LER-1980-052, /03L-0:on 801208,RCS Dose Equivalent I-131 Exceeded Tech Spec Level.Caused by Leaking Fuel Pins & Anticipated Dose Equivalent Iodine Transient Following RCS Transient.Rcs Circulated Through Makeup & Purification Sys |
| Event date: |
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| Report date: |
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| 3021980052R03 - NRC Website |
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IVtNT OESCAs#tCN a.NC **Cs A3LI CONst:WENCIS
,,,jg At 0930 during Reactor shutdown it s discovered by Reactor Coolant System samplig
,,g, that the Dose Eq.uivalent I-131 exceeded 1.0 microcuries per gram. This created
,,,y, an event contrary to T. S. 3.4.8.
Redundancy N/A. There was no effect upon i o,,! I the health or safety of the general'public. This is the nineteenth occurrence io..it reported under this specification.
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,,,; The cause of this event is attr uted to leaking fuel pins and an anticipated Dose, Equivalent Iodine transient following a Reactor Coolant System transient. The t,,,jg w I Reactor Coolant System was recirculated through the Makeup & Purification System; i
,,,,, g Dose Equivalent I-131 returned to less than 1.0 microcuries per gram at 2230.
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SUPPLEMENTARY INFORMATION Riport No.:
50-302/80-052/03L-0 Facility:
Crystal River Unit #3 R: port Date:
5 January 1981 Occurrence Date:
December 8, 1980 Identification of Occurrence:
Primary Coolant Dose Equivalent I-131 was greater than 1.0 microcuries per gram contrary to Technical Specification 3.4.8.a.
Conditions Prior to Occurrence:
Mode 3 (hot standby 0%).
Description of Occurrence:
Between 2030 and 2330 on December 7, 1980 Reactor power was de-creased from P4% to 0% for maintenance. The Reactor Coolant System was sampled at 2334 and the Dose Equivalent I-131 was determined to be within specificaticn. At 0730 on December 8, 1980 the RCS was sampled to investicate a higher than usual Gross Beta radioactivity result and the Dose Equivaler.t I-131 was de-termined to be 1.45 microcuries per gram at 0930.
Designation of Apparent Cause:
The cause of this event is attributed to leaking fuel pins and an anticipated Dose Equivalent Iodine transient following the Reactor Coolant System transient of the previous night.
Analysis of Occurrence:
Redundancy N/A. There was no effect upon the health or safety of the general public.
Corrective Action
The Reactor Coolant System was recirculated through the Makeup and Purification System; Dose Equivalent I-131 was determined to be less than 1.0 microcurie per gram at 2230 December 8, 1980.
Failure Data:
This is the nineteenth occurrence reported under this specifica-tion.
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C' Reactor Power History of Prior forty-eighe Hours Item I L
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Evene Date:
12/8/80 l
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DATE 12, 6,80 L
5 HOUR GMWE TURD G NWTH NI RATIO RATIO
(
'F?!"'
'TS5A'
'+MM (P7 9-M- --N UM T
- FJNT
=/cFP 1
96.21 9901 96.94 99.10 1.022
.99?
2 96.23 9890 76r94 77.14 1."22
.V93
'- 1 3
96.28 9892 96.94 99.00 1.021
.993 1
4 96.25 9898 96.94 99.40 1.025
.993 5
96d5 7887 76-94
- 77. ?;0 1--O o '-
^^"
'E 6
96.25 9894 96.90 99.50 1.027
.993 M
7 96.27 9896 96.9F.
99.50 1.026 993 O
96.25 9697 77.02 79 r64 1.027
.992 h
9 94.77 9901 95.43 98.60 1.033
.993 N
10 95.06 9898 95.72 99.00 1.034
.993 "5
!?
95v82 9994
%G3 9MA 1.032
.or 12 96.00 9904 96.74 99.70 1.031
.992 IE 13 96.01 9904 96.78 99.80 1.031
.992 1 12 06.05 0800 06.74 oo 70 1 031 093 E
15 96.08 9897 96.78 99.60 1.029
.993 I
2' 16 96.09 9898 96.78 99.60 1.029
.993
'2 '
!?
96 !?
