LER-1980-006, /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2651980006R01 - NRC Website |
|
text
_ __ _ - - _ _ _ _ _ _ _ _ _ - -_____________
NRC FORM 366 U. S. NUCLE AR REGULATORY COMMISSloN (7 77)
~
LICENSEE EVENT REPORT
) CONTROL BLOCK: l l
l l
l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
%/
1 e
lo lil I i l L l Q l A l D l 2 l@l 0 l0 l 0 l-l 0l Ol Ol -l O l 0l0l@l4l1l1l1l1l@l l
l@
7 8 9 LICENSEE CODE to 15 LsCENSE NUMSER 2$
26 LICENSE TYPE JG S7 CAT 58 CON'T lOlil 3g y l L l@l 0 l 5 l 0 l 0 lo l 216 l5 l@l 01310 l 8 l 8 l 0 l@l 0 l 3 l 2 l 2 I 810 l@
7 8
60 61 00CKET NUVBER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PRO 8A8LE CONSEQUENCES h lo l2] i While performing a reactor vessel pressure test as part of the Inservice insnection i
10131 l program (T.S.4.6.F) a visual inspection of the primary coolant system piping revealed I
- o ;4; l some water drops on the "A" core spray injection piping, 1ine 2-1403-10"-A.
An ultra-l go;3, g sonic inspection of 100 percent of the core spray piping welds in the primary contain-l lO ls i l ment disclosed several crack indications located in the pipe to elbow welds between l
lO l 7 l l the reactor vessel and first manual isolation valve in both core spray loops.
l 10181l I
SYSTEM
CAUSE
CAUSE COYP.
VALVE CODE CODE SU8 CODE COMPONENT CODE SUSCODE SUSCODE 1019l l C l J l@ ]Q l Cl@ l P l1 l P lE lX lX [@ l 0l@ l Z l@
8 9
to 11 12 13 Id 19 20 S E QUE NTI A L OCCUR R E NCE REPORT REVISION LER RO EVENT YE AR REPORT NO.
CODE TYPE N O.
@ su l 8l 0l l_[
l 0l 0l 6l l/l l0 l1 l lTl l-l l0l aEP RT c
_ 21 22 2J 24 26 27 28 M
30 Jt 32 T
N A ON ON PLA T M
HOURS 22 58 IT E FO 4 B.
SUPPLI MA F ACTI.,RE R l A [gl34 Flg lJS Zlg l36Z l@l0l0l0l0l y@
lY l@
lN l@
l0 l l l 0 l 5 l@
JJ J/
40 4*
42 43 44 4F CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 11 101 l The cause of the crack indications has not been determined.
The cause will be l
gl determined following a laboratory failure analysis on the subject pieces of pinino.
I
,, l The final results of the laboratory metallurgical analysis will be reported to the l
g3g l The affected sections of pipe on both loops will be replaced with carbon steel l
NRC.
g piping.
l 7
J 9 80 STA S
% POWER OTHER STATUS IS O RY DISCOVERY DESCRIPTION y l H l@ l0 l 0 l0 l@l NA l
lBl@l Routine Test l
's2Tlvt TY COkTENT AMOUNT OF ACTIVITY @ l riTs 1 l Z l @D OF RELEASE l Zl@l RELEASE LOCATION OP RELEASE NA l
NA l
7 8 9 10 tt 44 45 80 PERSONNEL EXPOSURES NuveER TYPE
DESCRIPTION
fiTTI I O l o l O l@l z l@l NA l
PERScNNa',N2u'!,ES oESCRiPriON@
NUMBER m l 010 l 0 l@l NA l
7 8 9 11 12 80 LOSS OF CR OAMAGE TO FACILtTV TYPE
DESCRIPTION
g l Z l@l NA l
7 8 9 to 80 ISSUE
DESCRIPTION
L2_L2]Lgf81 na i
i i l l l l i i 11 ! ! l$:
7 8 9 iO D O O4()ZO 3 5 5 D. Clark PHON E: 109-M4-2 241 Ex.
170 g
NAVE OF PREPARER
l.
LER NUMBER:
LER/R0 80-06/0lT-0 11.
LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station Ill.
FACILITY NAME: Unit Two IV.
DOCKET NUMBER: 050-265 V.
EVENT DESCRIPTION
On March 8,1980, during the Unit Two reactor vessel pressure test, a visual inspection of the primary coolant system piping revealed some water drops on the "A" core spray injection piping, line 2-1403-10"-A.
The reactor vessel pressure test was performed as part of the inservice inspection proar=~ to meet the surveillance requirements of Technical Specification 4.6.F.
A subsequent ul trasonic inspection of 100 percent of the core spray piping welds located in the primary containment was performed under the direct supervision of the Commonwealth Edison Company SNT-TC-1A Level til Examiner.
The inspection disclosed several crack indications in the welds in both core spray loops. The Indications were located in the pipe to elbow welds between the reactor vessel and the first manual isolation valve.
VI.
