Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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- _ _ _____________________________ _ _ . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-311 Unit Name Salem # 2 Date May 10, 1983 Completed by L. K. Miller Telephone 609-935-6000 Extension 4455 Month April 1983 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 16 r 2 0 . ~i 3 0 18 0 4 0 19 0 5 0 20 0 _
6 0 21 0 7 0 22 0 8 0 23 0 9 0 24 0 10 0 25 0 11 0 26 0 12 0 27 0 13 0 28 0 14 0 29 0 15 0 30 0 31 0 Pg. 8,1-7 R1 8305170147 830510 PDR ADOCK 05000311 R PDR Page 2 of 12
OPERATINGDATkREPORT Docket No. 50-311 Date May 10, 1983 Telephone 935-6000 Completed by L. K. Miller Extension 4455 Operating Status
- 1. Unit Name Salem No. 2 Notes
- 2. Reporting Period April. 1983
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating (Gross MWe) 1162
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity (Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
- 9. Power Level to Which Restricted, if any (Net MWe) 0
- 10. Reasons for Restrictions, if any REFUELING OUTAGE This Month Year to Date Cumulative
- 11. Hours in Reporting Period 719 2879 13585
- 12. No. of Hrs. Reactor was Critical _ 0 470.3 10925.9
- 13. Reactor Reserve Shutdown Hrs. 0 3.3 38.9
- 14. Hours Generator On-Line 0 459.4 10796.6
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated
(;MWH) 0 1109383.2 31625932.2
- 17. Gross Elec. Energy Generated (MWH) 0 257340 10273590
- 18. Net Elec. Energy Generated (MWH) (2491) 229278 9802925
- 19. Unit Service Factor 0 16.0 79.5
- 20. Unit Availability Factor 0 16.0 "I 79.5
- 21. Unit Capacity Factor (using MDC Net) 0 7.2 65.2
- 22. Unit Capacity Factor (using DER Net) 0 7.1 64.7
- 23. Unit Forced Outage Rate 0 8.6 3.5
- 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
N/A
- 25. If shutdown at end of Report Period, Estimated Date of Startup:
June 14,1983
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved Initial Criticality 6/30/80 8/2/80 Initial Electricity 9/1/80 6/3/81 Commercial Operation 9/24/81 10/13/81 8-1-7.R2 Page 3 of 12 yr- --s -
UNIT SHUTDOWN AND POWER REDUCTIONS Docket No. 50-311 REPORT MONTH April 1983 Unit Name Salem No.2 Date May 10, 1983 Completed by L.K. Miller Telephone 609-935-6000 .
Extension 4455 Method of Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to 1 2 Reactor Report Code 4 Code 5 Prevent Recurrence Generator Maj Overhaul 83-046 1/21 S 2377.6 C 4 ---
HA GENERA (Gen Overhaul items)
Major Turbine Overhaul 83-046 1/21 S 2377.6 C 4 ---
HA TURBIN (Gen Overhaul items)
Misc Major 83-046 1/21 S 2377.6 C 4 ---
HC HTEXCH Condenser Overhaul Nuclear Normal 83-046 1/21 S 2377.6 C 4 ---
CA FUELXX Refueling 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salem as S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- Source C-Re fueling 3-Automatic Scram, tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)
Page 4 of 12
MAJOR PLANT MODIFICATIONS C W NO3 50-311
. REPORT MONTH APRIL 1983 .
TNM: Salem 2 DATES May 10, 1983 .
COMPLETED BY: L. K. Miller TELEPHONE: 609/935-6000 X4455
- DCR NO. PRINCIPLE SYSTEM SUBJECT 2EC-1214A CVC Replace the existing balance drum lock-nut on the centrifugal charging / safety injection pumps (21 & 22),
2EC-1400 4kV AC Power System Modify short circuit bracing on the 4kV vertical lift metal clad switchgear equipment, buses 2A, 2B, 2C, 2E, 2F, 2G and 2H.
2 EC--1441 Cranes and Holst Redesign overhead (monorail) handling systems for 4,500 lb. capacity of aux.
feedwater motor driven pump motor.
2SC-0908 Containment Airlocks Modify containment airlocks for Unit #2 with Chicago Bridge and Iron supervision to be the same as Unit #1.
- DESIGN CHANGE REQUEST 8-1-7.R1 Page 5 of 12
MAJOR PLANT MODIFICATIONS DOCKET NO. : 50-311 REPORT MONTH APRIL UNIT NAMI:- Salem 2 DATE: May 10, 1983 COMPLETED BY: L.K. Miller TELEPHONE: 609/935-6000 X4455
- DCR NO. 10CFRSO.59 SAFETY EVALUATION 2EC-1214A These changes decrease the probability of shaft failure and increase the margin of safety involved. No unreviewed safety or environmental questions are involved.
