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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant ML20210U9301997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Haddam Neck Plant ML20210L0521997-07-31031 July 1997 Monthly Operating Rept for July 1997 for HNP ML20149E4451997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Haddam Neck Plant ML20140H5241997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Haddam Neck Plant ML20141D4141997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Connecticut Yankee Haddam Neck ML20137W8051997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Haddam Neck Plant ML20137A0801997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Haddam Neck Plant ML20138K5721997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Haddam Neck Plant.W/ ML20133M6121996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Yankee Haddam Neck Plant ML20132B9861996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Connecticut Yankee Haddam Neck Plant ML20134K7331996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Haddam Neck Plant ML20128Q7661996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Connecticut Yankee Haddam Neck Plant ML20029E6001994-04-30030 April 1994 Monthly Operating Rept 94-04 for Apr 1994 for Haddam Neck Plant ML20058P2691993-11-30030 November 1993 Monthly Operating Rept for Nov 1993 for Haddam Neck Plant ML20059M1881993-10-31031 October 1993 Monthly Operating Rept for Oct 1993 for Haddam Neck Plant.W/ ML20057G0561993-09-30030 September 1993 Monthly Operating Rept for Sept 1993 for Connecticut Yankee Haddam Neck Plant ML20057B3041993-08-31031 August 1993 Monthly Operating Rept for Aug 1993 for HNP ML20046D3961993-07-31031 July 1993 Monthly Operating Rept for Jul 1993 for Haddam Neck Plant ML20045H2301993-06-30030 June 1993 Monthly Operating Rept for June 1993 for HNP ML20045B9241993-05-31031 May 1993 Monthly Operating Rept for May 1993 for Haddam Neck Plant.W/ ML20035E6931993-03-31031 March 1993 Monthly Operating Rept for Mar 1993 for Haddam Neck Plant.W/ ML20044C1791993-02-28028 February 1993 Monthly Operating Rept for Feb 1993 for Haddam Neck Plant.W/ ML20128H6131993-01-31031 January 1993 Monthly Operating Rept for Jan 1993 for Haddam Neck Plant.W/ ML20127E5711992-12-31031 December 1992 Monthly Operating Rept for Dec 1992 for HNP ML20126A5011992-11-30030 November 1992 Monthly Operating Rept for Nov 1992 for Haddam Neck Plant.W/ ML20024H0611991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Connecticut Yankee Haddam Neck Plant ML20217A1991990-10-31031 October 1990 Monthly Operating Rept for Oct 1990 for Haddam Neck Plant ML20058A0891990-09-30030 September 1990 Revised Monthly Operating Rept for Aug 1990 for Haddam Neck Plant Unit 1 ML20059J1301990-08-31031 August 1990 Monthly Operating Rept for Aug 1990 for Haddam Neck Plant.W/ ML20044B3401990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Haddam Neck Plant ML20043G1161990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Haddam Neck Plant ML20043A1131990-04-30030 April 1990 Monthly Operating Rept for Apr 1990 for Haddam Neck Plant ML20012C1281990-02-28028 February 1990 Monthly Operating Rept for Feb 1990 for Haddam Neck Plant ML20006E8121990-01-31031 January 1990 Monthly Operating Rept for Jan 1990 for Haddam Neck Plant ML19332G2441989-11-30030 November 1989 Monthly Operating Rept for Nov 1989 for Haddam Neck Plant ML19325C6971989-09-30030 September 1989 Monthly Operating Rept for Sept 1989 for Haddam Neck Plant ML20247F6141989-08-31031 August 1989 Monthly Operating Rept for Aug 1989 for Haddam Neck Plant ML20245L8191989-07-31031 July 1989 Monthly Operating Rept for Jul 1989 for Haddam Neck Plant ML20246K1831989-06-30030 June 1989 Monthly Operating Rept for June 1989 for Haddam Neck Plant ML20244E1511989-05-31031 May 1989 Monthly Operating Rept for May 1989 for Haddam Neck Plant ML20247A1291989-04-30030 April 1989 Monthly Operating Rept for Apr 1989 for Haddam Neck ML20244D0831989-03-31031 March 1989 Monthly Operating Rept for Mar 1989 for Connecticut Yankee Haddam Neck Plant 1998-03-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 CY-99-047, Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use1999-03-23023 March 1999 Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use 05000213/LER-1999-001, :on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With1999-02-0101 February 1999
- on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With
05000213/LER-1997-016, :on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With1999-01-25025 January 1999
- on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With
ML20206F1971998-12-31031 December 1998 Annual Rept for 1998 for Cyap. with CY-99-027, Annual Rept for 10CFR50.59, for Jan-Dec 1998.With1998-12-31031 December 1998 Annual Rept for 10CFR50.59, for Jan-Dec 1998.With ML20198G9101998-12-22022 December 1998 Proposed Rev 2 of Cyap QAP for Haddam Neck Plant. Marked Up Rev 1 Included 05000213/LER-1997-018, :on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With1998-12-0808 December 1998
- on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With
05000213/LER-1998-009, :on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With1998-10-14014 October 1998
- on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With
05000213/LER-1998-008, :on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With1998-09-29029 September 1998
- on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With
05000213/LER-1997-021, :on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With1998-09-0101 September 1998
- on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With
ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co 05000213/LER-1998-007, :on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly1998-08-13013 August 1998
