Letter Sequence RAI |
---|
|
|
MONTHYEARML22321A1052022-11-17017 November 2022 License Amendment Request for Application to Adopt TSTF-477, Revision 3, Add Action for Two Inoperable Control Room AC Subsystems and Associated Technical Specification Changes Project stage: Request ML23060A1662022-12-20020 December 2022 Acceptance Review: Adopt TSTF-477, Revision 3-Acceptance Letter Project stage: Acceptance Review ML23202A0682023-07-21021 July 2023 NRR E-mail Capture - NRC Request for Additional Information Re. TSTF-477 LAR Project stage: RAI ML23208A1942023-07-27027 July 2023 NRR E-mail Capture - Limerick Generating Station - Audit Plan for TSTF-477 LAR Review (L-2022-LLA-0174) Project stage: Approval ML23242A2172023-08-30030 August 2023 Response to Request for Additional Information for Application to Adopt TSTF-477, Revision 3, Add Action for Two Inoperable Control Room AC Subsystems and Associated Technical Specification Changes Project stage: Response to RAI ML23276B4642023-10-0303 October 2023 NRR E-mail Capture - NRC Request for Additional Information Limerick TSTF-477 LAR Project stage: RAI ML23311A2412023-11-0707 November 2023 NRR E-mail Capture - NRC Notification to the Commonwealth of Pennsylvania Re. Limerick Generating Station, Units 1 and 2 Amendment - Control Room Ventilation System Technical Specifications Project stage: Other ML23313A0432023-11-13013 November 2023 Summary of Regulatory Audit in Support of Amendment Request for Control Room Air Conditioning Technical Specifications Project stage: Other ML23321A2362023-12-14014 December 2023 Issuance of Amendment Nos. 262 and 224 Adoption of TSTF-477, Revision 3 and Associated Technical Specification Changes Project stage: Approval 2023-11-07
[Table View] |
|
---|
Category:E-Mail
MONTHYEARML24250A1062024-09-0606 September 2024 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC - Fleet Request - Proposed Alternative to Utilize Code Case OMN-32 (L-2024-LLR-0030) ML24234A2772024-08-21021 August 2024 NRR E-mail Capture - Final RAI - Constellation Energy, LLC - Fleet Request - Proposed Alternative Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds (L-2024-LLR-0031) ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version ML24197A0162024-07-12012 July 2024 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC - Fleet Request - License Amendment Request to Adopt TSTF-591 ML24176A1292024-06-20020 June 2024 Estimated Completion Schedule Change Email ML24156A0082024-05-31031 May 2024 NRR E-mail Capture - Constellation Energy, LLC - Fleet Request - Acceptance of Proposed Alternative Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds (L-2024-LLR-0031 ML24131A0612024-05-10010 May 2024 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of Proposed Alternative to Utilize Code Case OMN-32 (L-2024-LLR-0030) ML24107A9192024-05-0808 May 2024 Email to Christian Williams Re Decision on the Limerick Exemption ML24107A9202024-05-0303 May 2024 Email to Christian Williams Re Availability of Environmental Assessment for the Limerick Exemption ML24122C6742024-05-0101 May 2024 Response to a Request from NRC Review of a Draft EA for an Exemption for the Limerick Generating Station ML24122B5072024-05-0101 May 2024 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of License Amendment Request to Adopt TSTF-591, Revision 0 ML24122C6702024-04-29029 April 2024 Request from NRC Review of a Draft EA for an Exemption for the Limerick Generating Station ML24051A0652024-02-16016 February 2024 Digital I&C LAR RAIs Re HFE (Email) ML24026A2922024-01-26026 January 2024 – Request for Additional Information Regarding Limerick Digital Instrumentation and Controls License Amendment Request ML23331A0062023-11-22022 November 2023 (External Sender) Supplement - Limerick Security Rule Exemption Request – ISFSI Docket No. Reference ML23311A2412023-11-0707 November 2023 NRR E-mail Capture - NRC Notification to the Commonwealth of Pennsylvania Re. Limerick Generating Station, Units 1 and 2 Amendment - Control Room Ventilation System Technical Specifications ML23304A0192023-10-30030 October 2023 NRR E-mail Capture - Final RCI - Constellation Energy Generation, LLC - Limerick 1 & 2 - Exemption from Security Rule (L-2023-LLE-0026) ML23276B4642023-10-0303 