2EC-1400 This change increases the bracing of the 4KV group and vital busses. No unreviewed safety or environmental questions are involved.
2EC-1441 The added connections are designed to fulfill the required capacity of the overhead handling systems. No unreviewed safety or environmental questions are involved.
2SC-0908 No change in design or parts or operation of the air locks will take place. No unreviewed safety or environmental questions are involved.
Page 6 of 12
SALEM UNIT 2 WO NO DEPT UNIT EQUIPMENT IDENTIFICATION -
901001 M 2 VALVE, 2CV185 FAILURE DESCRIPTION: VALVE LEAKING FROM BODY / BONNET AREA APPROXIMATELY 1/2 GPM WHEN IN SERVICE. 820730 CORRECTIVE ACTION: INSTALLED NEW VALVE DIAPHRAM. 820809 907345 M 2 26 SERVICE WATER PUMP STRAINER FAILURE DESCRIPTION: STRAINER TRANSFORMER SMOKING. 820917 CORRECTIVE ACTION: REPLACED TRANSFORMER. 820917 908727 M 2 VALVE, 21SW223 FAILURE DESCRIPTION: DISASSEMBLE, INSPECT, REPAIR AS NECESSARY. 820914 "
CORRECTIVE ACTION: REMOVED TUBE BUNDLE AND REINSTALLED VALVE. TUBE BUNDLE ,
WILL BE REINSTALLED UNDER WO# 924574 WHEN PARTS AVAILABLE.
830305 908728 M 2 VALVE, 22SW223 FAILURE DESCRIPTION: DISASSEMBLE, INSPECT, REPAIR AS NECESSARY. 820914 CORRECTIVE ACTION: REMOVED DAMAGED TUBE BUNDLE AND REINSTALLED VALVE. TUBE BUNDLE WILL BE REPLACED UNDER WO# 924575 WHEN PARTS AVAILABLE. 830310 908729 M 2 VALVE, 23SW223 FAILURE DESCRIPTION: DISASSEMBLE, INSPECT, REPAIR AS NECESSARY. 820914 CORRECTIVE ACTION: REMOVED DAMAGED TUBE BUNDLE AND REINSTALLED VALVE. TUBE l
BUNDLE WILL BE REPLACED ON WO# 984576 WHEN PARTS l
AVAILABLE. G20330 Page 7 of 12 1
SALEM UMIT 2 WO NO DEPT UNIT EQUIPMENT IDENTIFICATION 909841 M 2 22 CHARGING PUMP FAILURE DESCRIPTION: REPLACE 22 CHARGING PUMP LUBE OIL COOLER. 821122 CORRECTIVE ACTION: REPLACED COOLER. 830324 909842 M 2 21 SAFETY INJECTION PUMP FAILURE DESCRIPTION: REPLACE PUMP LUBE OIL COOLER. 821122 CORRECTIVE ACTION: REPLACED COOLER. 830325 909843 M 2 22 SAFETY INJECTION PUMP FAILURE DESCRIPTION: PEPLACE PUMP LUBE OIL COOLER. 821122 C
CORRECTIVE ACTION: REPLACED COOLER. 830404 910076 , M 2 VALVE, 2CV50 FAILURE DESCRIPTION: REPAIR VALVE SEAT. 821215 CORRECTIVE ACTION: REPLACED VALVE IAW DCP 2EC-1560 PKG 1 PEV 3 ODCN M6/O.
821219 923033 M 2 21 CHILLER CONDENSER FAILURE DESCRIPTION: PLUG BLOWN OUT OF CONDENSER. 830309 CORRECTIVE ACTION: INTERNAL THREADS OK. FOLLOWED ENGINEERING ADVICE TO USE 316 STAINLESS PIPE PLUG REPLACEMENT.
