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LER-1978-020, /01T-0:on 780614,seven of Nine Control Rods in Group 3 Inadvertently Dropped Into Core,Causing Operation W/More than One Inoperable Rod.Caused by Shorted Diode in DC Hold Secondary Power Supply.Fuses & Diode Replaced |
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| 2891978020R01 - NRC Website |
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LICENSEE EVENT REPORT CONTROL R, LOCK; l l
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(PLEASE PRINT OR TYPE ALL F ff R ED IN FO RMATION)
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COCK ET NUMgER ud 63 EVENT DATE 14 75 REPCRT O ATE 80 EVENT OESCRIPTION AND PROB A8LE CCNSECUENCES h
] l On ik June 1973 'it 1006 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82783e-4 months <br />, seven of the nine centrol rods in cup 3 inadvertantlyl I I dropped into the ecre resulting in operatien with nere than ene inoperable red (as de-l
@ l fined in T.S. h.7.1.2) which is a violation of T.S. 3.5.2.2.a, anc' whiOh also violatest
] I the red index linits of T.S. 3.";.2.5.e.
During the transient which fclieved, the quadt.
9 l rant pcVer tilt li=it of T.S. 3.5.2.h.a was exceeded but "as returned to an acceptablet
] [ value within fOur hcurs. Power was reduced to kO5 i=nediately and the centrol red l
gl 1sy=setry was cleared within one hour with a shutdown nargin greater than 15 Ak/k.
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':h cause for the dropped rods was a shorteddicde in the DC Hold Secondary Pcver Sup-l g l ply.
The shorted diede and resulting blevn fases caused icv voltage frem the Secen&/;
Supply. When the trip breakers for the Main Supply were trip tested during RPS sur-3
- veillanca, the rods dropped because of the insufficient vcitage. 31cvn fuses and failed dicde vere replaced and the output wave ferns checked.
gj a 9 90 p AciLITY METHCD OF STATUS
% PCWER OTHER STATUS OISCOVERY DISCOVERY OESC41PTICN 34
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] SSUEO@l DESCRIPTION 8
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D. G. Mitchell (215) 929-3601 Ext. 169 ?
NAME CF PREPARER PHONE:
3 7910258[OY
t LER #78-20
- 10 Event Descriptien and Probable Consequences Cent.
2.ere existed no threat to the health and safety of the public since =cre than the required shutdeva nargin existed during the occurrence.
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Attach =ent GQL 113h s
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AT"ACEEC "V LZ?. ~8-20 Cn l!. June 1978 at 1006 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82783e-4 months <br />, seven of the nine control reds in grcup 3 inadvertantly dropped into the cere. An F.PS surveillance was being perfer=ed at the ti=e which required manually tripping the trip breakers fer the DC Ecid Main Power Supply. The remaining DC Ecid Secendary ?cver Supply vill nor= ally held the reds, hcVever, the secccdary voltage was not sufficient to keep the reds latches because a shorted dicde resulted in blevn fases.
The unit var at 100T F.P. at the ti=e of the red drep. ?cver was r~duced i==ediately to h0% F.P.
While plant conditiens vere being stabilized, core power distributions and other core physics data vere being analyzed. Frc= the Technical Specifications it was determined that cperation with =cre than ene inoperable red is not per=itted, and an crderly pcver reductica vas begun.
Meanwhile, the two reds which had net drcpped vere scved in and the reds which had dropped vere successfully latched. Within ene hcur after the reds had dropped, all nine rods in the group vere aligned thus clearing the asy=:etric red alarms. Within the next twenty =inutes the grcup 3 reds vere all loci vithdrawn.
Having returned the centrol reds to an acceptable configuration, the unit power reducticn was stopped with reactor power at apprcxi=ately 30% F.P.
With ecndi-tiens stable, pcVer escalation began.
The present Unit 1 Technical Specifications does not define the time limit for shutting devn in this event. It has been noted that Standard Technical Specificatiens requires shutdevn within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. In the interi= until STS is i=plemented on Unit 1, Unit 2 Technical Specifications vill be used for guidance when an LCO is being viciated and no specific guidance is given in the Unit 1 Technical Specificaticas. Cperations Depar*=ent supervisien vill be familf arized with the reed to refer to Unit 2 Technical Specificaticus for additicnal guidance when required.