0395 94 79 CS.on 3 n37
.993
$2; 18 96,13 9893 96.78 99.90 1.032
.993
'E 19 96.08 9900 96.78 99.90 1.032
.993 i
I 5'
20 94,07 0900 06.02 1MJD 1.033 093 4
21 96.02 9902 96.74 100.00 1.034
.993 2
- 4 21 22 96.09 9892 96.70 99.90 1.033
.994
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l 23 o6E 9894 9 4,-7 4 09,90 1,033
.o93 24 96.00 9897 96.70 99.90 1.033
.993
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3 2
31 i E AVERAGE DAILY GENERATOR GROSS 821.02 MWH(E)
Pl 0 VE RAGE-D AIt,Y--THE RMAl,- POWER 2374 J2--NWHLTJ A
AVERAGE DAILY TURDINE GROSS HEAT. RATE 9898 BTU /KWH I 21 AVERAGE DAILY MWTH POWER 96.714 */*FP
'3' '
nVEEGE-DAILY-NUCLEAR--INST,-POWER 99,567- =AT-P-n l
3.1 RAT-TO-OF--NI-TO--NWTH - 1J30 o
7i 43#
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'DATE 12, 7,80 c
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1 HOUR GMWE TURB G MWTH NI RATIO RATIO i
'E710' (TSG4)
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HI-/NT MEJN-T 1
./=FP
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1 96.06 9892 96.70 100.10 1.035
.993 2
96 4 9839 96.66 14 h40 1.036
.?94 1
3 96.00 9894 96.66 100.00 1.035
.993 1
4 95.71 9890 96.29 99.60 1.034
.994 5
9M5 999" 96,29 99.60
.034
??3 2
6 95.43 9896 96.04 99.50 1.036
.994 I
E 7
92.26 9899 92.74 96.70 1.043
.995
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93.1-9 9023 93.94
? ?. 74) 1 r440
.992 9
95.91 9892 96.53 100.00 1.036
.994 10 95.93 9889 96.53 99.90 1.035
.994 of n1 969-1 9442 o?.30
? n07 o9" d'
12 96.09 9888 96.70 97.30 1.006
.994 I
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13 96.11 9890 96.70 97.20 1.005
.994 is tu 9A.no on9n 9/. 7n 07 3n 1_ nog equ 2
15 96.00 9900 96.70 97.20 1.005
.993 E
16 96.12 9889 96.74 97.20 1.005 994
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96 W 9No?
94,74 o'.30
? nO4
.9S" 18 96.13 9888 96.70 97.50 1.008
.994 f I.4
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19 96.05 9898 96.74 97.50 1.008
.993 24 gn rus 9393 og._vu o7 Sn i_gnn oo3 E
21 93.82 9882 94.21 95.50 1.014
.996 2
22 61.94 9975 61.05 66.30 1.086 1.015
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la 1o 2'-?0 1 ?75 902 2'
il 24 0.00 0
3.10 0.00 0.000 0.000 i(
297 2
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E AVERAGE DAILY GENERATOR GROSS 742.20 MWH(E)
D3 AVFR AGC-D AT4,Y-THE RM Al,-POWER 94 4 A54 4Wil4-T 1 AVERAGE DAILY TURDINE GROSS HEAT RATE 9072 BTU /UWil
'3 AVERAGE DAILY MWTH POWER 87.582 */aFP
- - AVE R AGEr-DA I LY-N UCLE A R-IJ4 G T-,--POWE R 99.446 a ATJ-37
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RATJMF-N T---TO-NWTH =-1,024 f
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DATE 12, 8,80
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HOUR GMWE TURB G NWTH NI RATIO RATIO (E710)
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(P753)
(P723)
NI/MT M E,'M T 4
C 1
1 0.00 0
1.43 0.00 0.000 0.000
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2 0.00 0
1.55 0.00 0.000 0.000 7
3 0.00 0
1.63 0.00 0.000 0.000 4
0.00 0
1.63 0.00 0.000 0.000 to-5 0.00 0
1.67 0.00 0.000 0.000 (U
6 0.00 0
1.67 0.00 0.000 0.000 3
7 0.00 0
1.75 0.00 0.000 0.000 is 0
0.00 0
1,71 0.00 0.000 0.000
( U 9
0.00 0
1.75 0.00 0.000 0.000 E
10 0.00 0
1.75 0.00 0.000 0.000 to 11 0.00 0
1.79 0.00' O.000 0.000 s
( 6 12 0.00 0
1,79 0.00 0.000 0.000 3
13 0.00 0
1.84 0.00 0.000 0.000 i,
14 0.00 0
3.34 0.00 0.000 DTEUD
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E 15 0.00 0
1.84 0.00 0.000 0.000 2
16 0.00 0
1,39 0.00 0.000 0.000 7
n' 17 0.00 0
3.06 5.70 1.864 0.'000 Y
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22 18 0.00 0
10.32 15.70 1.522 0.000 E
9 19 15.54 15019 20.27 27.80 1.372
.767 25 20 53.38 10371 54.20 63.90 1.179
.986 g(
=
21 70.50 10035 70.72 79.90 1.130
.997 i
n 22 81.24 9930 01.40 83.60 1.008
.998 k
i n
23 94.82 9959 96,13 98.80 1.028
.9G6 i
a' 24 96.61 9908 97.47 99.20 1.018
.991 30 f
146.01 PiWM( E )