October 2023 NRR E-mail Capture - NRC Request for Additional Information Limerick TSTF-477 LAR ML23255A2872023-09-12012 September 2023 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of Alternative to Use the Successive Inspection Requirements of BWRVIP-75-A ML23248A1282023-09-0101 September 2023 NRR E-mail Capture - Action: Opportunity to Review and Comment on a New NRC Information Collection, 10 CFR Part 50.55a, Codes and Standards (3150-XXXX) ML23237B3972023-08-24024 August 2023 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of Alternative Request to Use Updated BWRVIP Guidelines ML23208A1942023-07-27027 July 2023 NRR E-mail Capture - Limerick Generating Station - Audit Plan for TSTF-477 LAR Review (L-2022-LLA-0174) ML23202A0682023-07-21021 July 2023 NRR E-mail Capture - NRC Request for Additional Information Re. TSTF-477 LAR ML23201A1262023-07-18018 July 2023 Additional RAIs for Limerick Generation Station, Units 1 and 2 - LAR and Exemption Request for Digital I&C Installation Support ML23173A0632023-06-20020 June 2023 RAIs for Limerick Generation Station, Units 1 and 2 - LAR and Exemption Request for Digital I&C Installation Support ML23102A1642023-04-12012 April 2023 Generation Station, Unit No. 2 – Potential Emergent Relief Request for HPCI IST (EPID L-2023-LLR-0015) - Closure E-mail Dated 4/12/2023 ML23125A0522023-03-31031 March 2023 NRR E-mail Capture - Clean OL Pages for 50.69 LAR ML23089A1602023-03-30030 March 2023 NRR E-mail Capture - NRC Notification to the Commonwealth of Pennsylvania Re. Limerick Generating Station, Units 1 and 2 Amendment - Alternative 10 CFR 50.69 Categorization Approaches ML23086B9282023-03-27027 March 2023 Acceptance of Requested Licensing Action for License Amendment Request to Support Digital Modernization Project Installation ML23086A0822023-03-27027 March 2023 – Acceptance of Requested Licensing Action for Exemption Request to Support Digital Modernization Project Installation ML22354A2622022-12-20020 December 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of Request to Use Certain Provisions of the 2019 Edition of the ASME BPV Code, Section XI ML23060A1662022-12-20020 December 2022 Acceptance Review: Adopt TSTF-477, Revision 3-Acceptance Letter ML22200A0782022-07-19019 July 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request to Use Honeywell Mururoa V4F1 R Supplied Air Suits ML22172A0752022-06-17017 June 2022 Response: Review and Feedback on Draft Limerick Digital License Amendment Request (L-2020-LRM-0041) ML22136A0032022-05-13013 May 2022 NRR E-mail Capture - NRC Request for Additional Information - Limerick License Amendment Request (L-2021-LLA-0042) ML22124A2862022-05-0404 May 2022 Information Needed to Provide Substantive Feedback on Human Factors Engineering Supporting the Planned Limerick Digital I&C License Amendment Request ML22089A1172022-03-30030 March 2022 Additional Comments and Questions on Constellations March 31st Presentation ML22089A1162022-03-28028 March 2022 Comments and Questions on Constellations March 31st Presentation ML22112A2152022-03-28028 March 2022 Limerick_Acceptance Review TS Change to Correct Nonconservative Technical Specification Table 3.3.3-1 ML22041B5362022-02-10010 February 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Request for Additional Information Regarding Fleet License Amendment Request to Adopt TSTF-541 ML22034A0142022-02-0202 February 2022 NRR E-mail Capture - Audit Plan Supplement for LIM 50.69 LAR (L-2021-LLA-0042) ML22028A1832022-01-24024 January 2022 NRR E-mail Capture - Audit Plan Supplement for LIM 50.69 LAR (L-2021-LLA-0042) ML22020A0642022-01-13013 January 2022 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative for Repair of Water Level Instrumentation Partial Penetration Nozzles ML22005A1812022-01-0505 January 2022 NRR E-mail Capture - Staffs Questions Pertaining to Limerick Generating Station Digital Modernization Project LAR Pre-submittal Meeting Slides December 7, 2021 ML21301A0672021-10-28028 October 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Acceptance of License Amendment Request to Adopt TSTF-541 ML21295A0362021-10-20020 October 2021 NRR E-mail Capture - Supplement to Limerick 50.69 Audit Plan Dated October 1, 2021 (L-2021-LLA-0042) ML21286A0302021-10-13013 October 2021 Staffs Questions Pertaining to Limerick Generating Station Digital Modernization Project LAR Pre-submittal Meeting Slides October 20, 2021 ML21256A1902021-09-10010 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21252A0482021-09-0707 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Fleet Alternative Request for Repair of Water Level Instrumentation Partial Penetration Nozzles ML21215A3502021-08-0303 August 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Acceptance of License Amendment Request to Adopt TSTF-554 2024-09-06