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| 05000320/LER-1978-001-03, /03L-0 on 780208:reactor Bldg Purge Supply Fans & Associated Purge Recirculation Damper Sys Were Inoperable. Caused by Incomplete Const | /03L-0 on 780208:reactor Bldg Purge Supply Fans & Associated Purge Recirculation Damper Sys Were Inoperable. Caused by Incomplete Const | | | 05000320/LER-1978-001, Forwards LER 78-001/03L-0 | Forwards LER 78-001/03L-0 | | | 05000312/LER-1978-001-01, /01T-0:on 780320,non-nuclear Instrumentation Dc Power Short Resulted in Reactor Trip & RCS Cooldown in Excess of Tech Spec Figure 3.1.2-2 Limits.Caused by Operator Changing Lightbulb.Conditions Imposed for Return to Power | /01T-0:on 780320,non-nuclear Instrumentation Dc Power Short Resulted in Reactor Trip & RCS Cooldown in Excess of Tech Spec Figure 3.1.2-2 Limits.Caused by Operator Changing Lightbulb.Conditions Imposed for Return to Power | | | 05000289/LER-1978-001-01, /01T-0:on 780106,B&W Informed Util That During Certain Plant Transients,Difference Between Reactor Power as Indicated by out-of-core Instrumentation & as Calculated by Heat Balance May Exceed 4% of Full Power | /01T-0:on 780106,B&W Informed Util That During Certain Plant Transients,Difference Between Reactor Power as Indicated by out-of-core Instrumentation & as Calculated by Heat Balance May Exceed 4% of Full Power | | | 05000289/LER-1978-001, Forwards LER 78-001/01T-0 | Forwards LER 78-001/01T-0 | | | 05000320/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000320/LER-1978-002-03, /03L-0 on 780208:prior to Initial Refueling,Defect Found in Plate 6 of Seismic Instrumentation Triaxial Response Spectrum Recorder 714.Caused by Mfg Error | /03L-0 on 780208:prior to Initial Refueling,Defect Found in Plate 6 of Seismic Instrumentation Triaxial Response Spectrum Recorder 714.Caused by Mfg Error | | | 05000289/LER-1978-002-01, /01T-0:on 780112,valve FS-V156 Closed to Modify Sprinkler Sys Piping to B Emergency Diesel Radiator Room & Continuous Fire Watch Not Established for 24-h.Caused by Personnel Error.Fire Protection Tech Specs to Be Reviewed | /01T-0:on 780112,valve FS-V156 Closed to Modify Sprinkler Sys Piping to B Emergency Diesel Radiator Room & Continuous Fire Watch Not Established for 24-h.Caused by Personnel Error.Fire Protection Tech Specs to Be Reviewed | | | 05000289/LER-1978-002, Forwards LER 78-002/01T-0 | Forwards LER 78-002/01T-0 | | | 05000320/LER-1978-003, Forwards LER 78-003/01T-0 | Forwards LER 78-003/01T-0 | | | 05000320/LER-1978-003-01, /01T-0 on 780213:while in Mode 6,continuous Fire Watch Not Established When Cable Room Halon Sys Automatic Actuation Sys Was Inoperable.Caused by Misunderstanding | /01T-0 on 780213:while in Mode 6,continuous Fire Watch Not Established When Cable Room Halon Sys Automatic Actuation Sys Was Inoperable.Caused by Misunderstanding | | | 05000289/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000289/LER-1978-003-03, /03L-0:on 780112,emergency Diesel Generator 1B Failed to Start on Simulated Test Signal During Procedure SP1305-5.2.Caused by Drifting Oil Pressure Limit Switch. Setting Adjusted,New Limit Switch Ordered | /03L-0:on 780112,emergency Diesel Generator 1B Failed to Start on Simulated Test Signal During Procedure SP1305-5.2.Caused by Drifting Oil Pressure Limit Switch. Setting Adjusted,New Limit Switch Ordered | | | 05000320/LER-1978-004, Forwards LER 78-004/01T-0 | Forwards LER 78-004/01T-0 | | | 05000320/LER-1978-004-01, /01T-0:on 780214,after Initial Fueling,Two Fuel Assemblies Were Loaded Into Reactor Vessel W/O Having Source Range Audible Counts in Containment Bldg | /01T-0:on 780214,after Initial Fueling,Two Fuel Assemblies Were Loaded Into Reactor Vessel W/O Having Source Range Audible Counts in Containment Bldg | | | 05000289/LER-1978-004-03, /03L-0:on 780117,while Closing Valve MU-V74A,22 Gallon Per Minute Packing Gland Leak Developed.Caused by Worn