05000219/LER-1981-019-03, /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised

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/03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised
ML20003H304
Person / Time
Site: Oyster Creek
Issue date: 04/27/1981
From: Sklar J
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003H301 List:
References
LER-81-019-03L, LER-81-19-3L, NUDOCS 8105050511
Download: ML20003H304 (1)


LER-1981-019, /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised
Event date:
Report date:
2191981019R03 - NRC Website

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