l AVERAGE DAILY GENERATOR GROSS 472.12 MWil(I) a S'
AVERAGE DAILY THERMAL POWER I @
AVERAGE DAILY TURBINE GROSS HFAT RATE 271D FTU/KWH 19.255 -/aFP I
2 AVERAGE DAILY MWTH POWER AVERAGE DAILY NUCLEAR INST. POWER 19.983 */*FP n
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39 9
RATIO OF NI TO MWTH = 1.038
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e Tual 3urnup by Core Region Item 2
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Event Daca:
12/8/80 4
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The burnup was calculaced ac 102.5 EFFD for the tkree (3) enrichment regions.
t REGION NUMB R of FA BURNUP l
Batch 8
9 20,919 M/M l
60 18,780 M/M
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(_
D 52 8,166 M/M' E
56 2,537 MyD/MTU_
AVE.
10,631' #f0/Mr0' e
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CLEANUP FLOW HISTORY ITEM 3 EVENT DATE:
12/8/80 C
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i I_ tem 3 Cleanup flow history forty-eight (48) hours prior to the first sample in which the limit was exceeded indicated a letdown flowrate of forty three (43)gpm.
The "B" Makeup & Purification Demineralizer was in service.
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.c Degas Operations Item 4 Event Date:
12/8/80 DATE TIME LOCATION
{
12/6/80 0556 PZR 12/6/80 1140 "C" WGDT i
12/6/80 1420 PZR 1
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f Tim Duration When DEI-131 Exceeded 1.0 u C1/ gram and I-131 nalysis Results Item 5 Evene Data:
12/8/80
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e ITEM 5 As per Technical Specification 3.4.8, the four (4) hour sampling frequency as depicted on the table below was initiated at 0930 on 12/8/80 and the Dose Equivalent I-131 was 1.45 microcuries per gram. The four hour sampling frequency was terminated at 2230 on 12/8/80 when the DEI-131 was determined to be.386 microcuries per gram. The time duration when the specific activity of primary coolant exceeded 1.0 micrucuries per gram Dose Equivalent is fourteen (14) hours.
DATE TIME DEI-131 12/8/80 0930 1.45 12/8/80 1030 1.36 12/8/80 1430 1.32 12/8/80 1830 1.52 12/8/80 2230
.386 l
12/9/80 0332
.617 12/9/80 0812
.457 l
l
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| 05000302/LER-1980-001-01, /01T-0:on 800107,in Mode 1,determinted That Plant Was Taken Into Operational Mode While in Action Statement of Limiting Condition for Operation.Caused by Personnel Error.Revision to Tech Specs Has Been Submitted | /01T-0:on 800107,in Mode 1,determinted That Plant Was Taken Into Operational Mode While in Action Statement of Limiting Condition for Operation.Caused by Personnel Error.Revision to Tech Specs Has Been Submitted | | | 05000302/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000302/LER-1980-002-03, /03L-0:on 800105,following Normal Reactor Shutdown,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Leaking Fuel Pins & Anticipated Iodine Transient Following Shutdown | /03L-0:on 800105,following Normal Reactor Shutdown,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Leaking Fuel Pins & Anticipated Iodine Transient Following Shutdown | | | 05000302/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000302/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000302/LER-1980-003-03, /03L-0:on 800104,following Pressurizer Degassification Operations,Pressurizer Steam Space Sample Isolation Valve CAV-1 Would Not Close.Cause Unknown.Threads on Valve Stem Assembly Found Stripped.Evaluation Scheduled | /03L-0:on 800104,following Pressurizer Degassification Operations,Pressurizer Steam Space Sample Isolation Valve CAV-1 Would Not Close.Cause Unknown.Threads on Valve Stem Assembly Found Stripped.Evaluation Scheduled | | | 05000302/LER-1980-004, Supplemental Info to LER 80-004/04L-0:during Jan 1980, Analyses of Seawater Samples Collected at Six Sample Stations Not Performed Correctly Due to