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARML24274A2372024-10-0707 October 2024 – Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version ML24197A0162024-07-12012 July 2024 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC - Fleet Request - License Amendment Request to Adopt TSTF-591 ML24150A0242024-05-29029 May 2024 Notification of Commercial Grade Dedication Inspection (05000352/2024012 and 05000353/2024012) and Request for Information ML24079A2922024-03-21021 March 2024 Draft Request for Additional Information Regarding Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) - Non-Proprietary ML23276B4642023-10-0303 October 2023 NRR E-mail Capture - NRC Request for Additional Information Limerick TSTF-477 LAR ML23269A0522023-09-26026 September 2023 Request for Information and Notification of Conduct of IP 71111.21.N.04, Age-Related Degradation, Reference Inspection Report 05000352/2023010 and 05000353/2023010 ML23208A1942023-07-27027 July 2023 NRR E-mail Capture - Limerick Generating Station - Audit Plan for TSTF-477 LAR Review (L-2022-LLA-0174) ML23202A0682023-07-21021 July 2023 NRR E-mail Capture - NRC Request for Additional Information Re. TSTF-477 LAR ML23201A1262023-07-18018 July 2023 Additional RAIs for Limerick Generation Station, Units 1 and 2 - LAR and Exemption Request for Digital I&C Installation Support ML23173A0632023-06-20020 June 2023 RAIs for Limerick Generation Station, Units 1 and 2 - LAR and Exemption Request for Digital I&C Installation Support ML22320A1132022-11-21021 November 2022 Generation Station, Units 1 and 2 - Supplemental Information Needed for Acceptance of Digital Instrumentation and Controls License Amendment Requests ML22172A0752022-06-17017 June 2022 Response: Review and Feedback on Draft Limerick Digital License Amendment Request (L-2020-LRM-0041) ML22136A0032022-05-13013 May 2022 NRR E-mail Capture - NRC Request for Additional Information - Limerick License Amendment Request (L-2021-LLA-0042) ML22124A2862022-05-0404 May 2022 Information Needed to Provide Substantive Feedback on Human Factors Engineering Supporting the Planned Limerick Digital I&C License Amendment Request ML22103A2542022-04-19019 April 2022 Draft Request for Additional Information ML22089A1172022-03-30030 March 2022 Additional Comments and Questions on Constellations March 31st Presentation ML22045A4822022-02-14014 February 2022 Notification of Conduct of a Fire Protection Team Inspection ML22041B5362022-02-10010 February 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Request for Additional Information Regarding Fleet License Amendment Request to Adopt TSTF-541 ML22020A0642022-01-13013 January 2022 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative for Repair of Water Level Instrumentation Partial Penetration Nozzles ML21256A1902021-09-10010 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21144A2132021-05-24024 May 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21117A0342021-05-0505 May 2021 Request for Additional Information Regarding Proposed Alternative to Use ASME Code Case N-893 ML21062A0652021-03-0101 March 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative to Documentation Requirements for Pressure Retaining Bolting ML21049A2572021-02-18018 February 2021 Request for Additional Information Byron/Dresden Proposed Changes to Site Emergency Plans to Support Post-Shutdown and Permanently Defueled Conditions (EPID-2020-LLA-0240 & EPID-2020-LLA-0237) ML21048A3402021-02-11011 February 2021 Request for Information for Relief Request I4R-24 Associated with Residual Heat Removal Heat Exchanger Category C-A