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 Start dateReporting criterionEvent description
05000364/LER-2017-0053 January 2017
11 January 2018
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)()

During a reactor startup on November 13, 2017 at 0136, while at approximately 1.5°o power (MODE 2), an Excore Power Range Nuclear Instrument (N-42) was declared inoperable due to lower than expected detector amps and indicated power. N-42 was reading approximately 0.4°0 lower power than the other three Power Range instruments. The malfunction was determined to be the result of a failed High Voltage (HV) cable center pin connector to N-42. The HV cable connector was installed during N-42 rescahng on November 10, 2017 in preparation for startup physics testing. N-42 provides an input signal to Channel 2 of the Over Temperature Delta Temperature (OTDT) Reactor Trip Signal. Prior to the discovery of the N-42 failure, Channel 3 of OTDT had also been declared inoperable and associated bistables tripped due to a failed Pressurizer Pressure transmitter. Therefore, it was determined that two channels of OTDT were inoperable longer than allowed by Technical Specification (TS) 3.0.3. This condition is reportable per 10CFR50.73(a)(2X1)(B).

The HV cable connector was repaired and all channels were OPERABLE on November 14, 2017 at 1000. The installation of the HV cable connector with the faulty center pin was attributed to human error. Corrective actions include procedure changes, training, and departmental communications related to maintenance fundamentals.

05000364/LER-2017-00422 December 201710 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On October 31, 2017, while in Mode 6 and at 0% power level, the Turbine-Driven Auxiliary Feedwater (TDAFW) pump B-Train steam admission valve from the 2C Steam Generator failed to meet Technical Specification ('I'S) Surveillance Requirement (SR) 3.7.5,5. This SR requires that the valve's associated air accumulator provide sufficient air to ensure operation of the TDAFW pump during a loss of power or other failure of the normal air supply.

During the performance of a flow scan analysis it was identified that the air-operated actuator piston was leaking by the actuator ' o-ring. Although the steam admission valve would stroke open, the 2-hour acceptance criteria could not be met. It is likely that the steam admission valve was inoperable longer than allowed by the Required Action Statement (7 days) following the spring 2016 refueling outage when it passed its last associated surveillance. Therefore, this condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

Corrective actions included actuator repair during the outage and further evaluating the preventive maintenance frequency.

NRC FORM 386 (04.2017)

05000364/LER-2017-00320 December 201710 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On October 31, 2017, while in Mode 6 at 00 0 power level, it was discovered that a Unit 2 pressurizer safety valve (PSV). which had been removed during the October 2017 refueling outage (2R25) and shipped offsite for testing, failed its as-found lift pressure test. The PSV lifted below the Technical Specification (TS) 3.4.10 allowable lift setting value. Setpoint drift of the PSV is the most likely cause of the failure.

It is likely that the PSV was outside of the TS limits longer than allowed by the Required Action Statement (15 minutes) during the previous operating cycle in all applicable modes of operation. Therefore, this condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

The PSV was replaced during the October 2017 refueling outage.

05000364/LER-2017-00219 December 201710 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On November 1, 2017, while in Mode 6 and at 0% power level, one of the C Loop Main Steam Safety Valves (MSSV) as-found lift pressure did not meet the acceptance criteria of +/- 3% of the setpoint (1129 psig) as required by Technical Specifications (TS) Surveillance Requirement (SR) 3.7.1.1. The MSSV lifted at 1171 psig which is 9 psig outside of its acceptance range of 1096 to 1162 psig and 3.72°o above its setpoint. The apparent cause of exceeding the MSSV upper acceptance limit is degradation of the valve spring and/or valve spindle compression screw. The as-found settings remained within analytical bounds; therefore, operation of the facility in this condition had no impact on the health and safety of the public.

