05000265/LER-1980-016-03, /03L-0:on 800723,discovered That Pressure Switch PS-2-261-30C Would Trip at 841 Psig,Under Limit of 850 Psig. Caused by Instrument Drift.Pressure Switch Recalibr & Tested Satisfactorily

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/03L-0:on 800723,discovered That Pressure Switch PS-2-261-30C Would Trip at 841 Psig,Under Limit of 850 Psig. Caused by Instrument Drift.Pressure Switch Recalibr & Tested Satisfactorily
ML19338C942
Person / Time
Site: Quad Cities 
Issue date: 08/11/1980
From: Kan S
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19338C934 List:
References
LER-80-016-03L-04, LER-80-16-3L-4, NUDOCS 8009080407
Download: ML19338C942 (1)


LER-1980-016, /03L-0:on 800723,discovered That Pressure Switch PS-2-261-30C Would Trip at 841 Psig,Under Limit of 850 Psig. Caused by Instrument Drift.Pressure Switch Recalibr & Tested Satisfactorily
Event date:
Report date:
2651980016R03 - NRC Website

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pRC FOSM 386 U. S. NUCLEAR REGULATORY COMMISSION

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LICENSEE EVENT REPORT

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60 St OOCKET NUM9ER 68 69 EVENT DATE 74 75 BEPORT OATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES O'o gl While performing Main Steam Line Low Pressure Isolation Surveillance, QlS-20,.

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