-MT-23-032, 10 CFR 50.55a(z)(2) Request Regarding MO-2397, VR-112023-07-31031 July 2023 10 CFR 50.55a(z)(2) Request Regarding MO-2397, VR-11 ML23198A0412023-07-28028 July 2023 LRA Availability Letter ML23206A2342023-07-25025 July 2023 Independent Spent Fuel Storage Installation, and Monticello Nuclear Generating Plant, Changes in Foreign Ownership, Control or Influence ML23201A0352023-07-24024 July 2023 Notification of an NRC Biennial Licensed Operator Requalification Program Inspection and Request for Information ML23202A0032023-07-21021 July 2023 Independent Spent Fuel and Independent Spent Fuel Storage Installation, Monticello Nuclear Generating Plant, Submittal of Quality Assurance Topical Report (NSPM-1) L-MT-23-031, Subsequent License Renewal Application Supplement 4 and Responses to Request for Confirmation of Information - Set 12023-07-18018 July 2023 Subsequent License Renewal Application Supplement 4 and Responses to Request for Confirmation of Information - Set 1 ML23195A1732023-07-14014 July 2023 Revision of Standard Practice Procedures Plan IR 05000263/20235012023-07-13013 July 2023 Emergency Preparedness Inspection Report 05000263/2023501 2024-01-31
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000263/LER-2017-0062018-01-12012 January 2018 Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests due to Use of a Test Fixture, LER 17-006-00 for Monticello Regarding Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests Due to Use of a Test Fixture 05000263/LER-2017-0052017-09-20020 September 2017 Diesel Generator Emergency Service Water System Automatic Transfer to Alternate Shutdown Panel, LER 17-005-00 for Monticello Nuclear Generating Plant Regarding Diesel Generator Emergency Service Water System Automatic Transfer to Alternate Shutdown Panel 05000263/LER-2015-0042017-08-22022 August 2017 Past Inoperability of Turbine Stop Valve Scram Function Exceeded Technical Specification Requirements, LER 15-004-01 for Monticello Regarding Past Inoperability of Turbine Stop Valve Scram Function Exceeded Technical Specification Requirements 05000263/LER-2017-0042017-08-16016 August 2017 High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test, LER 17-004-00 for Monticello Regarding High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test 05000263/LER-2017-0032017-06-14014 June 2017 Main Steam Isolation Valve Leakage Exceeds Technical Specification Limits, LER 17-003-00 for Monticello Regarding Main Steam Isolation Valve Leakage Exceeds Technical Specification Limits 05000263/LER-2017-0012017-06-13013 June 2017 Reactor Scram and Group II Isolation Due to 11 Reactor Feed Pump (RFP) Removal from Service with 12 RFP Isolated, LER 17-001-00 for Monticello Regarding Reactor Scram and Group II Isolation Due to 11 Reactor Feed Pump (RFP) Removal from Service with 12 RFP Isolated 05000263/LER-2017-0022017-06-13013 June 2017 Main Steam Isolation Valve Closure Time Outside of Technical Specification Requirements, LER 17-002-00 for Monticello Nuclear Generating Plant Regarding Main Steam Isolation Valve Closure Time Outside of Technical Specification Requirements 05000263/LER-2016-0032017-05-25025 May 2017 HPCI Declared Inoperable Due to Excessive Water Level in Turbine, LER 16-003-01 for Monticello Regarding HPCI Declared Inoperable Due to Excessive Water Level in Turbine 05000263/LER-2016-0012017-05-25025 May 2017 High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak, LER 16-001-02 for Monticello Regarding High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak 05000263/LER-2016-0022016-09-30030 September 2016 Inadequate Appendix R Fire Barrier Impacts Safe Shutdown Capability, LER 16-002-00 for Monticello Regarding Inadequate Appendix R Fire Barrier Impacts Safe Shutdown Capability 05000263/LER-2014-0032016-07-13013 July 2016 Torus to Drywell Vacuum Breaker Dual Indication During Testing, LER 14-003-01 for Monticello Nuclear Generating Plant RE: Torus to Drywell Vacuum Breaker Dual Indication During Testing 05000263/LER-2014-0022016-07-13013 July 2016 Torus to Drywell Vacuum Breaker Did Not Indicate Closed During Testing, LER 14-002-01 for Monticello Regarding Torus to Drywell Vacuum Breaker Did Not Indicate Closed During Testing 05000263/LER-2015-0072016-01-21021 January 2016 Loss of Residual Heat Removal Capability, LER 15-007-00 for Monticello Regarding Loss of Residual Heat Removal Capability 05000263/LER-2015-0062016-01-21021 January 2016 - Reactor Scram due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line, LER 15-006-00 for Monticello Regarding Reactor Scram due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line ML1015505712009-09-12012 September 2009 Event Notification for Monticello on State Offsite Notification Due to Not Meeting Permit Requirements L-MT-05-035, LER 50-004-00 for Monticello Nuclear Generating Plant Regarding Voluntary LER for Control Rod Drive Insert Line Leakage2005-05-12012 May 2005 LER 50-004-00 for Monticello Nuclear Generating Plant Regarding Voluntary LER for Control Rod Drive Insert Line Leakage ML0216100952002-05-15015 May 2002 LERs 02-001-01 & 02-002-01 for Monticello Nuclear Generating Plant Re Mechanical Pressure Regulator Failure Causes Reactor Scram & Application of Instrument Deviation Acceptance Criteria Allowed As-Found Settings to Be Outside Tech Spec Val 2018-01-12
[Table view] |
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EVENT DESCRIPTION
On November 24, 2015 at 0534 hours0.00618 days <br />0.148 hours <br />8.829365e-4 weeks <br />2.03187e-4 months <br />, the Monticello Nuclear Generating Plant was at 0% power in Mode 3 (Hot Shutdown) for a forced outage. While initially placing Shutdown Cooling (SDC) [KE] in service, the 12 Residual Heat Removal (RHR) [BO] pump [P] tripped approximately 8-10 seconds after start due to the closure of the RHR SDC suction isolation valves [ISV].