Equipment Malfunctions.Samples Recollected & Analyzed | Supplemental Info to LER 80-004/04L-0:during Jan 1980, Analyses of Seawater Samples Collected at Six Sample Stations Not Performed Correctly Due to Equipment Malfunctions.Samples Recollected & Analyzed | | | 05000302/LER-1980-005-03, /03L-0:on 800116,during Surveillance Schedule Review,Discovered Incore Neutron Detector Sys Calibr Surveillance SP-140 Not Performed within Required Time Interval.Caused by Misinterpretation of Requirements | /03L-0:on 800116,during Surveillance Schedule Review,Discovered Incore Neutron Detector Sys Calibr Surveillance SP-140 Not Performed within Required Time Interval.Caused by Misinterpretation of Requirements | | | 05000302/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000302/LER-1980-006-03, /03L-0:on 800123,during Routine Surveillance, Reactor Bldg Charcoal Filter Bank Efficiency Was Less than 99%.Caused by Natural End of Life for Filter.Filters Replaced | /03L-0:on 800123,during Routine Surveillance, Reactor Bldg Charcoal Filter Bank Efficiency Was Less than 99%.Caused by Natural End of Life for Filter.Filters Replaced | | | 05000302/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000302/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000302/LER-1980-007-03, /03L-0:on 800130,during Daily Plant Operating Surveillance SP-300,discovered Average Reactor Bldg Temp of 130.5F.Caused by Temp Transmitter CI-563-TT Being Stuck,Due to Operation Outside Design Temp Range | /03L-0:on 800130,during Daily Plant Operating Surveillance SP-300,discovered Average Reactor Bldg Temp of 130.5F.Caused by Temp Transmitter CI-563-TT Being Stuck,Due to Operation Outside Design Temp Range | | | 05000302/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000302/LER-1980-008-03, /03L-0:on 800206,during ECCS Pump Operability Demonstration Surveillance SP-340,decay Heat Pump a Discharge Throttle Valve Would Not Control Flow Automatic Phase.Caused by Loose Wires on auto-manual Selector Switch | /03L-0:on 800206,during ECCS Pump Operability Demonstration Surveillance SP-340,decay Heat Pump a Discharge Throttle Valve Would Not Control Flow Automatic Phase.Caused by Loose Wires on auto-manual Selector Switch | | | 05000302/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000302/LER-1980-009-03, /03L-0:on 800209,following Power Reduction & on 800211,during Startup Operations,Rcs Sampling Revealed Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel Pins & Iodine Transient Following RCS Transient | /03L-0:on 800209,following Power Reduction & on 800211,during Startup Operations,Rcs Sampling Revealed Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel Pins & Iodine Transient Following RCS Transient | | | 05000302/LER-1980-010-01, /01T-1:on 800226,during Routine Operation,Power Supply Failure Initiated Transient Condition,Resulting in Reactor Trip,Turbine Trip & Engineered Safeguards Actuation. Caused by Failure of Nni Voltage Buffer Card 4-7-10(4) | /01T-1:on 800226,during Routine Operation,Power Supply Failure Initiated Transient Condition,Resulting in Reactor Trip,Turbine Trip & Engineered Safeguards Actuation. Caused by Failure of Nni Voltage Buffer Card 4-7-10(4) | | | 05000302/LER-1980-010, Forwards LER 80-010/01T-1 | Forwards LER 80-010/01T-1 | | | 05000302/LER-1980-011-04, /04L-0:on 800222,discovered Representative Sample Not Obtained for Feb from Test Well 4,contrary to Tech Spec. Apparently Caused by Intake Canal Mod Const Activity.Tech Spec Change Request Will Be Submitted to Delete Require | /04L-0:on 800222,discovered Representative Sample Not Obtained for Feb from Test Well 4,contrary to Tech Spec. Apparently Caused by Intake Canal Mod Const Activity.Tech Spec Change Request Will Be Submitted to Delete Requirement | | | 05000302/LER-1980-011, Forwards LER 80-011/04L-0 | Forwards LER 80-011/04L-0 | | | 05000302/LER-1980-012, Forwards LER 