05000364/LER-2015-002
01-08-2016 | On November 12, 2015 at approximately 02:00 CDT, Farley Unit 2 was operating in Mode 5 at zero percent power in a planned maintenance outage when evidence from troubleshooting became available which led to the discovery that all of the Reactor Coolant System (RCS) Leakage Detection Instrumentation had been inoperable on August 7, 2015 for a period longer than allowed by Technical Specifications (TS).
Troubleshooting discovered that the A, B, and D channels of the Containment Cooling Level Monitoring System (CCLMS) had been inoperable since July 6, 2015. On August 7, 2015 the C CCLMS was tagged out at the same time as both the R11 and R12 Containment Radiation Detectors were taken out of service for a period longer than allowed by TS 3.4.15 Condition E and Limiting Condition for Operation (LCO) 3.0.3. This is a condition prohibited by Technical Specifications and is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(B). The cause of this event was an incorrect conclusion regarding the operating conditions of the four Containment Cooler Level Indicators. Corrective actions included the repair of the containment coolers' sensing lines for full restoration of the CCLMS. Repairs were also made to the components associated with the steam leak in containment N`RC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (It sots 19.."'.‘ I ) / LICENSEE EVENT REPORT (LER) APPROVED BY ()MD: NO. 3150.0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and led back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Inform lion Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission. Washington DC 20555-0001, or by infernal e-mail to Infocollects.ResourceOnrc.gov, and to the Dal( Officer, Olice of Inlormalion and Regulatory Affairs, NEOB-10202. (3150-0104). Oka 01 Management and Budget. Washington, DC 20503.11 a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required lo respond to, the information collection. Joseph M. Farley Nuclear Plant, Unit 2 05000 - 364 ContentsNOA. REQUIREMENT FOR REPORTFor a period of seven hours and 54 minutes on August 7, 2015 all required Reactor Coolant System Leakage Detection Instrumentation monitors required by Technical Specifications (TS) 3.4.15 were out of service and the required action per TS 3.4.15 Condition E and Limiting Condition for Operation (LCO) 3.0.3 to place the unit in Mode 3 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> was not met. This is a condition prohibited by TS and is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(B). B. UNIT STATUS AT TIME OF EVENTUnit 2, Mode 1, 100 percent power C. DESCRIPTION OF EVENTOn November 12, 2015 at approximately 02:00 CDT, Farley Unit 2 was operating in Mode 5 at zero percent power and was in a planned maintenance outage to investigate a leak ins'de of conta nment. A troubleshooting effort was initiated to investigate numerous maintenance issues that had been occurring with the A, B, and D Containment Cooler Level Indicators (EIIS Code LI). The troubleshooting work revealed that the A, B, and D Containment Cooler Level Indicators were inoperable and were considered to have been inoperable since July 6, 2015, when drainage into the containment sump had exceeded one gallon per minute. During this time frame the plant conducted extensive investigations into the source of the leakage, including multiple containment walkdowns and observations, maintenance troubleshooting activities, and detailed chemistry sample results of the containment sump, all of which led to the conclusion of a Service Water leak from the C Containment Cooler. The plant also prepared for a maintenance outage in the event that the leakage approached shutdown thresholds and implemented measures to protect the plant from the consequences of increased leakage. During the November 2015 maintenance outage a steam leak was found in Containment and was verified as the cause of the Containment Cooling Level Monitoring System (CCLMS) alarms. The A, B, and D containment coolers' sensing lines were found to be clogged and therefore the level transmitters were unable to perform their function. A subsequent review of operator logs showed that on August 7, 2015 the B and C Containment Cooler Level Indicators were declared inoperable to perform troubleshooting. On the same day, containment radiation monitors R11 and R12 were taken out of service for calibration surveillance. Since A and D CCLMS were discovered to have been inoperable, this created an unrealized entry into Tech Spec 3.4.15 Condition E (all detection inoperable) for a period of seven hours and 54 minutes, and the required action of immediate entry into Limiting Condition for Operation (LCO) 3.0.3 requiring the plant to be in MODE 3 in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> was not met. The CCLMS and the steam leak were repaired prior to exiting the maintenance outage. Reported lessons learned are incorporated into the licensing process and led back to Industry Send comments regarcing burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to Infocollects.ResourceOnrc.gov, and to the Desk Officer, Office ot Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. II a means used to impose an irdormation collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond lo, the intonation collection. Joseph M. Farley Nuclear Plant, Unit 2 05000 - 364 NOD. CAUSE OF EVENTThe cause of the unrealized entry into Tech Spec 3.4.15 Condition E was an incorrect conclusion that the A, B, and D Containment Cooler Level Indicators, which had not been alarming, were operable, and that the C Containment Cooler Level Indicator was improperly alarming. This conclusion was reinforced by performance of multiple containment walkdowns and observations, maintenance troubleshooting activities, and detailed chemistry sample results of the containment sump that were strongly indicative of Service Water. E. SAFETY ASSESSMENTThe leak in containment migrated to the containment sump which was monitored by radiation detectors. The sump level was trended by a level monitoring indication. The site planned a maintenance outage to repair the leak. This condition had no significant effect on the health and safety of the public. The loss of all CCLMS, along with a planned removal from service of R11 and R12 for calibration, represented an unplanned entry into Tech Spec 3.4.15 Condition E. The Condition requires an immediate entry into LCO 3.0.3 and entry into Mode 3 in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. The August 7, 2015 event lasted 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> and 54 minutes which exceeded the 7 hour8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> time limit and therefore constitutes a condition that is reportable pursuant to 10CFR50.73 (a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications. F. CORRECTIVE ACTIONDuring the November 2015 planned maintenance outage repairs were completed on the containment coolers' sensing lines for full restoration of the CCLMS. Repairs were also made to the components associated with the steam leak in containment. G. ADDITIONAL INFORMATION1) Failed Components: Level Indicator [LI] 2) Previous Similar Events: A search did not reveal any similar reported events for Plant Farley. 3) Energy Industry Identification System Code: Containment Leakage Control System [BD] 4) Other systems affected: There were no other systems, structures, or components that were affected by or contributed to the event. 5) Commitment Information: This report does not create any licensing commitments. |
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Joseph M. Farley Nuclear Plant | |
Event date: | 08-07-2015 |
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Report date: | 01-08-2016 |
Reporting criterion: | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
3642015002R00 - NRC Website | |
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