When placing SDC in service, flow was rapidly increased after opening the RHR Division 2 Low Pressure Coolant Injection (LPCI) outboard injection valve [INV], causing a localized pressure transient in the reactor recirculation pump suction piping that resulted in an isolation of the SDC suction line. The RHR High Reactor Pressure annunciator [PA] was received and immediately cleared as the pressure switch [PS] upstream of 12 Recirculation Pump [AD] Suction valve in the 'B' Recirculation Loop actuated causing a Group 2 containment isolation signal. However, this was not expected as Reactor Pressure Vessel (RPV) [RPV] steam dome pressure remained stable at approximately 30 psig.
At 0535 hours0.00619 days <br />0.149 hours <br />8.845899e-4 weeks <br />2.035675e-4 months <br />, immediate actions were taken to restore 'B' RHR SDC to operable status.
At 0545 hours0.00631 days <br />0.151 hours <br />9.011243e-4 weeks <br />2.073725e-4 months <br />, an alternative method of decay heat removal was established by utilizing the Condensate [SD] system and 'F' Safety Relief valve [RV].
At 1354 hours0.0157 days <br />0.376 hours <br />0.00224 weeks <br />5.15197e-4 months <br />, the 12 RHR pump and 12 RHR Service Water pump were successfully placed in service on SDC and the plant reached Mode 4 (Cold Shutdown) at 1428 hours0.0165 days <br />0.397 hours <br />0.00236 weeks <br />5.43354e-4 months <br />.
EVENT ANALYSIS
The event was determined to be reportable in accordance with 10 CFR 50.73(a)(2)(v)(B) as an Event or Condition that Could have Prevented the Fulfillment of the Safety Function of Structures or Systems that are Needed to Remove Residual Heat. This event is considered a Safety System Functional Failure per NEI 99-02, Revision 7.
SAFETY SIGNIFICANCE
Prior to attempting to place 'B' SDC in service, the Condensate system and the 'F' Safety Relieve Valve were in service providing decay heat removal. These systems remained in service and, as demonstrated by steadily lowering RPV pressure and temperature, provided adequate decay heat removal until SDC was placed in service. Additionally, the Reactor Water Cleanup System [CE] was available for decay heat reject if needed. After the closure of the SDC suction valves and subsequent trip of the 12 RHR pump, immediate actions were taken to restore SDC to operable status. Since the reactor remained adequately cooled, there were no actual consequences as a result of the initial failed attempt to place SDC in service. There was no impact to the health and safety of the public.
CAUSE
Both reactor high pressure SDC isolation pressure switches are located on the 'B' Recirculation Suction Piping. When initially placing SDC in service the LPCI outboard injection valve was opened and flow into the 'B' Recirculation system increased to approximately 4000 gpm in several seconds. This rapid flow increase caused a localized pressure transient in the 'B' Recirculation pump piping that resulted in the isolation of the SDC suction valves. Closure of the SDC suction valves subsequently caused a trip of the 12 RHR pump due to loss of pump suction. Written documentation in the operations manual did not adequately address the sensitivity of the pressure switches while placing 'B' SDC in service.
CORRECTIVE ACTION
Since the Condensate system and the 'F' Safety Relieve Valve were already in service providing decay heat removal, an alternate method of decay removal did not need to be established. Immediate actions were taken to restore 'B' SDC to operable status.
The Operations Manual used to place 'B' SDC in service was re-performed in its entirety to verify proper valve alignment, ensure the piping was full of water, and verify acceptable temperatures existed prior to attempting to place the system in service. This included venting the RHR suction and discharge lines prior to placing 'B' SDC in service. Existing procedural guidance allowed the associated LPCI injection valve to be slowly throttled open to achieve required RHR pump flow without introducing a pressure transient that would challenge the reactor high pressure SDC isolation setpoint.
The 12 RHR pump was successfully started and placed in SDC mode to cool down the plant to MODE 4. The Operations Manual has been updated to provide additional guidance for placing SDC in service including the pressure switch sensitivity to injection flow rate changes when changing the position of the LPCI outboard injection valve.
PREVIOUS SIMILAR EVENTS
There were no Licensee Event Reports with similar causes of loss SDC within the 3 last years.
ADDITIONAL INFORMATION
The Institute of Electrical and Electronics Engineer codes for equipment are denoted by [XX].