05000311/LER-1981-061-03, /03L-0:on 810713,disagreement Between Individual Rod Position Indicators for Rods 1SB2 & 2SB2 & Shutdown Rod Bank Demand Indicators Exceeded Tech Spec.Caused by Failed Operational Amplifiers.Amplifiers Replaced

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/03L-0:on 810713,disagreement Between Individual Rod Position Indicators for Rods 1SB2 & 2SB2 & Shutdown Rod Bank Demand Indicators Exceeded Tech Spec.Caused by Failed Operational Amplifiers.Amplifiers Replaced
ML20010C723
Person / Time
Site: Salem 
Issue date: 08/12/1981
From: Dickey F
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010C719 List:
References
LER-81-061-03L-01, LER-81-61-3L-1, NUDOCS 8108200345
Download: ML20010C723 (1)


LER-1981-061, /03L-0:on 810713,disagreement Between Individual Rod Position Indicators for Rods 1SB2 & 2SB2 & Shutdown Rod Bank Demand Indicators Exceeded Tech Spec.Caused by Failed Operational Amplifiers.Amplifiers Replaced
Event date:
Report date:
3111981061R03 - NRC Website

text

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U. S. NUCLE AR REGULATORY CoMMinich

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' LICENSEE EVENT REPORT CONTROL SLOCK:

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- (PLEAst PRINT OR TYPE ALL REQuinED INFO:tMATION)

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. DOCKET NUMBER e6. 89 EVENT DATE 74 75 REeQRT O ATE 80 j

} EVENT DESCRIPTION AND PMosABLk CONSEQUENCES h l177] l At 0855 and 1042 hours0.0121 days <br />0.289 hours <br />0.00172 weeks <br />3.96481e-4 months <br />, respectively, on July 13, 1981, the control operator noticedj g l that the-indiOldual r<v1 position indicators for rods-ISB2 and 2SB2 were in disagree j l ment with the. shutdown rod bank demand indicators by greater than + 12 steps. The l

O 4 F TTl 1 individual rod position indicators were declared inoperable at said hours,' and actiorg O s l' statement-3.1.3.2.1.a was entered.

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CAUSE

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lt i o l l Both indicators were inoperable due to failure of the operational amplifiers.

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j i i l lSB2 the amplifier board was replaced, and on 2SB2 the operational amplifier was l

4 gl replaced.- Both were recalibrated, tested satisfactorily, and returned to service.

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, 3 l Action statemeit 3.1.3.2.1.a was tcrminated at 1040 and 1243 hours0.0144 days <br />0.345 hours <br />0.00206 weeks <br />4.729615e-4 months <br />, respectively, l

i' i 4 l for ISB2 and 2SB2.

(81-46, 81-47, 81-48, 81-49).

7 e e so F ActuTV METt*00 08 STATUS

'<. PotA E R OTHER STATUS DISCOVE R Y OISCOVERY DESCRIPTION 32 W@ l0 j 0 l3 l@l N/A l

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