Packing in Valve.Valve Placed on Backseat.Packing Replaced 780118 | /03L-0:on 780117,while Closing Valve MU-V74A,22 Gallon Per Minute Packing Gland Leak Developed.Caused by Worn Packing in Valve.Valve Placed on Backseat.Packing Replaced 780118 | | | 05000289/LER-1978-004, Forwards LER 78-004/03L-0 | Forwards LER 78-004/03L-0 | | | 05000320/LER-1978-005-99, /99T-0 on 780208:during Surveillance of Dike,Noted That Area of Rock rip-rap Had Slid 15 Feet Down Slope.Caused by Ratio of incline.Rip-rap Repositioned | /99T-0 on 780208:during Surveillance of Dike,Noted That Area of Rock rip-rap Had Slid 15 Feet Down Slope.Caused by Ratio of incline.Rip-rap Repositioned | | | 05000320/LER-1978-005, Forwards LER 78-05l/01T | Forwards LER 78-05l/01T | | | 05000289/LER-1978-005-01, /01T-0:on 780119,Plant Operation Review Committee Found Containment Integrity Violated by Opening Valves BS-V47A & B During Pump Operability Test.Caused by Error in Operating Procedure OP 1104-5.Procedure to Be Revised | /01T-0:on 780119,Plant Operation Review Committee Found Containment Integrity Violated by Opening Valves BS-V47A & B During Pump Operability Test.Caused by Error in Operating Procedure OP 1104-5.Procedure to Be Revised | | | 05000289/LER-1978-005, Forwards LER 78-005/01T-0 | Forwards LER 78-005/01T-0 | | | 05000320/LER-1978-006-01, /01T-0 on 780217:core Alterations Made When Containment Integrity Had Been Broken & During Break in Communications W/Control Room | /01T-0 on 780217:core Alterations Made When Containment Integrity Had Been Broken & During Break in Communications W/Control Room | | | 05000320/LER-1978-006, Forwards LER 78-006/01T-0 | Forwards LER 78-006/01T-0 | | | 05000289/LER-1978-006-03, /03L-0:on 780124,during Normal Operation,Reactor Coolant Sample Isolation Valve CA-V13 Failed to Close When Actuated by Remote Signal.Caused by Valve Stem Thread Wear. Containment Isolation Valve CA-V2 Closed | /03L-0:on 780124,during Normal Operation,Reactor Coolant Sample Isolation Valve CA-V13 Failed to Close When Actuated by Remote Signal.Caused by Valve Stem Thread Wear. Containment Isolation Valve CA-V2 Closed | | | 05000289/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000320/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000320/LER-1978-007-03, /03L-0 on 780216:diesel Generator DF-X-1B Tripped. Caused by Spurious Actuation of Reverse Power Relay.Relay Reset & Surveillance Test on Diesel Generator Rerun | /03L-0 on 780216:diesel Generator DF-X-1B Tripped. Caused by Spurious Actuation of Reverse Power Relay.Relay Reset & Surveillance Test on Diesel Generator Rerun | | | 05000289/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000289/LER-1978-007-03, /03L-0:on 780128,while at 50% of Full Power,Incore Quadrant Power Tilt Limit Exceeded.Transient Caused by Transient Power Operations & Maneuvering to all-rods-out Configuration.Xenon Burned Out & Tilt Returned to Limits | /03L-0:on 780128,while at 50% of Full Power,Incore Quadrant Power Tilt Limit Exceeded.Transient Caused by Transient Power Operations & Maneuvering to all-rods-out Configuration.Xenon Burned Out & Tilt Returned to Limits | | | 05000289/LER-1978-008, Forwards LER 78-008/01T-0 | Forwards LER 78-008/01T-0 | | | 05000289/LER-1978-008-01, /01T-0:on 780202,once-through Steam Generator Feedwater Nozzles Flooded During Operation Below 5% Full Power.Caused by Incorrect Procedure Due to Operating Inexperience.Shutdown & Cooldown Procedures Revised | /01T-0:on 780202,once-through Steam Generator Feedwater Nozzles Flooded During Operation Below 5% Full Power.Caused by Incorrect Procedure Due to Operating Inexperience.Shutdown & Cooldown Procedures Revised | | | 05000320/LER-1978-008-03, /03L-0 on 780224:during Final Turnover Insp Three Fire Penetration Seals Found Not Functional.Caused by Seals Being Breached During Const.Fire Watch Was Posted | /03L-0 on 780224:during Final Turnover Insp Three