PROBABLE CONSEQUENCES OF TPE OCCURRENCE:
The reactor has been in the cold shutdown condition since November 25, 1979 for refueling. The crack indication was first noticed during the vessel pressure test which was required to be performed before the reactor could be returned to operation. No steam or water leakage was detected during the initial drywell entry while the reactor was in the process of being shutdown for the refueling outage. The core spray piping which is included in the primary coolant system boundary is inspected as part of the station inservice inspection program. Several special inspections have also been performed on the core spray piping, These inspections include the inspections required in R.O.Bulletin 75-01; an augmented inspection recommended in General Electric Service Information Letter #117; and a special inspection performed in January, 1978. The results of the inservice inspection and the special inspections have all been satisfactory. A list of welds which have been inspected, and weld maps are attached.
l l
i
Vll.
CAUSE
The cause of the crack indications has not been determined.
The cause will be determined following a laboratory failure analysis on the subject pieces of piping.
Two of the welds which were found to have crack indications were found satisfactory during the inservice inspection performed during the current outage. We can not specify the reason for missing the indications at that time. We can only speculate that it could have been the failure of the ultrasonic test equipment, f ailure to set-up and calibrate properly, or failure on the part of the testing operator.
The pipe was manufactured by United States Steel Corporation, and is type A-312, grade TP 304, schedule 80 seamless stainless steel pipe, heat number X25210.
The elbows were manufactured by Taylor Forge Corporation, type A403 grade L? 304, schedule 80 seamless steel elbows, heat number 251350Cq.
Vill.
CORRECTIVE ACTION' Several pieces of the existing core spray line will be cut out as shown in the attached sketches. The removed pieces of piping will be visually inspected by a Commonwealth Edison metallurgist following removal. Commonwealth Edison will send representative samples of the failed pipe to Argonne National Laboratory for failure analysis.
Representative samples will also be sent to Brookhaven National Laboratory for the NRC to conduct an analysis parallel to ou r own.
The final results of the laboratory metallurgical analysis will be reported to the NRC.
The repair of the core spray piping involves removing the affected sections of pipe on both loops. These sections will be replaced with carbon steel piping and fittings.
The existing stainlest, teel isolation valves will be retained in the piping sy r.em.
The replaced section will be welded approximately 15 inches from the nozzle safe-end. The heat input created during welding will have no affect on the safe-end.
The replacement carbon steel pipe is type SA-333, grade 6, schedule 80 seamless pipe. The fi ttings are type SA420, grade WPL-6, schedule 80 seamless elbows. The repair work will be performed under the requirements of ASME Boiler and Pressure Vessel Code Section XI.
The repair parts have been procured in accordance with ASME Boiler and Pressure Vessel Code Section lit, Class 1.
. ~.
1 The carbon steel pipe that will be installed in the core spray lines will be considered as a final fix for that particular section of piping. At this time, Commonwealth Edison does not know if the safe-end and the stainless steel piping between the safe-end and the carbon steel portion is a final fix.
The company will address this portion of pipe and evaluate the prospective alternatives to obtain a final fix pending the results of the metallurgical failure analysis.
As requested by the NRC, the safe-end to pipe weld as well as all dissimilar-metal welds made as part of the regair will be inspected for the next two refueling outages.
The inspections will be performed using current company approved ultrasonic test procedures. An ultrasonic inspection of the Unit One core spray piping located inside the primary containment will be done during the next refueling outage in the Fall,1980.
i
QUAD-C ITIES UtilT TWO CORE SPRAY PIPE flDE HISTORY wint. 78 ISI Weld No Fall 76 ISI Spec, insp.
Cracks Found
'A' Loop Type R.O. Bull. 75-01 SIL 117 Jan. 78 Fall 79 ISI tiarch, 1980 14A-Fi N-SE !
X X
l X
14A-F2 SE-P X
X X
14A-54 P-E X
X X
X 14A-S5 E-E X
X X
X 14A-56 l E-P X
14A-F8 j P-V X
X X
X 14A-F9 1 V-E X
X X
14A-S10 I E-P X
ikA-Sil l P-E X
14A-F12 ! E-V v.
14A-F13 i V-P IkA-Fl4 i P-P 14A-515 ' P-P X
14A-Sl6 i P-E X
X 14A-F17 I E-P X
'B' Loop l
148-51 l ti-SE X
X X
x 148-F2 i SF-P X
X X
14B-S4 P-E X
X X
X 148-S5 E-E X
X X
X X
14B-56 ; E-P X
X X
X 148-F8 P-V X
X 14B-F9 V-P X
X X
l 14B-510 P-E X
X l
14B-511 E-P X.
X 148-512 ' P-E X
X 140-Fl3 E-V X
X i
140-F14 V-P X
148-515 P-E X
X 148-Fl6 E-P X
X
L 6+1 y
m s-
',i i I)h l.
I t.
,i w
g..
sq l *.,'
ej
(.(l
/
O o
3
~
'u W
l A
r
') v1 g
ei
}
=
0 D
,+
~
b' r
et
+ m J
.E R
L.f y
h a.., ra
--*=a d
)
tt.
R c(
U".r 3
w b o
n V-C U
E
'r 3
us e
o w
~
N g
q d;
4f n
T J
N I.
n o
M c!
g ci o
s'.
fi m')
v>.
d O
g
,h d
Q, F* f o g
g
\\q c.
i e,
- - g (f) O Y
,d.
