05000333/LER-1981-031-03, /03L-0:on 810401,indicated Core Flow Appeared Higher than Expected.Possibly Caused by Error in Procedure That Sets Amplifier Gain Which Corrects Core Flow for Reverse Flow Through Idle Jet Pumps.Investigation Underway

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/03L-0:on 810401,indicated Core Flow Appeared Higher than Expected.Possibly Caused by Error in Procedure That Sets Amplifier Gain Which Corrects Core Flow for Reverse Flow Through Idle Jet Pumps.Investigation Underway
ML19343D626
Person / Time
Site: FitzPatrick 
Issue date: 05/01/1981
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343D624 List:
References
LER-81-031-03L, LER-81-31-3L, NUDOCS 8105050596
Download: ML19343D626 (1)


LER-1981-031, /03L-0:on 810401,indicated Core Flow Appeared Higher than Expected.Possibly Caused by Error in Procedure That Sets Amplifier Gain Which Corrects Core Flow for Reverse Flow Through Idle Jet Pumps.Investigation Underway
Event date:
Report date:
3331981031R03 - NRC Website

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U.S. NUCLEAR REGULATORY CoMMISSloN NRc FORM 366

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