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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant ML20210U9301997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Haddam Neck Plant ML20210L0521997-07-31031 July 1997 Monthly Operating Rept for July 1997 for HNP ML20149E4451997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Haddam Neck Plant ML20140H5241997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Haddam Neck Plant ML20141D4141997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Connecticut Yankee Haddam Neck ML20137W8051997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Haddam Neck Plant ML20137A0801997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Haddam Neck Plant ML20138K5721997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Haddam Neck Plant.W/ ML20133M6121996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Yankee Haddam Neck Plant ML20132B9861996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Connecticut Yankee Haddam Neck Plant ML20134K7331996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Haddam Neck Plant ML20128Q7661996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Connecticut Yankee Haddam Neck Plant ML20029E6001994-04-30030 April 1994 Monthly Operating Rept 94-04 for Apr 1994 for Haddam Neck Plant ML20058P2691993-11-30030 November 1993 Monthly Operating Rept for Nov 1993 for Haddam Neck Plant ML20059M1881993-10-31031 October 1993 Monthly Operating Rept for Oct 1993 for Haddam Neck Plant.W/ ML20057G0561993-09-30030 September 1993 Monthly Operating Rept for Sept 1993 for Connecticut Yankee Haddam Neck Plant ML20057B3041993-08-31031 August 1993 Monthly Operating Rept for Aug 1993 for HNP ML20046D3961993-07-31031 July 1993 Monthly Operating Rept for Jul 1993 for Haddam Neck Plant ML20045H2301993-06-30030 June 1993 Monthly Operating Rept for June 1993 for HNP ML20045B9241993-05-31031 May 1993 Monthly Operating Rept for May 1993 for Haddam Neck Plant.W/ ML20035E6931993-03-31031 March 1993 Monthly Operating Rept for Mar 1993 for Haddam Neck Plant.W/ ML20044C1791993-02-28028 February 1993 Monthly Operating Rept for Feb 1993 for Haddam Neck Plant.W/ ML20128H6131993-01-31031 January 1993 Monthly Operating Rept for Jan 1993 for Haddam Neck Plant.W/ ML20127E5711992-12-31031 December 1992 Monthly Operating Rept for Dec 1992 for HNP ML20126A5011992-11-30030 November 1992 Monthly Operating Rept for Nov 1992 for Haddam Neck Plant.W/ ML20024H0611991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Connecticut Yankee Haddam Neck Plant ML20217A1991990-10-31031 October 1990 Monthly Operating Rept for Oct 1990 for Haddam Neck Plant ML20058A0891990-09-30030 September 1990 Revised Monthly Operating Rept for Aug 1990 for Haddam Neck Plant Unit 1 ML20059J1301990-08-31031 August 1990 Monthly Operating Rept for Aug 1990 for Haddam Neck Plant.W/ ML20044B3401990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Haddam Neck Plant ML20043G1161990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Haddam Neck Plant ML20043A1131990-04-30030 April 1990 Monthly Operating Rept for Apr 1990 for Haddam Neck Plant ML20012C1281990-02-28028 February 1990 Monthly Operating Rept for Feb 1990 for Haddam Neck Plant ML20006E8121990-01-31031 January 1990 Monthly Operating Rept for Jan 1990 for Haddam Neck Plant ML19332G2441989-11-30030 November 1989 Monthly Operating Rept for Nov 1989 for Haddam Neck Plant ML19325C6971989-09-30030 September 1989 Monthly Operating Rept for Sept 1989 for Haddam Neck Plant ML20247F6141989-08-31031 August 1989 Monthly Operating Rept for Aug 1989 for Haddam Neck Plant ML20245L8191989-07-31031 July 1989 Monthly Operating Rept for Jul 1989 for Haddam Neck Plant ML20246K1831989-06-30030 June 1989 Monthly Operating Rept for June 1989 for Haddam Neck Plant ML20244E1511989-05-31031 May 1989 Monthly Operating Rept for May 1989 for Haddam Neck Plant ML20247A1291989-04-30030 April 1989 Monthly Operating Rept for Apr 1989 for Haddam Neck ML20244D0831989-03-31031 March 1989 Monthly Operating Rept for Mar 1989 for Connecticut Yankee Haddam Neck Plant 1998-03-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 CY-99-047, Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use1999-03-23023 March 1999 Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use 05000213/LER-1999-001, :on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With1999-02-0101 February 1999
- on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With
05000213/LER-1997-016, :on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With1999-01-25025 January 1999
- on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With
ML20206F1971998-12-31031 December 1998 Annual Rept for 1998 for Cyap. with CY-99-027, Annual Rept for 10CFR50.59, for Jan-Dec 1998.With1998-12-31031 December 1998 Annual Rept for 10CFR50.59, for Jan-Dec 1998.With ML20198G9101998-12-22022 December 1998 Proposed Rev 2 of Cyap QAP for Haddam Neck Plant. Marked Up Rev 1 Included 05000213/LER-1997-018, :on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With1998-12-0808 December 1998
- on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With
05000213/LER-1998-009, :on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With1998-10-14014 October 1998