80-012/04L-0 | Forwards LER 80-012/04L-0 | | | 05000302/LER-1980-012-04, /04L-0:on 800229,discovered That Environ Samples Were Not Taken from Locations at Required Frequencies.Caused by Personnel Error.Incident Occurrence Infrequent Therefore No Corrective Actions Necessary | /04L-0:on 800229,discovered That Environ Samples Were Not Taken from Locations at Required Frequencies.Caused by Personnel Error.Incident Occurrence Infrequent Therefore No Corrective Actions Necessary | | | 05000302/LER-1980-013, Forwards LER 80-013/04L-0 | Forwards LER 80-013/04L-0 | | | 05000302/LER-1980-013-04, /04L-0:on 800304,more than Two Std Deviations Were Discovered Between Preoperational Study & Operational Study in Metabolic Function of Discharge Salt Marshes.Possibly Caused by Natural or Seasonal Variations | /04L-0:on 800304,more than Two Std Deviations Were Discovered Between Preoperational Study & Operational Study in Metabolic Function of Discharge Salt Marshes.Possibly Caused by Natural or Seasonal Variations | | | 05000302/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000302/LER-1980-015-03, /03L-0:on 800306,while Performing Engineered Safeguards Functional Test,Decay Heat Suction Isolation Valve Began to Close Inadvertently.No Apparent Cause for Event.Investigation Underway | /03L-0:on 800306,while Performing Engineered Safeguards Functional Test,Decay Heat Suction Isolation Valve Began to Close Inadvertently.No Apparent Cause for Event.Investigation Underway | | | 05000302/LER-1980-016-01, /01T-0:on 800401,inadvertent Actuation of Fire Svc Deluge Sys Resulted in Damage to Auxiliary Bldg Ventilation Exhaust Filter AHFL-2A.Caused by Personnel Error During Reset of Fire Svc Panel alarm.AHFL-2A Media Replaced | /01T-0:on 800401,inadvertent Actuation of Fire Svc Deluge Sys Resulted in Damage to Auxiliary Bldg Ventilation Exhaust Filter AHFL-2A.Caused by Personnel Error During Reset of Fire Svc Panel alarm.AHFL-2A Media Replaced | | | 05000302/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | | | 05000302/LER-1980-017-03, /03L-0:on 800405,during Repair of B once-through Steam Generator Feedwater swing-disc Check Valve FWV-46, Discovered Valve Disc Retainer Pin Missing.Caused by Deficiency Occurring During Initial Manufacturer Assembly | /03L-0:on 800405,during Repair of B once-through Steam Generator Feedwater swing-disc Check Valve FWV-46, Discovered Valve Disc Retainer Pin Missing.Caused by Deficiency Occurring During Initial Manufacturer Assembly | | | 05000302/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000302/LER-1980-018-03, /03L-0:on 800413,during Chemistry Surveillance, Discovered That RCS Chloride & Fluoride Concentrations Were 0.24 Ppm & 0.274 Ppm.Caused by Chloride & Fluoride Contamination on Walls & Floors of Fuel Transfer Canal | /03L-0:on 800413,during Chemistry Surveillance, Discovered That RCS Chloride & Fluoride Concentrations Were 0.24 Ppm & 0.274 Ppm.Caused by Chloride & Fluoride Contamination on Walls & Floors of Fuel Transfer Canal | | | 05000302/LER-1980-018, Fowards LER 80-018/03L-0 | Fowards LER 80-018/03L-0 | | | 05000302/LER-1980-019-01, /01T-0:on 800517,crack Indication Discovered During Insp of Fuel Assembly NJ018E Upper End Fitting Holddown Spring.Investigation of Cause Underway.When Determined,Rept W/Corrective Actions Will Be Sent | /01T-0:on 800517,crack Indication Discovered During Insp of Fuel Assembly NJ018E Upper End Fitting Holddown Spring.Investigation of Cause Underway.When Determined,Rept W/Corrective Actions Will Be Sent | | | 05000302/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000302/LER-1980-020-03, /03L-0:on 800501,during Review of Surveillance Procedures,Discovered That Procedure for Weekly Battery Check SP-510 Was Not Performed for Wk of 800406.Caused by Damaged Hydrometer Used to Perform Surveillance | /03L-0:on 800501,during Review of Surveillance Procedures,Discovered