TS Limiting Condition for Operation (LCO) 3.7.1, IvISSVs, requires five MSSVs per steam generator to be operable in Modes 1, 2, and 3. Since the failure affected the lift pressure over a period of time, it is assumed that the C Loop MSSV was inoperable for a time greater than allowed by TS. Therefore, this occurrence is considered reportable per 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

The C Loop MSSV was replaced on November 5, 2017, while in Mode 5.

05000364/LER-2017-00123 June 2017
21 August 2017
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On June 23, 2017, during continued troubleshooting of a jacket water (JW) leak on the 2B Emergency Diesel Generator (EDG), it was determined that the backup service water (SW) makeup flow path to the JW expansion tank would not pass flow. This troubleshooting was conducted to validate operability assumptions made on April 21, 2017, after recurrence of a leak from the JW keep warm pump.

Based upon the measured leak rate from the April 21st event, the 2B EDG would have been unable to meet its 7 day mission time without the use of makeup water to the JW expansion tank. Had the 2B EDG received a demand signal after March 3rd, the EDG may not have been able to perform its safety function during a design basis accident due to the JW leak rate and inability to makeup to the JW expansion tank.

Since the 2B EDG may not have met its mission time from March 3, 2017 to April 21, 2017, the station unknowingly operated in a condition prohibited by Technical Specifications which is reportable under 50.73(a)(2)(i)(B).

05000364/LER-2016-00110 CFR 50.73(a)(2)(iv)(A), System Actuation

On 5/11/2016 at 0653 CDT, with Unit 2 (U2) at 29 percent power, the Hi-Hi Steam Generator (SG) setpoint was reached. This caused the main feedwater valves to isolate, the running main feedwater pumps to trip, automatic start of the Motor Driven Auxiliary Feed Pumps, and the main turbine to trip automatically. The reactor was manually tripped per procedure. This event is reportable as required by 10 CFR 50.73(a)(2)(iv)(A) due to a manual actuation of the Reactor Protection System and the automatic actuation of the Auxiliary Feedwater system.

The cause of the manual reactor trip was determined to be inadequate control of the feedwater system, leading to an overfilling of the Steam Generators. Corrective actions included additional training provided to the startup control room team on manipulations that affect the feedwater system. Also, more specific guidance on feedwater system operation and control during Startup from Hot Standby to Power Operations will also be incorporated into operating procedures.

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION 0,..0 .5 , ' 1- r.

% LICENSEE EVENT REPORT (LER) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Joseph M. Farley Nuclear Plant, Unit 2 05000- 364

A. PLANT AND SYSTEM IDENTIFICATION

Westinghouse - Pressurized Water Reactor Energy Industry Identification Codes are identified in the text as (XX).

B. DESCRIPTION OF EVENT

On 5/11/2016 at 0653 CDT, with Unit 2 (U2) at 29 percent power, the Hi-Hi Steam Generator (SG) setpoint was reached. This caused the main feedwater valves to isolate, the running main feedwater pumps to trip, automatic start of the Motor Driven Auxiliary Feed Pumps, and the main turbine to trip automatically. The reactor was manually tripped per procedure.

C. UNIT STATUS AT TIME OF EVENT

Unit 2, Mode 1, 29 percent power

D. CAUSE OF EVENT

The cause of the manual reactor trip was determined to be inadequate control of the feedwater system, leading to an overfilling of the Steam Generators.

E. REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT

This event is reportable as required by 10 CFR 50.73(a)(2)(iv)(A) due to a manual actuation of the reactor protection system and automatic actuation of the auxiliary feedwater system. The reactor was shut down at 0653 and mode 3 was entered to complete the necessary procedural actions. The Motor Driven Auxiliary Feed Pumps also started automatically which is reportable by 10 CFR 50.73(a)(2)(iv)(A). There was no loss of safety function and no radioactive release associated with this event. All required safety systems were available and the plant responded as expected. There were no actual consequences detrimental to the health and safety of the public and is considered to be of very low safety significance.

F. CORRECTIVE ACTION

Corrective actions included additional training provided to the startup control room team on manipulations that affect the feedwater system. Also, more specific guidance on feedwater system operation and control during Startup from Hot Standby to Power Operations will also be incorporated into operating procedures.