- on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With
05000213/LER-1998-008, :on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With1998-09-29029 September 1998
- on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With
05000213/LER-1997-021, :on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With1998-09-0101 September 1998
- on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With
ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co 05000213/LER-1998-007, :on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly1998-08-13013 August 1998
- on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly
CY-98-136, Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line1998-08-12012 August 1998 Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line ML20237B7461998-07-22022 July 1998 1998 Defueled Emergency Plan Exercise Scenario Manual, Conducted on 980722 ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 05000213/LER-1998-005, :on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow1998-06-0909 June 1998
- on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow
05000213/LER-1998-006, :on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed1998-06-0808 June 1998
- on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed
05000213/LER-1998-004, :on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B1998-06-0404 June 1998
- on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B
05000213/LER-1998-003, :on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency1998-06-0202 June 1998
- on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency
05000213/LER-1998-002, :on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established1998-05-19019 May 1998
- on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established
05000213/LER-1998-001, :on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue1998-05-0707 May 1998
- on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue
CY-98-068, Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms1998-04-15015 April 1998 Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms CY-98-045, Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing1998-04-13013 April 1998 Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing ML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217F0611998-03-31031 March 1998 Historical Review Team Rept ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 CY-98-046, Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal1998-03-12012 March 1998 Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant CY-98-010, Annual Rept for 10CFR50.59,Jan-Dec,19971997-12-31031 December 1997 Annual Rept for 10CFR50.59,Jan-Dec,1997 ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20217P4861997-12-31031 December 1997 1997 Annual Financial Rept, for Cyap ML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant 05000213/LER-1997-020, :on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process1997-12-16016 December 1997
- on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process
ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant 05000213/LER-1997-017, :on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled1997-11-18018 November 1997
- on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled
05000213/LER-1997-019, :on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required1997-11-17017 November 1997
- on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required
ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant 05000213/LER-1997-018, :on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures1997-10-30030 October 1997
- on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures
ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant 05000213/LER-1997-015, :on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure1997-09-12012 September 1997
- on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure
05000213/LER-1996-027, :on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable1997-09-12012 September 1997
- on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable
05000213/LER-1996-016, :on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed1997-09-12012 September 1997
- on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed
05000213/LER-1997-014, :on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks1997-09-0505 September 1997
- on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks
05000213/LER-1996-021, :on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys1997-09-0505 September 1997
- on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys
05000213/LER-1996-005, :on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope1997-09-0505 September 1997
- on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope
1999-04-28
[Table view] |
Text
I CONNECTICUT YANKEE ATOMIC POWER COMPANY HADDAM NECK PLANT 3C2 INJUN HOLLOW ROAD e EAST HAMPTON, CT 06424-3099 August 15,1993 Re: Technical Specification 6.9.1.8 Docket No. 50-213 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555
Dear Sir:
In acconlance with reponing irquirements of Technical Specification 6.9.1.8, the Connecticut Yankee Haddam Neck Plant Monthly Operating Report 93-08 covering operations for the period July 1,1993 to July 31,1993 is hereby forwarded.
