05000298/LER-1980-023-04, /04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades

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/04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades
ML19344E101
Person / Time
Site: Cooper 
Issue date: 07/22/1980
From: Borer P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19344E093 List:
References
LER-80-023-04T, LER-80-23-4T, NUDOCS 8008260630
Download: ML19344E101 (1)


LER-1980-023, /04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades
Event date:
Report date:
2981980023R04 - NRC Website

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'NRC FOlfA 366 U. S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: l l

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8 60 61 OOCKET NukiER 68 69 EVENT OATE 74 75 REPORT OATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUhNCES h ITTT1 IDuring normal operation, condenser cooling water outlet temperature limit of I

10 i 3 i l1030F was exceeded. No effect on public health and safety. During the event an I

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