925245 M 2 EL 100 CONTAINMENT AIR LOCK FAILURE DESCRIPTION: OUTER DOOR STUCK OPEN 4 INCHES AND INOPERABLE. 830226 CORRECTIVE ACTION: REALIGNED DOOR AND REPLACED CAMSHAFT FOLLOWER ROLLER Page 8 of 12
_ ._ __ _ _ - - _ _ _ - _ _ _-_ _ - .._~_ _ _ _ _ . _ - . _ - -. _ . . . _ . - _ _ _ . . _ . _ - _ . ._ ~ . ._
\
SRLEM UNIT 2
!, WO NO DEPT UNIT EQUIPMENT IDENTIFICATION .
l /
J 925248 M 2 2B VITAL BUS INFEED BREAKER FAILURE DESCRIPTIUN: INFEED. BREAKER 22BSD TRIPPED OPEN WITH '
NO FLAGS INDICATION. ,
i 3
CORRECTIVE ACTION: CONTROL CIRCUIT CHECK FOR SHORTS OR TRIP PERMISSIVE SAT. t FOUND BLOWN FUSE CAUSING TRIP CONDITION VIA 27X-22 RELAY.
~
]l '
925493 M 2 VALVE, 2SJ79 q
FAILURE DESCRIPTION: VALVE WILL NOT MOVE. 830130 I CORREC'TIVE ACTION:
REPLACED SEAT AND STEM PLUG ASSEMBLY, GASKETS AND PACKING.
830217 1 -
l 927478 M 2 EL l'00 CONTAINMENT AIR LOCK 1
FAILURE DESCRIPTION: DOOR WON'T OPEN. 830226 -
- CORRECTIVE ACTION
- ADJUSTED DOOR. 830226 4 i i
928635 M 2 VALVE, 2MS132 l FAILURE DESCRIPTION: VALVE IS LEAKING BY SEAT. 830108 -
CORRECTIVE ACTION: DISASSEMBLED, CLEANED, RESTELLITED DISC AND CAGE. BLUE CHECK 100%. 830222.
l 991853 M 2 VALVE, 22GB9 :
FAILURE DESCRIPTION: VALVE LEAKING BADLY. 820520 t l
I CORRECTIVE ACTION: LAPPED DISC AND SEAT. MACHINED GASKET SEATING SURFACE. I
! INSPECTED AND CLEANED BONNET. 830225 t
l
! Page 9 of 12 t 1
l l
l
_ = _ _ .- - __ ..
^
x .:.
1 SALEM UNIT 2
- WO NO '
DEPT UNIT. EQUIPMENT IDENTIFICATION _.
919714 P 2; 22 S/G STEAM FLOW CH 1 FAILURE DESCRIPTION: . CALIBRATE. 830219 CORRECTIVE ACTION: REPLACED MULTIPLIER / DIVIDER 2FM-522B 919999 P 2 RMS, 2R31 FAILURE DESCRIPTION: .CH[gNEL IN NO SCAN. 830209 CORRECTIVE ACTION: REPLACED OPTO-COUPLER IN LOOPS 1&2 RECEIVER. INSTALLED JUMPER ON CHANNEL.ID SWITCH TO ENABLE LOOP 1. BENCH CHECK SAT.
- 923049 P 2 VALVE, 21MS10 ATMOS RELIEF FAILURE. DESCRIPTION: . VALVE WILL NOT OPERATE. BLOWING AIR OUT OF CONTROLLER.
830313 ,
~ CORRECTIVE ACTION: REPLACED POSITIONER PILOT GASKET. 830314 4
930649 P 2 24 S/G PRESSURE CH 1 FAILURE DESCRIPTION: CHANNEL READING 40-60 PSI LOW. 821208 CORRECTIVE ACTION: REPLACED CAPACITORS C2, 3, 4, 6& 7. 821208 :
i Page 10 of 12
B SALEM UNIT 2 OPERATIONS
SUMMARY
REPORT APRIL 1983 The First Refueling Outage of Salem Unit No. 2 commenced on January 21st, 1983, and has continued through the month of April.
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REFUELING INFORMATION DOCKET NO.: 50-311 COMPLETED BY: L.K. Miller UNIT NAME: Salem 2 DATE: May 10, 1983 TELEPHONE: 609/935-6000 EXTENSION: 4455 Month May 1983
- 1. Refueling information has changed from last month:
YES X NO
- 2. Scheduled date for next refueling: March 31, 1984
- 3. Scheduled date for restar' following refueling: June 10, 1984
- 4. A) Will Technical Specification changes or other license amendments be required?
YES NO NOT DETERMINED TO DATE 5/1/83 B) Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES NO X If no, when is it scheduled? February 1984
- 5. Scheduled date (s) for submitting proposed licensing action:
March 1984 (if required)
- 6. Important licensing considerations associated with refueling:
NONE
- 7. Number of Fuel Assemblies:
A) Incore 193 B) In Spent Fuel Storage 72
- 8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170
- 9. Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity: March 2000 8-1-7.R4 Page 12 of 12 l