Very truly yours, Vice President Haddam Neck Station JPS/va ec:
(1)
Regional Administrator, Region 1 U. S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 (2)
William J. Raymond Sr. Resident Inspector Connecticut Yankee i
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9308190142 930731 PDR ADOCK 05000213 F
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j Connecticut Yankee Atomic Power Company Haddam Neck Plant Haddam, Connecticut 1
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I Monthly Operating Report No. 93-08 For The Month of July 1993 a
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____._________..______.____m,__..___
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Plant Ooerations Sunuimy - July 1993 ne following is the Summary of Plant Operations for July 1993.
On July 1st at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />, the plant was in Cold Shutdown Mode 5 for the 17th Refueling and i
Maintenance Outage.
On July 7th at 0330 hours0.00382 days <br />0.0917 hours <br />5.456349e-4 weeks <br />1.25565e-4 months <br />, a heat up of the Reactor Coolant System commenced.
5 On July 11th at 0827 hours0.00957 days <br />0.23 hours <br />0.00137 weeks <br />3.146735e-4 months <br />, Mode 4 Hot Shutdown was attained.
i On July 13th at 0132 hours0.00153 days <br />0.0367 hours <br />2.18254e-4 weeks <br />5.0226e-5 months <br />, Mode 3 Hot Standby was attained.
On July 17th at 1836 hours0.0213 days <br />0.51 hours <br />0.00304 weeks <br />6.98598e-4 months <br />, Mode 2 Stanup was entered.
On July 18th at 0355 hours0.00411 days <br />0.0986 hours <br />5.869709e-4 weeks <br />1.350775e-4 months <br />, the Reactor was critical. At 1546 hours0.0179 days <br />0.429 hours <br />0.00256 weeks <br />5.88253e-4 months <br />, a manual reactor trip was initiated for startup physics testing, Mode 3 Hot Standby. At 2032 hours0.0235 days <br />0.564 hours <br />0.00336 weeks <br />7.73176e-4 months <br />, Mode 2 Startup was reached. At 2209 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.405245e-4 months <br />, the Reactor was critical.
On July 19th at 1338 hours0.0155 days <br />0.372 hours <br />0.00221 weeks <br />5.09109e-4 months <br />, the startup physics tests were complete. Cycle 18's core was released to Operations for heat up. At 1448 hours0.0168 days <br />0.402 hours <br />0.00239 weeks <br />5.50964e-4 months <br />, an automatic reactor trip occurred due to 2 out of the 4 wide range NIS channels being in trip at the same time, (n:f: LER 93-013) entered Mode 3 Hot Standby.
At 1720 hours0.0199 days <br />0.478 hours <br />0.00284 weeks <br />6.5446e-4 months <br />, Mode 2 Stanup was reached. At 1841 hours0.0213 days <br />0.511 hours <br />0.00304 weeks <br />7.005005e-4 months <br />, the Reactor was critical.
On July 20th at 1118 hours0.0129 days <br />0.311 hours <br />0.00185 weeks <br />4.25399e-4 months <br />, the generator was phased to the grid commencing Power Operation Mode 1, at 5% load. The Cycle 17 Refueling was at an end.
On July 21st at 0101 hours0.00117 days <br />0.0281 hours <br />1.669974e-4 weeks <br />3.84305e-5 months <br />, the plant commenced a load reduction for the turbine overspeed test. At 0126 hours0.00146 days <br />0.035 hours <br />2.083333e-4 weeks <br />4.7943e-5 months <br />, operations took the unit off line and conducted the test entering Mode 2 Stanup. At 0148 hours0.00171 days <br />0.0411 hours <br />2.44709e-4 weeks <br />5.6314e-5 months <br />, the test was completed. At 0158 hours0.00183 days <br />0.0439 hours <br />2.612434e-4 weeks <br />6.0119e-5 months <br />, the turbine was relatched. At 0249 hours0.00288 days <br />0.0692 hours <br />4.117063e-4 weeks <br />9.47445e-5 months <br />, the generator was phased to the grid attaining Mode 1 Power Operation at 5%. At 0352 hours0.00407 days <br />0.0978 hours <br />5.820106e-4 weeks <br />1.33936e-4 months <br />, the plant was at 30% load for a chemistry hold.