G. ADDITIONAL INFORMATION

Other system affected:

No systems other than those mentioned in this report were affected by this event.

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (11-2015) /0 ,..

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LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Joseph M. Farley Nuclear Plant, Unit 2 05000- 364 Commitment Information:

This report does not create any licensing commitments

Previous Similar Events:

05000364/LER-2015-0027 August 201510 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On November 12, 2015 at approximately 02:00 CDT, Farley Unit 2 was operating in Mode 5 at zero percent power in a planned maintenance outage when evidence from troubleshooting became available which led to the discovery that all of the Reactor Coolant System (RCS) Leakage Detection Instrumentation had been inoperable on August 7, 2015 for a period longer than allowed by Technical Specifications (TS).

Troubleshooting discovered that the A, B, and D channels of the Containment Cooling Level Monitoring System (CCLMS) had been inoperable since July 6, 2015. On August 7, 2015 the C CCLMS was tagged out at the same time as both the R11 and R12 Containment Radiation Detectors were taken out of service for a period longer than allowed by TS 3.4.15 Condition E and Limiting Condition for Operation (LCO) 3.0.3. This is a condition prohibited by Technical Specifications and is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(B).

The cause of this event was an incorrect conclusion regarding the operating conditions of the four Containment Cooler Level Indicators. Corrective actions included the repair of the containment coolers' sensing lines for full restoration of the CCLMS. Repairs were also made to the components associated with the steam leak in containment N`RC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (It sots 19.."'.‘ I ) / LICENSEE EVENT REPORT (LER) APPROVED BY ()MD: NO. 3150.0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and led back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Inform lion Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission. Washington DC 20555-0001, or by infernal e-mail to Infocollects.ResourceOnrc.gov, and to the Dal( Officer, Olice of Inlormalion and Regulatory Affairs, NEOB-10202. (3150-0104). Oka 01 Management and Budget.

Washington, DC 20503.11 a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required lo respond to, the information collection.

Joseph M. Farley Nuclear Plant, Unit 2 05000 - 364

NO

A. REQUIREMENT FOR REPORT

For a period of seven hours and 54 minutes on August 7, 2015 all required Reactor Coolant System Leakage Detection Instrumentation monitors required by Technical Specifications (TS) 3.4.15 were out of service and the required action per TS 3.4.15 Condition E and Limiting Condition for Operation (LCO) 3.0.3 to place the unit in Mode 3 within 7 hours was not met. This is a condition prohibited by TS and is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(B).

B. UNIT STATUS AT TIME OF EVENT

Unit 2, Mode 1, 100 percent power

C. DESCRIPTION OF EVENT

On November 12, 2015 at approximately 02:00 CDT, Farley Unit 2 was operating in Mode 5 at zero percent power and was in a planned maintenance outage to investigate a leak ins'de of conta nment. A troubleshooting effort was initiated to investigate numerous maintenance issues that had been occurring with the A, B, and D Containment Cooler Level Indicators (EIIS Code LI). The troubleshooting work revealed that the A, B, and D Containment Cooler Level Indicators were inoperable and were considered to have been inoperable since July 6, 2015, when drainage into the containment sump had exceeded one gallon per minute. During this time frame the plant conducted extensive investigations into the source of the leakage, including multiple containment walkdowns and observations, maintenance troubleshooting activities, and detailed chemistry sample results of the containment sump, all of which led to the conclusion of a Service Water leak from the C Containment Cooler. The plant also prepared for a maintenance outage in the event that the leakage approached shutdown thresholds and implemented measures to protect the plant from the consequences of increased leakage.

During the November 2015 maintenance outage a steam leak was found in Containment and was verified as the cause of the Containment Cooling Level Monitoring System (CCLMS) alarms. The A, B, and D containment coolers' sensing lines were found to be clogged and therefore the level transmitters were unable to perform their function.