That Procedure for Weekly Battery Check SP-510 Was Not Performed for Wk of 800406.Caused by Damaged Hydrometer Used to Perform Surveillance | | | 05000302/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000302/LER-1980-021-03, /03L-0:on 800506,during Insp of Feedwater swing- Disc Check Valve FWV-45,valve Hinge Pin Was Discovered Missing.Caused by Deficiency During Initial Assembly of Valve by Manufacturer.Valve Is Being Repaired | /03L-0:on 800506,during Insp of Feedwater swing- Disc Check Valve FWV-45,valve Hinge Pin Was Discovered Missing.Caused by Deficiency During Initial Assembly of Valve by Manufacturer.Valve Is Being Repaired | | | 05000302/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000302/LER-1980-022, Forwards LER 80-022/04L-0 | Forwards LER 80-022/04L-0 | | | 05000302/LER-1980-022-04, /04L-0:on 800528,samples Not Obtained for Apr from Test Wells 1 & 4 & Ph Results Not Reported for Waste Water Ponds,Test Well 5 & Discharge Canal.Caused by Elimination of Test Well Sites Due to Canal Mod & Loss of Ph Data | /04L-0:on 800528,samples Not Obtained for Apr from Test Wells 1 & 4 & Ph Results Not Reported for Waste Water Ponds,Test Well 5 & Discharge Canal.Caused by Elimination of Test Well Sites Due to Canal Mod & Loss of Ph Data | | | 05000302/LER-1980-023-03, /03L-0:on 800517,radioactive Matl in Form of Bagged Contaminated Waste & Poly Wrapped Scrap Lumber Was Taken to Site Dump.Caused by Apparent Communication Problem Between Health Physics Personnel & Bldg Servicemen | /03L-0:on 800517,radioactive Matl in Form of Bagged Contaminated Waste & Poly Wrapped Scrap Lumber Was Taken to Site Dump.Caused by Apparent Communication Problem Between Health Physics Personnel & Bldg Servicemen | | | 05000302/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000302/LER-1980-024, Forwards LER 80-024/04L-0 | Forwards LER 80-024/04L-0 | | | 05000302/LER-1980-024-04, /04L-0:on 800523,discovered That I-131 Charcoal Cartridge for Wk Ending 800401 Was Inadvertently Discarded. Caused by Personnel Error.Responsible Personnel Were Instructed on Proper Procedures | /04L-0:on 800523,discovered That I-131 Charcoal Cartridge for Wk Ending 800401 Was Inadvertently Discarded. Caused by Personnel Error.Responsible Personnel Were Instructed on Proper Procedures | | | 05000302/LER-1980-025-03, /03L-0:on 800609,while Performing SP-112 Calibr of Reactor Protection Sys,Count Rate Amplifier for Channel a Source Range Neutron Flux Monitor Found out-of-tolerance Caused by Defective Pulse & Output Amplifier Cards | /03L-0:on 800609,while Performing SP-112 Calibr of Reactor Protection Sys,Count Rate Amplifier for Channel a Source Range Neutron Flux Monitor Found out-of-tolerance Caused by Defective Pulse & Output Amplifier Cards | | | 05000302/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000302/LER-1980-026-03, /03L-0:on 800714,while Performing SP-710 Rc Decay Heat Removal & Rc Makeup Sys Chemistry Surveillance Program, Chloride & Fluoride Concentrations Exceeded Limits.Caused by High Temp of Decay Heat Sys & Migration of Elements | /03L-0:on 800714,while Performing SP-710 Rc Decay Heat Removal & Rc Makeup Sys Chemistry Surveillance Program, Chloride & Fluoride Concentrations Exceeded Limits.Caused by High Temp of Decay Heat Sys & Migration of Elements | | | 05000302/LER-1980-026, Forwards LER 80-026/03L-0 | Forwards LER 80-026/03L-0 | | | 05000302/LER-1980-027-01, /01T-0:on 800728,in Mode 5,while Performing OP-401 Core Flooding Sys,Check Valve CFV-79 Failed Allowing About 500 Gallons of Liquid to Enter Nitrogen Sys Via NGV-4. Apparently Caused by CFV-79 Failure & Open NGV-4 | /01T-0:on 800728,in Mode 5,while Performing OP-401 Core Flooding Sys,Check Valve CFV-79 Failed Allowing About 500 Gallons of Liquid to Enter Nitrogen Sys Via NGV-4. Apparently Caused by CFV-79 Failure & Open NGV-4 | |
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