On July 22nd at 1235 hours0.0143 days <br />0.343 hours <br />0.00204 weeks <br />4.699175e-4 months <br />, chemistry was within specifications and the plant staned a power ascension.
On July 23rd at 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br />, the plant was at 80% 1oad and holding for flux maps.
On July 26th at 1155 hours0.0134 days <br />0.321 hours <br />0.00191 weeks <br />4.394775e-4 months <br />, a power ascension was commenced. At 1708 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.49894e-4 months <br />, power was at 100% load.
ne plant continued to operate at 100% load for the remainder of the month.
AVER AGE DAILY UNIT POWER LEVEL Docket No: 50-213 Unit: Connecticut Yankee Haddam Neck Date: August 15, 1993 Completed By: K. Emmons/M. Bigalbal Month: July Telephone: (203) 267-3654 DAX AVER AGE POWER LEVEL DAX AVERAGE POWER LEVEL (MWe-Net)
(MWe-Net) 1 R
17 R
2 Q
18 Q
3 Q
19 R
4 20 11 5
a 21 2_&
6 Q
22 15J1 7
R 23 414 8
Q 24 G
9 R
25 M
10 26 412 11 Q
27 141 12 Q
28 5J42 13 Q
29 547 14 R
30 141 15 Q
31 144 16 Q
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NRC OPERATING STATUS REPORT s
i Haddam Neck
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- 1. Docket: 50-213
- 2. Reporting Period: 07/93 Outage + On-line Hours: 468.7 + 275.3 = 744.0 1
- 3. Utility contact: M. P. Bain (203) 267-3635
- 4. Licensed Thermal Power (MWt): 1825
- 5. Nameptate Rating (Gross MWe): 667 x 0.9 = 600.3
- 6. Design Electrical Rating (Net MWe): 582 i
- 7. Maxinun Dependable capacity (Gross MWe): 586.9
- 8. Maximum Dependable Capacity (Wet MWo): 560.1 j
- 9. If changes occur above since last report, reasons are: NONE
- 10. Power tevet to which restricted, if any (Net MWe): N/A
- 11. Reasons for restriction, if any: N/A MONTH YEAR-TO-DATE CUMULATIVE
- 12. Report period hours:
744.0 5,087.0
'224,255.0
- 13. Hours reactor critical:
321.8 3,521.2 178,327.6
- 14. Reactor reserve shutdown hours:
0.0 0.0 1,285.0
- 15. Hours generator on-line:
2 75.3 3,457.8 171,745.0
- 16. Unit reserve shutdown hours:
0.0 0.0 398.0 i
- 17. Gross thermal energy generated (MWtH):
394,896.0 6,071,512.0 296,954,284.0
- 18. Cross electrical energy generated (MWeH):
121,929.0 2,017,255.0 97,339,837.0 *
- 19. Net electrical energy generated (MWeH):
109,601.2 1,913,316.9 92,474,518.5 *
- 20. Unit service factor 37.0 68.0 76.6
't
- 21. Unit availability factor:
37.0 68.0 76.8 I
- 22. Unit capacity factor using MDC net:
26.3 67.2 74.9 -
'I
- 23. Unit capacity factor using DER net:
25.3 64.6 70.9
- 24. Unit forced outage rate:
0.0 1.0 5.6
{
f
- 25. Forced outape hours:
0.0 34.1 10,112.6 l
- 26. Shutdowns scheduled over next 6 months (type,date, duration): NONE f
-I
- 27. If currently shutdown, estimated startup date: N/A l
.I
.j
- Cumulative values from the first criticality (07/24/67). (The remaining cumulative values are from the first date of comnercial operation, 01/01/68).