and C-B Examinations ML21015A1852021-01-15015 January 2021 Temporary Instruction 2515/194 Inspection Documentation Request ML20239A7982020-08-25025 August 2020 NRR E-mail Capture - Exelon Generation Company, LLC - Fleet License Amendment Request to Adopt TSTF-568, Revision 2 ML20156A2992020-06-0404 June 2020 RAI for RR to Use Inservice Testing Program Safety Relief Valve Testing ML20153A7042020-06-0101 June 2020 NRR E-mail Capture - Preliminary RAI for Fleet Request to Use Alternative OMN-26 ML20149K7012020-05-28028 May 2020 Request for Additional Information for License Amendment Request to Use Inservice Testing Program Safety Relief Valve Testing ML20098C4342020-04-0606 April 2020 Draft Request for Additional Information - Limerick Generating Station, Unit 1 - Emergency LAR to Increase Allowable MSIV Leakage ML19344A0332019-12-10010 December 2019 Request for Additional Information License Amendment Request to Adopt TSTF-505, Revision 2 Risk Informed Completion Times Exelon Generation Company Limerick Generating Station, Units 1 and 2 Docket Nos. 50-352 and 50-353 ML19344A0242019-12-0909 December 2019 Request for Additional Information (RAI) - Limerick Units 1 and 2: TSTF-505, Use of Risk Informed Completion Times (Ricts) for Actions to Be Taken When Limiting Conditions for Operation (Lcos) Are Not Met ML19275H1362019-10-0202 October 2019 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Request to Use ASME Code Case N-879 ML19179A0612019-07-19019 July 2019 Three Mile Point 1 - Supplemental Information Needed to Proposed Alternative to Use ASME Code Case N-879 ML19192A0312019-07-10010 July 2019 NRR E-mail Capture - LIMERICK-REQUEST for Additional Information: Risk Informed Completion Times TSTF-505, Revison 2, Provide RISK-INFORMED Completion Times - RITSTF Initiative 4B ML19168A0882019-06-17017 June 2019 Letter to R. W. Libra Alternative Request Pertaining to Dry Shielded Canisters Equipped with Boral Neutron Absorber Plates - Supplemental Information Needed (W/Enclosursi) ML18276A0202018-10-0202 October 2018 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Amendment Request to Revise Emergency Plan for Limerick and Peach Bottom ML18081B0682018-03-26026 March 2018 Second Round RAI for Limerick, 10 CFR 50.69 ML18067A1482018-03-0808 March 2018 Enclosurequest for Additional Information (Letter to P. R. Simpson Request for Additional Information Regarding Exelon Generating Company, Llc'S Decommissioning Funding Plan Update for Independent Spent Fuel Storage Installation) ML17354A0182017-12-19019 December 2017 E-mail Request for Information (Rai): Relief Request I3R-23 Regarding Limited Examination Coverage ML18040A9212017-11-0707 November 2017 Attachment - Limerick Generating Station, Units 1 and 2, Request for Additional Information Application to Revise TSs to Adopt TSTF-542, Revision 2 ML17207A0772017-07-31031 July 2017 Supplemental Information Needed for Acceptance of Requested Licensing Action Adoption of Title 10 of the Code of Federal Regulations Section 50.69 ML17137A1652017-05-16016 May 2017 Request for Additional Information for Relief Request Associated with Reactor Pressure Vessel Nozzle Repairs ML17062A4912017-03-0303 March 2017 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Fleet Alternative to RPV Threads in Flange Examination (CAC Nos. MF8712-MF8729) ML17018A1932016-12-0909 December 2016 NRR E-mail Capture - (External_Sender) Limerick Flood MSA Question ML16221A6712016-08-0808 August 2016 Draft Request for Additional Information ML16221A6122016-08-0808 August 2016 Draft Request for Additional Information ML16174A2982016-06-22022 June 2016 Draft Request for Additional Information 2024-07-15
[Table view] |
Text
From: Audrey Klett Sent: Tuesday, October 3, 2023 3:17 PM To: Flickinger, Stephen F:(Constellation Nuclear)
Cc: Elena Herrera Torres
Subject:
NRC Request for Additional Information re. Limerick TSTF-477 LAR (EPID L-2022-LLA-0174)
Attachments: Final RAI 4-19 for Limerick TSTF-477.docx
Expires: Monday, January 1, 2024 12:00 AM
- Steve,
Attached is a request for additional information (RAI, #4-19) for the subject LAR. As discussed earlier today, the NRC staff is requesting Constellation to respond to the RAI on or by October 31,2023.