A subsequent review of operator logs showed that on August 7, 2015 the B and C Containment Cooler Level Indicators were declared inoperable to perform troubleshooting. On the same day, containment radiation monitors R11 and R12 were taken out of service for calibration surveillance. Since A and D CCLMS were discovered to have been inoperable, this created an unrealized entry into Tech Spec 3.4.15 Condition E (all detection inoperable) for a period of seven hours and 54 minutes, and the required action of immediate entry into Limiting Condition for Operation (LCO) 3.0.3 requiring the plant to be in MODE 3 in 7 hours was not met.

The CCLMS and the steam leak were repaired prior to exiting the maintenance outage.

Reported lessons learned are incorporated into the licensing process and led back to Industry Send comments regarcing burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to Infocollects.ResourceOnrc.gov, and to the Desk Officer, Office ot Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. II a means used to impose an irdormation collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond lo, the intonation collection.

Joseph M. Farley Nuclear Plant, Unit 2 05000 - 364

NO

D. CAUSE OF EVENT

The cause of the unrealized entry into Tech Spec 3.4.15 Condition E was an incorrect conclusion that the A, B, and D Containment Cooler Level Indicators, which had not been alarming, were operable, and that the C Containment Cooler Level Indicator was improperly alarming. This conclusion was reinforced by performance of multiple containment walkdowns and observations, maintenance troubleshooting activities, and detailed chemistry sample results of the containment sump that were strongly indicative of Service Water.

E. SAFETY ASSESSMENT

The leak in containment migrated to the containment sump which was monitored by radiation detectors.

The sump level was trended by a level monitoring indication. The site planned a maintenance outage to repair the leak. This condition had no significant effect on the health and safety of the public.

The loss of all CCLMS, along with a planned removal from service of R11 and R12 for calibration, represented an unplanned entry into Tech Spec 3.4.15 Condition E. The Condition requires an immediate entry into LCO 3.0.3 and entry into Mode 3 in 7 hours. The August 7, 2015 event lasted 7 hours and 54 minutes which exceeded the 7 hour time limit and therefore constitutes a condition that is reportable pursuant to 10CFR50.73 (a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications.

F. CORRECTIVE ACTION

During the November 2015 planned maintenance outage repairs were completed on the containment coolers' sensing lines for full restoration of the CCLMS. Repairs were also made to the components associated with the steam leak in containment.

G. ADDITIONAL INFORMATION

1) Failed Components: Level Indicator (LI) 2) Previous Similar Events: A search did not reveal any similar reported events for Plant Farley.

3) Energy Industry Identification System Code: Containment Leakage Control System (BD) 4) Other systems affected: There were no other systems, structures, or components that were affected by or contributed to the event.

5) Commitment Information: This report does not create any licensing commitments.

05000364/LER-2015-0019 January 2015
13 January 2016
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On 1/9/2015 at 1255 CST with Unit 2 operating at 100 percent thermal power the Turbine Driven Auxiliary Feedwater (TDAFW) pump was declared inoperable based on a causal investigation for a November 2014 surveillance test failure. The causal analysis identified that a design vulnerability existed which was the cause of both the November failure and a similar April 2014 failure. This vulnerability with the governor control system created a configuration within the software that had the potential for an expected trip signal to be recognized as a shutdown signal during the start sequence. Due to his condition, the TDAFW Pump could not be relied on to start for some plant conditions in the accident analysis for a Main Steam Line Break (MSLB) such that a reasonable assurance of operability could no longer be supported. Other accident analysis conditions were found to be unaffected. The cause of the design error was missing information in the original design documentation which would have provided an opportunity to develop the design change correctly in 2011.

For corrective actions, a temporary modification was made to increase a timer setpoint to eliminate the design vulnerability. This modification will be made permanent through the design change process. Design documents will be revised to add missing information which led to the design vulnerability.

Supplement: A past operability review has been completed and the results are appended to this LER.

