05000364/LER-2004-003, Regarding Technical Specification 3.0.4 Violation Due to Turbine Driven Auxiliary Feedwater Pump Inoperable
| ML041600171 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 06/04/2004 |
| From: | Stinson L Southern Nuclear Operating Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| NL-04-0952 LER 04-003-00 | |
| Download: ML041600171 (5) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(ix)(A) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
| 3642004003R00 - NRC Website | |
text
L M. Stinson (Mike)
Vice President Southern Nuclear Operating Company, Inc.
40 Inverness Center Parkway Post Office Box 1295 Birmingham, Alabama 35201 Tel 205.992.5181 Fax 205.992.0341 June 4, 2004 Docket No.: 50-364 SOUTHERN A COMPANY Energy to Serve YourWorld' TM NL-04-0952 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report 2004-003-00 Technical Specification 3.0.4 Violation Due to Turbine Driven Auxiliary Feedwater Pump Inoperable Ladies and Gentlemen:
Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2004-003-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B).
This letter contains no NRC commitments. If you have any questions, please advise.
Sincerely, L.M. Stinson LMS/WAS/sdl Enclosure: Licensee Event Report 2004-003-00 cc:
Southern Nuclear Operating Company Mr. J. B. Beasley, Jr., Executive Vice President Mr. D. E. Grissette, General Manager - Plant Farley RTYPE: CFA04.054; LC# 14048 U. S. Nuclear Repulatory Commission Dr. W. D. Travers, Regional Administrator Mr. S. E. Peters, NRR Project Manager - Farley Mr. C. A. Patterson, Senior Resident Inspector-Farley CL, ),
- L
NR OM36US ULA EUAOY APPROVED BY OMB NO. 3150-0104 EXPIRES 7431.2004 NRC FORM 366 U.S. NUCLEAR REGULATORY
, the NRC may not conduct or sponsor, and a digits/characters or each block) person Is not required to respond to. the Information collection.
FACIULTY NAME (1)
DOCKET NUMBER (2)
T PAGE (3)
Joseph M. Farley Nuclear Plant - Unit 2 05000364 l
1 OF 4 TITLE(4) Technical Specification 3.0.4 Violation Due to Turbine Driven Auxiliary Feedwater Pump Inoperable EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
FACILITY NAME DOCKET NUMBER SEQUENTIAL REV MO DAY YEAR YEAR UENUMBER RNO MO DAY YEAR 04 09 2004 2004 003 00 06 04 2004 FACILITY NAME DOCKET NUMBER OPERATING THIS REPORT IS SUBMITTiED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) (11)
MODE (9) 20.2201 (b)
_ 20.2203(a)(3)(ii)
I 50.73(a)(2)(ii)(B) 50.73(a)(2)(ix)(A)
POWER 20.2201(d) 20.2203(a)(4) 150.73(a)(2)(iii) 50.73(a)(2)(x)
LEVEL (10) 00 20.2203(a)(1) 50.36(c)(1)(i)(A)
_50.73(a)(2)(iv)(A) 73.71 (a)(4) 20.2203(a)(2)(i) 50.36(c)(1)(ii)(A) 50.73(a)(2)(v)(A) 73.71 (a)(5) 20.2203(a)(2)(ii) 50.36(c)(2) 50.73(a)(2)(v)(B)
OTHER 20.2203(a)(2)(iii) 50.46(a)(3)(ii) 50.73(a)(2)(v)(C)
Specify in Abstract below or In
=
20.2203(a)(2)(iv)
= 50.73(a)(2)(i)(A)
= 50.73(a)(2)(v)(D)
(If more space is required, use additional copies of (if more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17)
The wiring for the TDAFWP speed control was returned to the required configuration and surveillance testing was performed which verified the operability of the TDAFWP.
The wiring configuration for this circuit will be reconciled between field wiring and plant drawings for both FNP units and applicable drawing change requests will be submitted by August 15, 2004.
Additional Information
The following LER has been submitted in the past two years concerning poor work practices, configuration control, or procedure adherence:
LER 2002-003-00, Unit 1, Condensate Storage Tank piping Missile Barrier not in place.
Coincident with this event, on April 9, 2004, at 1810, the 2A Motor Driven Auxiliary Feedwater Pump (MDAFWP) was also declared inoperable due to a tripped breaker for the pump room cooler fan. The fan breaker starter coil was found shorted and replaced. The fan motor was successfully started, and the MDAFWP LCO was cleared at 0610 on April 10, 2004. Technical Specification 3.7.5, Required Action C.2 for two inoperable AFW trains, requires that the unit be placed in Mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> if at least one AFW train is not returned to operable status. The MDAFWP was returned to service within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Therefore, the Completion Time of Required Action C.2 was not exceeded.