Y v.
c.!
l w
t-9 g
I m
y oc2
.o w
w t.
e e];
d 39
y s+,l o a e x
c u..
<J sa c
.t.,
0
- l O
'}
h")
i
]
C I
o q
w' e
r c.
d) 0 l}
~Ey
.to Cl.
I c.-
b'
. 8 1
i 5
w -r, t.
- - 3 c! '
t tu i
i--
e i
i M
J.
\\
- ~:
W'F O:5 e,a g, %
i s-
=
.4.
C e h
.l 4*
i to i)
{
y
'l
}
Z. pl
~
h
-}\\i tu, j
I
.. r u,
e-WU
.e_
r
'T e
%g y.1 l4 i
1 s
- 37 U
X 7
t D
=
I W() h4, 4
~'
'~
M gl.
I'
.. s I
u.:
U.'
t'-
.r>
d d
=%'
s0
cq a;
l-s%
i su e
c 9-M,
$z h
E p
1 o-l g$
'^
Y hs'?'
?
z w
b o.
c o
a ti 9
I M
4 3.1' J
21 c
4 e
m.
T 2;
o t
e-t
,o a-
- - n 4'E s
d b
i; 6
f.
r c.
l o
s t!
. ~l b!
NC c
5 C
'D C
1) tti y
\\-
D[s J*e) finWjy
D w
wus M.e
91 G
.n m
A
/rl
((\\)
k s
i1 1.
~
to M. E,\\ L V-i f
(;
/
e
(()
o e
c E
w Q
N - j. m h +
4 e
.i j
,\\
co s u't e :
't
.s tm
- - r S:~3 j!ry,
\\
~c
~~,
~
~~-
\\t.
9 'd {\\
c t
r co I
o-i, e i '-
CQ-j
,{l
.' \\ ll d
/
c4
/
4 m
o p
Te c
p
}1 dl cl al x
l ni ;
e n
g,s:i.ce.
o g
i c
3 I
'A g
,O
~
f;
.s p
,[ ;..,,
,71 y9 o-a
%g
- ~.
u sn O s
c,:
v h,E 5h
- - b'
)
M.,
N
[ $
dc7
.O s
c i
, g' s
i M
0 c,! 7 9
,.s tt, l
p e
t. l[.
to f O J d
\\
5
..j CQ' i.
2 d O O l
Ui vj 3-O
't,!
i
~,
.p s 5 N
P. 'I Si LO g
l
'O.
/
,,9
.f
~
s IO l
)
c.7 s'
a--
E f. 'i C'S j
l N
E I
I O
At h
'O c
c.
T.
o i
gi I
. 0 Is, m;
l o
i l. b v,,, fl
.(
j e.l 4
s e
e t
g
. :s, s
e i
n) s y
i 4
i ;ll i
1D l
.l e'.
cf.
2 l_
[i.p.I i
' g~j) f.. y-l 3
U
'l
+
4 i
aa i
r t
D D.c1
,W llI(
e t1 L
v
~
'I D;e
- - S l,
5Q
I w
e+
o a. -
N i;
a G tO si w
M ca G
e; cd T '
m 7.
2 m d
ni d ' s
G 1 CD.l
~~
O 2
l 6l t
,2 -
m T
d.
~~
o o
I b
9:
9 i
m s. c M.
9ll i
&.-i r
e%.
6 w
v.
m s
o Cp
,d r, A t
i Y
t t
V Aj
)
Ti C;
6'
"'SE.0 e-c-
i I
L.,,
e-e o
._ W w. I Nx
- - CI j u\\li j \\. :m i
'[)
fI f
e --
ft b
- ^ * * '
~~
l
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000265/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001-03, /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | | | 05000254/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000254/LER-1980-002-03, /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | | | 05000265/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000265/LER-1980-002-03, /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | | | 05000265/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000265/LER-1980-003-03, /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | | | 05000254/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000254/LER-1980-003-03, /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | | | 05000254/LER-1980-004-03, /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | | | 05000254/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004-03, /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | | | 05000265/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000265/LER-1980-005-03, /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | | | 05000254/LER-1980-005-03, /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | | | 05000254/LER-1980-006-03, /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | | | 05000254/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000265/LER-1980-006-01, /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | | | 05000265/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000254/LER-1980-007-03, /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | | | 05000254/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000265/LER-1980-007-03, /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | | | 05000265/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000254/LER-1980-008-03, /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | | | 05000265/LER-1980-008-03, /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | | | 05000265/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000254/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000265/LER-1980-009-03, /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | | | 05000265/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-009-03, /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | | | 05000254/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-010-03, /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | | | 05000254/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-010-03, /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | | | 05000265/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-011-03, /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | | | 05000265/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-011-03, /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | | | 05000254/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000265/LER-1980-012-03, /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | | | 05000254/LER-1980-012-03, /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | | | 05000265/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000254/LER-1980-013-03, /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | | | 05000265/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000254/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000265/LER-1980-013-03, /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | |
|