05000364/LER-2014-00315 November 201410 CFR 50.73(a)(2)(iv)(A), System Actuation

On 11/15/2014 at 0348 CST while withdrawing control rods for reactor startup and low power physics testing with control bank C at approximately 50 steps and the reactor subcritical, Digital Rod Position Indication (DRPI) for one of the control rods (M12) changed to 90 steps. The control room operators stopped withdrawing rods and entered the Abnormal Operating Procedure (AOP) for Malfunction of the Rod Control System. The reactor trip breakers were opened at 0353 CST and all rods inserted as expected. Causal analysis determined that the DRPI signal for rod M12 was invalid due to a failure of the detector/encoder card associated with the M12 rod.

This notification is being made as required by 10CFR 50.73(a)(2)(iv)(A) due to a manual actuation of the reactor protection system occurring when the control room operators opened the Unit 2 reactor trip breakers via the main control board hand switch during reactor startup procedures. This was a valid actuation of the reactor protection system.

For corrective actions, the suspect DRPI detector/encoder card was replaced. The card will be sent to a vendor for failure analysis to determine the component on the card that actually failed. As an enhancement action, the AOP for Malfunction of the Rod Control System will be revised to assess rod position indication malfunction.

APPROVED BY OMB: NO. 315B-0104 EXPIRES: 01/31/20I7 R.:parted lessons teamed aro incorporated into the icansIng process and led back to Industry.

Send comments regarang burden esumate to the EOM, Pnvacy and Information Collections Branch (T-5 F53) US. Nuclear Regulatory Comrassoon, Washington, DC 20555.0001, or by Inland email to Infocollects.RE .sourceOnrcgov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOS1 0202, (3150-0104), Office of Air germ! and Budget, Washington DC 20503.11 a moans used to Impose an Information celestial does not display a currently valid OMB curitml numba, the NRC m“y not conduct or spori_orr, end a person is not required to respond to, the Information collodion.

05000364/LER-2014-00214 October 201410 CFR 50.73(a)(2)(iv)(A), System Actuation

On 10/14/14 at 0341 CDT, Unit 2 reactor was manually tripped after a lightning strike In the High Voltage Switchyard (HVSY) led to a phase 3 to ground fault on a 500kV transmission line resulting in a B train Loss of Site Power (LOSP). The fault caused the 2B Startup Auxiliary Transformer (SAT) Instantaneous overcurrent relay to actuate and resulted in de- energizing the 2B SAT. A missing nut in the Power Circuit Breaker (PCB) protection circuitry caused a high resistance on one side of the current transformer circuit resulting in an imbalance in current flows and an actuation in the primary differential instantaneous overcurrent relaying. The B train LOSP in conjunction with the 2B Emergency Diesel Generator (EDG) being out of service for a planned maintenance outage caused a loss of Component Cooling Water (CCW) to the Reactor Coolant Pumps (RCP). The Unit 2 Abnormal Operating Procedures for loss of CCW and loss of A or B Train Electrical Power were entered and the reactor was manually tripped and the RCPs were secured. The reactor trip is reportable per 10 CFR 50.73(a)(2)(iv)(A) for manual actuation of the reactor protection system. Additionally, the reactor trip resulted in a valid actuation of the Auxiliary Feedwater system which is reportable per 10 CFR 50.73(a)(2)(iv)(A).

Corrective actions include: installed the missing PCB current transformer (CT) nut; satisfactorily tested primary and secondary protective relaying for 2B SAT; and strengthening of switchyard standards of the utility performing the maintenance. Extent of Condition walkdowns were performed for other circuits in the HVSY and repaired as necessary.

NBC FoRm 366 (03.2014)

05000364/LER-2013-00129 May 201310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On May 29, 2013, with Unit 2 operating in Mode 1 at 100% power, Engineering personnel performing a review of Unit 2 beginning-of-cycle power ascension data identified that 2C Steam Generator Steam Flow Transmitter FT-494 did not meet Technical Specification calibration accuracy requirements. Based on this information the steam flow instrument was declared inoperable and the required actions of the appropriate Technical Specification were performed.