Fire Penetration Seals Found Not Functional.Caused by Seals Being Breached During Const.Fire Watch Was Posted | | | 05000320/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000289/LER-1978-009-03, /03L-0 on 780315:dc Breaker CB3 Failed to Trip on One of Several Tests.Caused by Apparent Binding of Breaker Operating Linkage.Binding May Have Been Due to Insufficient Exercise of Breaker &/Or Lack of Maint | /03L-0 on 780315:dc Breaker CB3 Failed to Trip on One of Several Tests.Caused by Apparent Binding of Breaker Operating Linkage.Binding May Have Been Due to Insufficient Exercise of Breaker &/Or Lack of Maint | | | 05000320/LER-1978-009-03, /03L-0 on 780302:surveillance Requirements Re Control Rod Drive Mechanism Not Met.Failed to Realize Specific Submode Had Been Entered | /03L-0 on 780302:surveillance Requirements Re Control Rod Drive Mechanism Not Met.Failed to Realize Specific Submode Had Been Entered | | | 05000320/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000289/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000320/LER-1978-010-03, /03L-0 on 780307:river Water Pump Outlet & Prelube Valves & Redundant RCP Seal Injection Valves Not Functionally Tested Before Being Placed in Svc | /03L-0 on 780307:river Water Pump Outlet & Prelube Valves & Redundant RCP Seal Injection Valves Not Functionally Tested Before Being Placed in Svc | | | 05000320/LER-1978-010, Forwards LER 78-010/03L-0 | Forwards LER 78-010/03L-0 | | | 05000289/LER-1978-010, Forwards LER 78-010/01T-0 | Forwards LER 78-010/01T-0 | | | 05000289/LER-1978-010-01, /01T-0:on 780318,during Emergency Sequence & Power Transfer test,1A & 1C Makeup Pumps Tripped When Transferring to Onsite Source Due to Malfunctioning Time Delay Relay & Diesel Generators Failed to Start Due to Pressure Swit | /01T-0:on 780318,during Emergency Sequence & Power Transfer test,1A & 1C Makeup Pumps Tripped When Transferring to Onsite Source Due to Malfunctioning Time Delay Relay & Diesel Generators Failed to Start Due to Pressure Switches | | | 05000289/LER-1978-011-03, /03L-0:on 780318,snubber MS-201 Found W/No Fluid in Reservoir.Caused by Pinched Rod Wiper Seal | /03L-0:on 780318,snubber MS-201 Found W/No Fluid in Reservoir.Caused by Pinched Rod Wiper Seal | | | 05000320/LER-1978-011-03, /03L-0 on 780311:entered Mode 4 W/O Establishing Containment Integrity & Surveillance on Bldg Door Not Performed.Door Failure Caused by Damaged O Ring Seals | /03L-0 on 780311:entered Mode 4 W/O Establishing Containment Integrity & Surveillance on Bldg Door Not Performed.Door Failure Caused by Damaged O Ring Seals | | | 05000320/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000289/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000320/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000289/LER-1978-012-03, /03L-0:on 780406,during Functional Tests,One Snubber DHH-187 Would Not Lock Up Upon Compression.Cause Undetermined.Valve Block Replaced & Satisfactory Test Made | /03L-0:on 780406,during Functional Tests,One Snubber DHH-187 Would Not Lock Up Upon Compression.Cause Undetermined.Valve Block Replaced & Satisfactory Test Made | | | 05000289/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000320/LER-1978-012-03, /03L-0:on 780314,Unit 2 Entered Mode 4 with Only One Operable Bldg Spray Sys.Caused by Clerical Error | /03L-0:on 780314,Unit 2 Entered Mode 4 with Only One Operable Bldg Spray Sys.Caused by Clerical Error | | | 05000289/LER-1978-013-01, /01T-0:on 780413,B&W Informed Util That Small Break on Reactor Coolant Pump Discharge Had Not Been Analyzed in Fsar.Procedures to Be Revised & Operators to Be Trained in Response to Small Break LOCA | /01T-0:on 780413,B&W Informed Util That Small Break on Reactor Coolant Pump Discharge Had Not Been Analyzed in Fsar.Procedures to Be Revised & Operators to Be Trained in Response to Small Break LOCA | |
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