CONNECTICUT YANKEE REACTOR COOLANT DATA
. JULI 1993 Date Time pH COND Cl DO B Lithium Gross Act I-RATIO l-131 ACT Tritium uS/cm ppm ppb ppm ppm uCi/ml uCi/mi uCi/ml 01-Jul-93 08:00 4.64 9.43 <0.005 2570
<0.005 4.91 E-02 4.38E-02 02-Jul-93 08:08 4.57 9.29 <0.005 2582
<0.005 5.02E-02 5.38E-02 03-Juk93 07:30 4.60 8.85 <0.005 2575 <0.005 6.96E-02 7.63E-05 7.03E-02 04-Jul-93 07.50 4.61 9.27 <0.005 2582 <0.005 7.44E-02 1.29E-04 05-Jul-93 07:30 4.65 7.94 <0.005 2575
<0.005 8.60E-02 1.11 E-04 06-Jul-93 07:45 4.62 9.05 <0.005 2582
<0.005 8.71E-02 1.29E-04 5.19E-02 07-Jul-93 07:45 4.92 10.38 <0.005 4000 2564
<0.005 1.43E-01 2.05E-04 8.55E-02 OG-Jul-93 08:10 4.83 9.28 <0.005 3000 2555
<0.005 1.71 E-01 9.10E-05 5.60E-02 09-Jul-93 08:15 5.00 9.65 0.006 10 2549
<0.005 2.19E-01 2.84E-04 10-Juk93 08:00 4.99 9.94 <0.005 5 2552
<0.005 2.25E-01 1.90E-04 3.31E-02 11-Jul-93 08:20 5.35 12.76 0.007 5 2509 1.12 7.20E-02 4.07E-04 3.54E-02 12-Jul-93 08:22 5.22 10.99 0.011
<5 2485 1.01 5.80E-03 9.65E-05 2.94E-02 13-Jul-93 07:55 5.41 14.20 0.015
<5 2476 1.15 2.71 E-03 1.57E-05 2.78E-02 14-Jul-93 08:14 5.44 13.79 0.017
<5 2440 1.15 3.67E-03 3.40E-05 3.24E-02 l
15-Jul-93 06:50 5.42 14.51 0.015
<2 2440 8.60E-03 3.22E-02 16-Jul-93 07:58 5.41 13.27 0.014
<2 2452 1.02E-02 4.61E-06 3.40E-02 17-Jul-93 08:20 5.44 13.55 0.025
<5 2420 1.01 2.45E-03 2.89E-06 3.97E-02 18-Jul-93 08:30 5.58 10.57 0.008
<S 1807 0.89 8.50E-03 2.80E-02 19-Jul-93 07:45 5.99 10.12 0.008
<5 1209 0.48 2.53E-03 1.90E-02 20-Jul-93 07:50 5.83 13.13 0.015
<2 1747 1.39 1.66E-02 6.26E-05 1.79E-02 21-Jul-93 07:45 5.83 14.18 OM16
<5 1667 1.38 1.37E-01 0.66 7.56E-04 3.05E-02 22-Jul-93 08:25 5.98 19.76 0.019
<5 1578 1.07 1.14E-01 0.58 4.14E-04 3.17E-02 23-Juk93 08:10 6.06 17.94 0.013
<5 1472 1.80 3.46E-01 0.47 6.97E-04 4.77E-02 i
24-Jul-93 08:13 6.10 17.75 0.017
<5 1400 1.77 3.52E-01 0.58 9.46E-04 8.33E-02 l
25-Jul-93 08:35 6.15 23.40 0.017
<5 1385 2.02 3.14E-01 0.56 9.41 E-04 8.69E-02 26-Jul-93 07:35 6.19 21.40 0.021
<5 1390 2.13 3.67E-01 0.56 9.83E-04 1.08E-01 27-Jul-93 07:53 6.23 21.30 0.021
<5 1356 2.20 5.20E-01 0.61 1.24E-03 1.52E-01 28-Jul-93 07:56 6.29 25.40 0.021
<5 1335 2.57 4.92E-01 0.71 1.49E-03 1.99E-01 29-Jul-93 07:57 6.28 23.80 0.014
<5 1327 2.51 5.12E-01 0.76 1.74E-03 2.68E-01 30-Jub93 08:25 6.24 22.30 0.018
<5 1327 2.44 5.02E-01 0.75 1.59E-03 2.93E-01 31-Juk93 08:25 6.18 18.50 0.016
<5 1318 1.92 5.18E-01 0.68 1.37E-03 3.12E Minimum 4.57 7.94 <0.005
<5 1209
<0.005 2.45E-03 0.47 2.89E-06 1.79E-02 Average 5.49 14.38 0.011 281 2040 1.03 1.77E-01 0.63 5.39E-04 8.22E-02 Maximum 6.29 25.40 0.025 4000 2582 2.57 5.20E-01 0.76 1.74E-03 3.12E-01 Hydrogen CRUD Aerated Liquid Waste Processed (gallons) 1.50E+05 cc/Kg mg/L Waste Liquid Processed through Boron Recovery (gallons) 3.88E+04 17-Jul-93 41.5 19-Jul-93
<1 Average Primary Leak Rate (gallons per minute) 2.56E-04 18-Jul-93 28.6 26-Jul-93
<1 Primary to Secondary Leak Rate (gallons per minute) _
1.52E-04 22-Juk93 35.4 29-Jub93 23.4 30-Jul-93 22.9 31-Juh93 32.6