However, since the data utilized in the engineering review was obtained on May 14, 2013, it is known that FT-494 has been inoperable since May 14, 2013. Consequently, the time limits of the applicable Technical Specification required action were not met. This represents a condition prohibited by Technical Specifications and is reportable under 10CFR50.73(a)(2)(i)(B). Steam flow transmitter FT-494 was re-calibrated and returned to service on June 1, 2013. This out-of- tolerance condition of FT-494 also occurred at the beginning of the previous fuel cycle. This supplemental report contains causal analysis and corrective action information that was not available for the original report.

Joseph M. Farley Nuclear Plant, Unit 2 05000 364

05000364/LER-2012-00110 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On September 12, 2012, while Unit 2 was in Mode 1 at approximately 100% power, an external inspection of the Unit 2 Turbine Driven Auxiliary Feedwater (TDAFW) Pump flow orifice plates (OR) identified the thickness to be 1/8 inch versus 1/2 inch as specified in design drawings. An evaluation of this condition was unable to provide assurance of orifice plate geometry and integrity under design maximum flow conditions. As a result, the Unit 2 TDAFW Pump (P) was declared INOPERABLE and Technical Specification 3.7.5 condition B was entered. Temporary Modification SNC429958 was subsequently implemented to limit the maximum pressure drop across the orifice plates to an acceptable level by restricting the open movement of the TDAFW flow control valves. This allowed the restoration of the TDAFW Pump to OPERABLE status within the time limit of Technical Specification 3.7.5 condition B. A review of maintenance history has determined that prior to initial plant operation, design changes were issued in 1977 and 1978 to replace originally installed 1/8 inch orifice plates with 1/2 inch orifice plates. For unknown reasons these design changes for orifice plate replacement were not implemented.

Since the 1/8 inch orifice plates have been in place for the life of the plant, this represents a condition prohibited by Technical Specifications and is reportable under 10CFR50.73(a)(2)(i)(B).

This condition is additionally reportable under 10CFR50.73(a)(2)(ii)(B) and 10CFR50.73(a)(2)(v)(D).

05000364/LER-2011-0017 July 201110 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On July 30, 2011 at 23:04 while at 100% power, the Unit 2 Turbine Driven Auxiliary Feedwater Pump (TDAFWP) automatically tripped on overspeed during surveillance testing. Through subsequent investigation it was determined that Unit 2 was not in compliance with Technical Specification (TS) 3.7.5 in that the Unit 2 TDAFWP had been rendered inoperable on July 7, 2011 at approximately 10:44 as a result of an inappropriately planned maintenance activity to correct an apparent wiring discrepancy that impacted turbine governor speed control. Electrical leads were incorrectly identified as spares and erroneously removed per plant drawings that contained unknown legacy errors. In addition, on several occasions during the time the Unit 2 TDAFWP was unknown to be inoperable; a second train of Auxiliary Feedwater (AFW) was made inoperable to support routine scheduled maintenance of Emergency Diesel Generators (EDG) and a Motor Driven Auxiliary Feedwater Pump (MDAFWP). This resulted in two of three trains of AFW being inoperable. This represents a condition that could have prevented the fulfillment of a safety function because two out of the three trains of AFW are required to meet flow requirements for limiting design basis accidents (DBA). The Unit 2 TDAFWP wiring was restored to the correct configuration and subsequent surveillance testing was completed satisfactory on August 1, 2011 at 03:40.

