05000321/LER-1981-108-03, RCIC Steam Line Dp Switch N017 Actuated High.Caused by Setpoint Drift.Barton Model 288A Switch Recalibr.Administrative Setpoint Lowered

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RCIC Steam Line Dp Switch N017 Actuated High.Caused by Setpoint Drift.Barton Model 288A Switch Recalibr.Administrative Setpoint Lowered
ML20028A461
Person / Time
Site: Hatch 
Issue date: 11/04/1982
From: Tipps S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028A458 List:
References
LER-81-108-03X, LER-81-108-3X, NUDOCS 8211220190
Download: ML20028A461 (1)


LER-1981-108, RCIC Steam Line Dp Switch N017 Actuated High.Caused by Setpoint Drift.Barton Model 288A Switch Recalibr.Administrative Setpoint Lowered
Event date:
Report date:
3211981108R03 - NRC Website

text

ZRC FORM 366 U. S. NUCLE AR REGULATC RY COMMISSION mm UPDATE REPORT - PREVIOUS LICENSEE EVENT REPORT REPORT DATE 10/27/81 g

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8 f,0 61 DOCKET NUMBE R 68 6'J EVENT DATE 14 lb REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 lWhile the plant was operating steady-ntnen ne 1non uwe; tan ugi7 ncTc I

gOi3, l Steam Line dp Switch, was found to actuate at 214 inches of water. Tech.l l 0 l4 l l Specs. Table 3. 2-3, item 10, requires actuation at </= 300 percent flow l l_(207 inches : 191 + 16 inches water head correction). Redundant switch, 1

O 3 lN018 was operable. Plant operation was not affected. Public health and l

O e l0 lil l safety were not af fected by this repetitive event as last reported on LERl l 50-321/1981-0 95.

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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lThe cause of this event has been attributed to setpoint drift.

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