- on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly
CY-98-136, Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line1998-08-12012 August 1998 Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line ML20237B7461998-07-22022 July 1998 1998 Defueled Emergency Plan Exercise Scenario Manual, Conducted on 980722 ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 05000213/LER-1998-005, :on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow1998-06-0909 June 1998
- on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow
05000213/LER-1998-006, :on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed1998-06-0808 June 1998
- on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed
05000213/LER-1998-004, :on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B1998-06-0404 June 1998
- on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B
05000213/LER-1998-003, :on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency1998-06-0202 June 1998
- on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency
05000213/LER-1998-002, :on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established1998-05-19019 May 1998
- on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established
05000213/LER-1998-001, :on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue1998-05-0707 May 1998
- on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue
CY-98-068, Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms1998-04-15015 April 1998 Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms CY-98-045, Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing1998-04-13013 April 1998 Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing ML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217F0611998-03-31031 March 1998 Historical Review Team Rept ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 CY-98-046, Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal1998-03-12012 March 1998 Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant CY-98-010, Annual Rept for 10CFR50.59,Jan-Dec,19971997-12-31031 December 1997 Annual Rept for 10CFR50.59,Jan-Dec,1997 ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20217P4861997-12-31031 December 1997 1997 Annual Financial Rept, for Cyap ML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant 05000213/LER-1997-020, :on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process1997-12-16016 December 1997
- on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process
ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant 05000213/LER-1997-017, :on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled1997-11-18018 November 1997
- on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled
05000213/LER-1997-019, :on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required1997-11-17017 November 1997
- on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required
ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant 05000213/LER-1997-018, :on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures1997-10-30030 October 1997
- on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures
ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant 05000213/LER-1997-015, :on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure1997-09-12012 September 1997
- on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure
05000213/LER-1996-027, :on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable1997-09-12012 September 1997
- on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable
05000213/LER-1996-016, :on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed1997-09-12012 September 1997
- on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed
05000213/LER-1997-014, :on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks1997-09-0505 September 1997
- on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks
05000213/LER-1996-021, :on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys1997-09-0505 September 1997
- on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys
05000213/LER-1996-005, :on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope1997-09-0505 September 1997
- on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope
1999-04-28
[Table view] |
Text
O CONNECTICUT YANKEE AT O M IC POWER COMPANY HADDAM NECK PLANT 362 INJUN HOLLOW ROAD e EAST HAMPTON. CT 06424-3099 December 15,1993 Re: Technical Specification 6.9.1.8 Docket No. 50-213 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555
Dear Sir:
In acconiance with reporting requirements of Technical Specification 6.9.1.8, the Connecucut Yankee HaMam Neck Plant Monthly Operanng Report 93-12 covering operations for the period November 1,1993 to November 30,1993 is hereby forwarded.
Very truly yours, A
John P. Stetz Vice President HnMam Neck Station JPS/va cc-(1)
Regional Admirustrator, Region 1 U. S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 (2)
Wilham J. Raymond Sr. Resident Inspector Connecticut Yankee 23004G f#
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1 M'onthly Operating Report No. 93-12 For The Month of 1
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Plant Oncrations Summ arv - November 1993 The following is the Summary of Plant Operations for November 1993.
On November 1st, at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />, the plant was in Mode 1. Power Operation at 100% load.
On November 18th, at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />, the plant commenced a load reduction for a repair needed on the Number 1 Steam Generator Safety Valve (MS-SV-14). At 0055 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br />, the load reduction was stopped at 80% power for a special test on the " Rod Position Indication Systen..