NRC FORM See (10-2010)

05000364/LER-2010-0035 August 200910 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

During the period between August 5 and August 9, 2009, the Unit 2 power supply to 1-2R 600 V load center (LC) did not meet the Unit 2 portion of Technical Specification (TS) 3.8.9 "Distribution Systems - Operating." This was discovered on August 9, 2009 when during routine surveillance for on-site AC distribution, the Unit 2 4160 V supply breaker DH08-2 to 1-2R 600 V LC was found in due to the 4160 V supply breaker DH08-2 from Unit 2 being open, and the required action statement was entered on August 9, 2009 at 02:02. Subsequently, the 4160 V supply breaker DH08-2 was closed on August 9, 2009 at 03:36. The 4160 V supply breaker DH08-2 being open resulted in a failure to meet TS 3.8.9 limiting condition for operation (LCO) for maintaining two trains of AC vital bus electrical power distribution subsystems operable. The 1-2R 600 V LC did not meet its surveillance requirement of correct breaker position and voltage for longer than the allowed by TS.

The 4160 V supply breaker DH08-2 was left open due to omission of relevant information in procedures and the interpretation of LCO 3.8.9 that existed at the time.

05000364/LER-2010-00222 May 201010 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 22, 2010 at 16:34, with Unit 2 at 100% power, the reactor was manually tripped due to 2C Steam Generator (SG) Feedwater Regulating Valve (FRV) failing closed. At approximately 16:34, the control room crew received multiple alarms associated with 2C SG level and a process cabinet failure.

The crew noted no feedwater flow and decreasing level in 2C SG. Manual control of the 2C SG FRV was attempted but there was no power or control capability of the main feedwater regulating valve. At approximately 40% narrow range level in the 2C SG, the crew manually tripped Unit 2 prior to the automatic trip setpoint of 28% narrow range level. All safety systems functioned as designed without complications.

Investigation revealed that the controller driver (NCD) card in the 2C SG FRV controller circuitry failed causing the 2C SG FRV to close. The failed NCD card was replaced. Unit 2 was restarted and returned to Mode 1 on May 23, 2010 at 17:12.

05000364/LER-2008-00110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

Auxiliary Building B-Train Battery (EJ). The STP was signed off as satisfactory. This quarterly STP was repeated on May 7, 2008 and Cell number 33 of B-Train Battery was determined to have a voltage of 2.06 V which is below the minimum allowed cell voltage of 2.08 V. Technical Specifications (TS) Action statements were entered which resulted in Cell number 33 being replaced on June 3, 2008. On June 6, 2008 during the review of the paper work associated with this Cell replacement, SNC determined that the February 11, 2008 STP was approved in error since the recorded voltage for Cell number 33 was 2.06 V which is below the minimum allowed voltage of 2.08 V. The recorded voltage was transcribed illegibly by the journeymen and subsequently misread by the journeymen and supervisor as 2.16 V. This error resulted in the B-Train battery being inoperable between February 11 and May 7, 2008 due to not completing the required TS Action Statement.

Cell number 33 of the 2B Auxiliary Building Battery was replaced on June 3, 2008. Personnel involved in the event have been coached on the importance of attention to detail when using procedures and legibility of recorded data.

