05000265/LER-1980-017-03, /03L-0:on 800724,during Testing,Pressure Switch PS-2-1622B Was Found to Actuate at 20.3 Rather than 13.8 Inches of Water.Caused by Setpoint Drift.Switch Replaced

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/03L-0:on 800724,during Testing,Pressure Switch PS-2-1622B Was Found to Actuate at 20.3 Rather than 13.8 Inches of Water.Caused by Setpoint Drift.Switch Replaced
ML19338C948
Person / Time
Site: Quad Cities 
Issue date: 08/12/1980
From: Steffes C
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19338C947 List:
References
LER-80-017-03L-05, LER-80-17-3L-5, NUDOCS 8009080417
Download: ML19338C948 (1)


LER-1980-017, /03L-0:on 800724,during Testing,Pressure Switch PS-2-1622B Was Found to Actuate at 20.3 Rather than 13.8 Inches of Water.Caused by Setpoint Drift.Switch Replaced
Event date:
Report date:
2651980017R03 - NRC Website

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43 OOCKET NUMSER 68 69 EVENT D ATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h lo I:I l While performing Torus to Reactor Building Vacuum Breaker Surveillance Test, qts-48, l Es i36l pressure switch PS-2-1622B was found to actuate at 20.3 inches of water. Technical l

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