At 1220 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.6421e-4 months <br />, the load reduction was recommenced.
At 1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />, the plant was at 65% power for funher testing on Rod Position Indication.
On November 19th, at 0210 hours0.00243 days <br />0.0583 hours <br />3.472222e-4 weeks <br />7.9905e-5 months <br />, the test was completed and a load reduction was recommenced.
At 0339 hours0.00392 days <br />0.0942 hours <br />5.605159e-4 weeks <br />1.289895e-4 months <br />, the plant was at 30% power and holding for an adjustment of the turbine smoothing oil.
At 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br />, the load reduction continued.
At 0628 hours0.00727 days <br />0.174 hours <br />0.00104 weeks <br />2.38954e-4 months <br />, the turbine was separated from the grid and entered Mode 2 Stanup. At 1003 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.816415e-4 months <br />, the reactor was manually tripped entering Mode 3. Hot Standbe.
Work commenced on valve MS-SV-14, in loop one.
On November 21st, at 0456 hours0.00528 days <br />0.127 hours <br />7.539683e-4 weeks <br />1.73508e-4 months <br />, with repairs and tests satisfactory completed, loop one was returned to service.
At 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />, the plant commenced a critical approach withdrawing the control rods.
At 1020 hours0.0118 days <br />0.283 hours <br />0.00169 weeks <br />3.8811e-4 months <br />, the reactor was critcal at Mode 2, start up.
At 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />, latched the turbine for stan up.
At 1740 hours0.0201 days <br />0.483 hours <br />0.00288 weeks <br />6.6207e-4 months <br />, tripped the turbine due to a governor problem.
At 2252 hours0.0261 days <br />0.626 hours <br />0.00372 weeks <br />8.56886e-4 months <br />, with the governor problem solved, another turbine stan up was recommenced.
At 2336 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.88848e-4 months <br />, tripped turbine again due to a voltage regulator problem.
On November 22nd, at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />, the turbine was latched and then immediately tripped manually from the control room.
At 0304 hours0.00352 days <br />0.0844 hours <br />5.026455e-4 weeks <br />1.15672e-4 months <br />, relatched the turbine again.
At 0325 hours0.00376 days <br />0.0903 hours <br />5.373677e-4 weeks <br />1.236625e-4 months <br />, tripped the turbine due to the voltage regulator problem.
On November 23rd, at 0101 hours0.00117 days <br />0.0281 hours <br />1.669974e-4 weeks <br />3.84305e-5 months <br />, the problem on the voltage regulator was repaired and latched the turbine for start up.
At 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />, the generator was phased to the grid. at 0310 hours0.00359 days <br />0.0861 hours <br />5.125661e-4 weeks <br />1.17955e-4 months <br />, the plant. attained Mode 1. Power Operations. At 0322 hours0.00373 days <br />0.0894 hours <br />5.324074e-4 weeks <br />1.22521e-4 months <br />, the plant was at 10% load and holding for chemistry acceptance.
At 0609 hours0.00705 days <br />0.169 hours <br />0.00101 weeks <br />2.317245e-4 months <br />, chemistry was within specifications and the plant staned a power ascension to 30% load.
At 0845 hours0.00978 days <br />0.235 hours <br />0.0014 weeks <br />3.215225e-4 months <br />, the governor would not allow the load to be increased past 160 MWe. At 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br />, the plant commenced a power reduction.
At 1150 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.37575e-4 months <br />, the turbine was taken i
off the line to repair the governor.
On November 24th, at 1310 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.98455e-4 months <br />, relatched the turbine to test the governor.
At 1329 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.056845e-4 months <br />, tripped the turbine, the test for the repair on the governor was satisfactory.
At 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br />, relatched the turbine.
At 1753 hours0.0203 days <br />0.487 hours <br />0.0029 weeks <br />6.670165e-4 months <br />, the generator was phased to the gnd for a power ascension. At 1802 hours0.0209 days <br />0.501 hours <br />0.00298 weeks <br />6.85661e-4 months <br />, the plant entered Mode 1. Power Operation.
At 1835 hours0.0212 days <br />0.51 hours <br />0.00303 weeks <br />6.982175e-4 months <br />, the plant was at 10% load on chemistry hold. At 2032 hours0.0235 days <br />0.564 hours <br />0.00336 weeks <br />7.73176e-4 months <br />, chemistry was within specifications an the plant commenced a power increase.