05000364/LER-1999-001, Forwards LER 99-001-00 Re Reactor Trip Due to Loss of Condenser Vacuum Steam Dump Drain Line Failure.Commitments Made by Licensee,Listed2 July 1999
05000364/LER-1998-005, Forwards LER 98-005-00 Re TS 3.0.4 Not Being Met During Mode Change Due to Turbine Driven Auxiliary Feedwater Pump Being Inoperable.No NRC Commitments Contained in LER10 June 1998
05000364/LER-1998-004, Forwards LER 98-004-00,IAW 10CFR50.73(a)(2)(i).Commitments Made within Ltr,Listed18 May 1998
05000364/LER-1998-002, Forwards LER 98-002-00 Re Discovery of Turbine Auto Stop Oil Pressure Switch Setpoints Being Out of TS Limits.Commitments Made by Util,Discussed4 May 1998
05000364/LER-1998-001, Forwards LER 98-001-00 Re Manual Reactor Trip Due to Dropped Control Rod K-2.Two NRC Commitments Contained in Corrective Action Section of LER16 April 1998
05000364/LER-1995-001, Forwards LER 95-001-01.Rev Provides Corrected Total of in-service Sleeves & Sleeved Tubes in 2C S/G Following U2RF10 & Includes Data Associated W/L* Tubes as Result of Event Described in LER 96-002-00 (Unit 2)14 June 1996
05000364/LER-1984-002, Revised LER 84-002-01:on 840124,hourly Firewatch Patrol in Train B Auxiliary Bldg Battery Charger Room Not Performed at Specified Times.Caused by Personnel Error.Personnel Counseled & Firewatch Patrol Immediately Performed27 February 1984
05000364/LER-1983-054, Updated LER 83-054/03X-1:on 831028 & 1103,instrumentation Channel Associated W/Flow Transmitter FT-496 Declared Inoperable Due to Erroneous Indication.Cause unknown.FT-496 Instrumentation Channel Operable on 831029 & 110413 December 1983
05000364/LER-1983-022, Forwards LERs 83-020/03L-0 & 83-022/03L-0.W/o LER 83-022/03L-020 May 1983
05000364/LER-1983-021, Forwards LER 83-021/03L-05 May 1983
05000364/LER-1983-019, Forwards LER 83-019/03L-03 May 1983
05000364/LER-1983-018, Forwards LER 83-018/03L-022 April 1983
05000364/LER-1983-016, Forwards LER 83-016/03L-014 April 1983
05000364/LER-1983-015, Forwards LER 83-015/03L-024 March 1983
05000364/LER-1983-014, Forwards LER 83-014/03L-08 April 1983
05000364/LER-1983-003, Forwards LER 83-003/03L-016 February 1983
05000364/LER-1983-002, Forwards LER 83-002/03L-017 February 1983
05000364/LER-1982-051, Forwards LER 82-051/03L-029 December 1982
05000364/LER-1982-049, Corrected LER 82-049/03L-0:on 821201,containment Atmosphere Activity Monitor R-11 & R-12 Declared Inoperable When Vacuum Pump Tripped Due to Erroneous High Flow Signal. Caused by Defective High Flow Relay.Relay Replaced23 December 1982
05000364/LER-1982-047, Corrected LER 82-047/03X-1:on 821124,determined FNP-2-STP-63.0 (Area Temp Monitoring) Not Performing Per Tech Specs.Caused by Personnel Error.Procedure FNP-2-STP-1.0 Revised.Area Temp Monitoring Completed28 December 1982
05000364/LER-1982-046, Forwards LER 82-046/03L-01 December 1982
05000364/LER-1982-043, Forwards LER 82-043/01T-010 November 1982
05000364/LER-1982-041, Forwards LER 82-041/03L-028 October 1982
05000364/LER-1982-033, Forwards LER 82-033/03L-119 October 1982
05000364/LER-1982-032, Forwards LER 82-032/03L-019 August 1982
05000364/LER-1982-029, Corrected LER 82-029/03L-0:on 820623,7 River Water Pump Declared Inoperable When Motor Tripped.Caused by Ground Fault on Phase C Power Supply Cable.Defective Cable Replaced & Declared Operable on 82062612 July 1982
05000364/LER-1982-028, Forwards LER 82-028/01T-024 June 1982
05000364/LER-1982-027, Corrected LER 82-027/03L-0:on 820622,steam Jet Air Ejector Noble Gas Activity Monitor Declared Inoperable When Pegged High While All Other Indications Normal.Caused by Faulty Detector.Detector Replaced & Declared Operable on 8212 July 1982
05000364/LER-1982-025, Forwards LER 82-025/03L-09 July 1982
05000364/LER-1982-01927 May 1982
05000364/LER-1982-01727 May 1982
05000364/LER-1982-016, Forwards LER 82-016/03L-028 April 1982
05000364/LER-1982-013, Forwards LER 82-013/03L-06 April 1982
05000364/LER-1982-007, Forwards LER 82-007/03L-016 February 1982