MAINTENANCE DEPARTMENT Report Month July 1993 System MALFUNCTION Effect on Corrective Action Special Precautions Taken To Provide or Safe Taken to Prevent For Reactor Safety During Repair Component Cause Result Operation Repetition There were no rcportable iteins for the Maintenance Dept rtment for July 1993 l
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_m__ _ _ _ _ __ _,,, _. _
I&C DEPARTMENT Repon Month: July 1993 System MALFUNCTION Effect on Corrective Action Special Precautions Taken To Provide or Safe Taken to Prevent For Reactor Safety During Repair Component Cause Result Operation Repetition Steam Line Incorrect Lack of None Return each steam line brea (
N'one Flow Valve steam line transmitter to service by Fransmitters Lineup break correcting valve lineup reactor protection function 4
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UNIT SIIUTDOWNS AND POWER REDUCTION Docket No: 50-213 Unit Name: Connecticut Yankee Date: August 15, 1993 Report Month:
Julv 1993 Completed By:
K. W. Emmons TeIephone: (203) 267-3654 No.
Date Type Duration Reason Method of LER System Component (Hours)
Shutting Report Code Code Cause and Corrective Action to Prevent Recurrence down Reactot 73-03 e 7/1/93 S
467.3 C
1 n/a AC RCT Continuation of Core XVII - XVill Refueling and Maintenance Outage 73-04 7/21/93 5
1.38 B
n/a n/a D
771rn Turbine Overspeed Trip Test
- IIEF, REASON METIIOD SYSTEM COMPONENT F Forced A Equipment Failure 1 Manual IEEE Standard IEEE Standard S Scheduled B Maintenance or Test 2 Manual Scram 805-1984 and/or 803A-1983 and/or C Refueling 3 Automatic. Scram NUREO-0161 Exhibit F NUREO-0161 Eahibit H D Regulatory Restriction 4 Continued E Operator Training 5 Reduced Load F Administrative 9 Other O Operator Error 11 Other (Exp'am) i
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Pefuelin e In form ation Reauest 1.
Name of facility thWm Neck 2.
Scheduled date for. ext refuelmg shutdown.
October 15,1994 i
3.
Schehled date for restart following refueling.
l December 6,1994 4.
(a)
Will refueling or resumption of operation thereafter require a txhnical specification change or other license arrendment?
Urinown at this time (b)
If answer is yes, what,in general, will tiese be?
(c)
If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety t
Review Commince to detennine whether any unreviewed safety questions are associated with the cost reload?
Wa (d)
If in t.uch review has taken placc, when is it scheduled?
rVa 5.
Scheduled date(s) for submitung proposed hcensmg action and supporting information.
6.
Iripor vit licensing considerations un+tM with refueling, e.g., new or different fuel design or supplier, anreviewed design or performance analysis -49. significant changes in fuel design, new operating proce&2res.
rVa 7.
The numt,er of fuel assen,thes (a) in the core and (b) in the spent fuel storage pool.
}
(a) 157 (b) 809 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned,in number of fuel amblies.
t i168
-r 9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.
1998
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