At 2245 hours0.026 days <br />0.624 hours <br />0.00371 weeks <br />8.542225e-4 months <br />, the plant was at 30% load for a chemistry hold.
On November 25th, at 0155 hours0.00179 days <br />0.0431 hours <br />2.562831e-4 weeks <br />5.89775e-5 months <br />, chemistry was within specifications and the plant staned a power ascension.
On November 26th, at 0310 hours0.00359 days <br />0.0861 hours <br />5.125661e-4 weeks <br />1.17955e-4 months <br />, power was at 100% load.
l On November 29th, at 1043 hours0.0121 days <br />0.29 hours <br />0.00172 weeks <br />3.968615e-4 months <br />,1B Main feed pump exhibited a problem with high vibrations and overheating on the seals.
At 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />, the plant commenced a load reduction.
At 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, the plant was at 52% load and holding to repair the impeller and casing on IB Main Feed Pump.
The plant continued operating at 52% power for the month of November.
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NRC OPERATING STATUS REPORT Haddam Neck
- 1. Docket: 50 213
- 2. Reporting Period: 11/93 Outage + on-line Hours: 122.6 + 597.4 = 720.0 j
- 3. Utility
Contact:
R. E. Borg (203) 267-3649
- 4. Licensed Thermal Power (MWt): 1825
- 5. Nameplate Rating (Gross MWe): 667 x 0.9 = 600.3
- 6. Design Electrical Rating (Net MWe): 582 1
- 7. Maximm Dependable capacity (Gross MWe): 586.9
{
- 8. Maxima Dependable capacity (Net MWe): 560.1
- 9. If changes occur above since test report, reasons are: NONE i
- 10. Power level to which restricted, if any (Net MWe): N/A i
- 11. Reasons for restriction, if any: N/A l
MONTH YEAR-TO-DATE CUMULATIVE
- 12. Report period hours:
720.0 8,016.0 227,184.0
- 13. Hours reactor critical:
671.7 6,401.9 181,208.3 1
- 14. Reactor reserve shutdown hours:
0.0 0.0 1,285.0
- 15. Hours generator on-Line:
597.4 6,171.7 174,458.9
- 16. Unit reserve shutdown hours:
0.0 0.0 398.0 I
- 17. Gross thermal energy genersted (MWtH):
986,090.0 10,777,069.0 301,689,841.0 *
{
- 18. Gross electricet energy generated (MWeH):
331,921.0 3,562,608.0 98,885,190.0
- 19. Net electrical energy generated (MWeN):
313,655.2 3,381,666.6 93.942,868.2
- 20. Unit service factor:
83.0 77.0 76.8 1
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- 21. Unit availability factor:
83.0 77.0 77.0
\\
- 22. Unit capacity factor using MDC net 77.8 75.3 75.0 l
- 23. Unit capacity factor using DER not:
74.9 72.5 71.1
- 24. Unit forced outage rate:
4.8 2.5 5.5
- 25. Forced outage hours:
30.1 156.7 10,235.2 l
- 26. Shutdowne schedetad over neat 6 months (type,dete, duration): NONE
- 27. If currently shutdown, estlanted starte date: N/A I
- Ctmulative values from the first criticality (07/24/67). (The remaining cumulative values are from the first date cf comercist operation, 01/01/68).
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- l AVERAGE DAILY UNIT POWER LEVEL Docket No: 50-213 Unit: Connecticut Yankee Haddam Neck Date: December 15, 1993 Completed By: M. Bigalbal/K. Emmons Month: November 1993 Telephone: (203) 267-3654 l
l m
AVER AGE POWER IEVEL M
AVER AGE POWER LEVEL (MWe-Net)
(MWe-Net) l 1
1Bf 17 11Q 2
ill 18 12_4 3
181 19 il 4
1B_Q 20 Q
i 5
11Q 21 Q
6 181 22 Q
7 181 23 j_}.
i 8
181 24 i
9 181 25 3_L4 10 181 26 121 11 181 27 181 12 53 1 28 181 13 ill 29 ill 14 181 30 2.81 15 ill 31 16 18_Q
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CONNECTICUT YANKEE '
REACTOR COOLANT DATA NOVEMBER 1993 Reactor Coolant Analysis minimum average maximum pH @ 25 decrees C 6.1 6.3 6.4 Conductivity (uS/cm) 17.5 20.5 24.5 Chlorides (ppb) 10.1 12.8 17.9 Dissolved Oxygen (ppb)
<5.0
<5.0
<5.0 Boron (ppm) 980 1157 1392 Lithium (ppb) 1748 1949 2204 Total Act. (uCi/ml) 5.65E-02 5.65E-02 9.14E-01 1-131/133 ratio 5.20E-01 9.67E+00 6.55E+01 I-131 (uCi/ml) 5.75 E-04 6.05E-03 7.19E-02 Cmd (mg/l)
< l.0
<.1.0
<1.0 Tntium (uCi/ml) 1.35E+00 2.06E+00 2.47E+00 Hydrogen (cc/kg) 28.1 34.5 46.9 I
Aerated liquid waste processed (gallons):
1.71 E+05 Waste liquid processed through boron recovery (gallons):
0.00E+00 Average primary leak rate (gallons per minute):
2.74E-01 Primary to secondary leak rate (gallons per day):
2.17E+01 Mfs/93 w,
MAINTENANCE DEPARTMENT November 1993 Report Month System MALFUNCTION Effect on Corrective Action Special Precautions Taken To Provide or Safe Taken to Prevent For Reactor Safety During Repair Component Cause Result Operation Repetition 5 team Generator Unknown Steam Leak None Replaced MS-SV-14 Plant taken off line safety Valve WS-SV-14 rurbine Governor Incorrect Unable to None Replaced governor cup valve Plant taken off line cup valve increase load installed above 30% poier
'B' Main Impeller Excessive None Replaced pump rotating assembly Reduced power to 50% and isolated pump Peedwater pump failure vibration and repaired casing 1
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I&C DEPARTMENT Report Month -November 1993 System MALFUNCTION Effect on Corrective Action Special Precautions Taken To Provide or Safe Taken to Prevent For Reactor Safety During Repair Component Cause Result Operation Repetition F
i There were no re portable iter is for the 1 &C Department in November 1993 i
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UNIT SilCTDOWNS AND POWER REDUCTION Docket No:
50-213 Unit Name: Connecticut Yankee Date:
December 15, 1993 Report Month:
Novennber 1993 Completed By: Mary Bigalbal Telephone: (203) 267-3141 r
No.
Date Type Duration Reason Method of LER System Component (Hours)
Shutting Report Code Code Cause and Corrective Action to Prevent Recurrence down Reactor 73-07 11/14 S
126.5 A
1 n/a 3B RV Repair #1 Steam Generator Safety Valve (MS-SV-14) 73-0P 11/23 P
64.67 A
n/a n/a TA 65 Turbine governor problem. Replaced governor cup valve components 73-09 11/29 P
37.25 A
5 n/a SK P
High vibration on the *B' main feed pump. Repair 'B' main feed pump impeller IXZ3 REASON METHOD SYSTEM COMPONENT F Porced A Equipment Failure 1 Manual IEEE Standard IEEE Standard S Scheduled B Maintenance or Test 2 Manual Scram 805-1984 and/or 803 A-1983 and/or l
C Refueling 3 Automatic Scram
, NUREO-0161 Exhibit P NUREO-0161 Exhibit H D Regulatory Restriction 4 Continued E Operator Training 5 Reduced Load F Administrative 9 Other
+
O Operator Error H Other (Explain)
Refueline Information Reauest 1.
Name of facility HaddamNeti 2.
Scheduled date for next refueling shutdown.
November 12,1994 3.
Scheduled dale for restart following refuchng.
January 5,1995 4
(a)
Will refueling or resumption of operation thereafter require a techrucal specincation change or other heense amendment?
Unknown at this time (b)
If answer is yes, what, in general, will thcae be?
(c)
If answer is no, has the reload fuel deman and core configuranon been reviewed by your Plant Safety Review Comminee to determine whether any unreviewed safety questions are associated with the ccue reland?
Wa (d)
If no such review has taken place, when is it scMIM7 Wa 5.
9hMn1M date(s) for submitting proposed bcennng action and supparung infonnation.
6.
Important licensing considerations annmarM with refueling, e.g., new a different fuel design or supplier, unreviewed design or performance analysis =%. significant changes in fuel design, new operating procakses.
Na 7.
'Ihe number of fuel assernblies (a) in the core and (b) in the spent fuel storage pool (a) 157 (b) 809 8.
'Ihe present inwamart spent fuel pool storage cepecity and the size of any increase in licensed storage capec sy that has bass iequested or is planned,in number of fuel assemblies.
I168 9.
The projected date of the last refueling that can be discharged to the spent fuel pool assummg the present hcensed capamry.
1998
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