- Thanks,
Audrey Klett, Senior Project Manager U.S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Division of Operating Reactor Licensing Plant Licensing Branch 1 301-415-0489
Hearing Identifier: NRR_DRMA Email Number: 2258
Mail Envelope Properties (SJ0PR09MB933683F5B1E305BB3F1CEC6887C4A)
Subject:
NRC Request for Additional Information re. Limerick TSTF-477 LAR (EPID L-2022-LLA-0174)
Sent Date: 10/3/2023 3:16:37 PM Received Date: 10/3/2023 3:16:00 PM From: Audrey Klett
Created By: Audrey.Klett@nrc.gov
Recipients:
"Elena Herrera Torres" <Maria.HerreraTorres@nrc.gov>
Tracking Status: None "Flickinger, Stephen F:(Constellation Nuclear)" <Stephen.Flickinger@constellation.com>
Tracking Status: None
Post Office: SJ0PR09MB9336.namprd09.prod.outlook.com
Files Size Date & Time MESSAGE 429 10/3/2023 3:16:00 PM Final RAI 4-19 for Limerick TSTF-477.docx 50883
Options Priority: Normal Return Notification: No Reply Requested: No Sensitivity: Normal Expiration Date: 1/1/2024
REQUEST FOR ADDITIONAL INFORMATION LIMERICK GENERATING STATION, UNITS 1&2 DOCKET NOS. 50-352 AND 50-353 EPID NO. L-2022-LLA-0174 LICENSE AMENDMENT REQUEST FOR APPLICATION TO ADOPT TSTF-477, REVISION 3 AND ASSOCIATED TECHNICAL SPECIFICATION CHANGES
By letter dated November17,2022 (Agencywide Documents Access and Management System Accession No.ML22321A105), Constellation Energy Generation, LLC (the licensee) submitted a license amendment request(LAR) for the Limerick Generating Station, Units1 and2 to revise the technical specifications(TS) to adopt TSTF-477, Revision3, Add Action for Two Inoperable Control Room AC [Air Conditioning] Subsystems(72 FR 141432, dated March 26, 2007; ML062510321), and make associated TS changes.
By email dated July 21, 2023 (ML23202A068), the U.S.Nuclear Regulatory Commission(NRC) staff sent the licensee a request for additional information (RAI). By letter dated August 30, 2021 (ML23242A217), the licensee responded to the request. The NRC staff also performed a licensing audit (audit plan dated July 27, 2023, ML23208A194).
The NRC staff has reviewed the information provided by the licensee in its application, as supplemented, and via the audit and has determined that the staff needs the following additional information to complete its review of the LAR. The following requests are numbered sequentially from the RAI sent on July 21, 2023. On September 28, 2023, the NRC and licensee staff had a clarification call. Updates to the RAIs based on this call are shown below in tracked changes.
As discussed with Mr. Stephen Flickinger of the licensees staff on October 3,2023, the NRC staff is requesting the licensee to respond to the RAI on or by October 31,2023.
BACKGROUND
Regulatory Basis
Title10 of the Code of Federal Regulations (10CFR), Section50.36(c)(2) requires that technical specifications (TS) contain limiting conditions for operability (LCOs), which are the lowest functional capability or performance levels of equipment required for safe operation of the facility. When an LCO of a nuclear reactor is not met, the licensee shall shut down the reactor or follow any remedial action permitted by the TS until the LCO can be met. Typically, the TS require restoration of equipment in a timeframe commensurate with its safety significance, along with other engineering considerations. The regulation under 10CFR50.36(b) requires that TS be derived from the analyses and evaluation included in the safety analysis report, and amendments thereto.
NRC Consideration of Risk Insights
The proposed amendment is not a risk-informed amendment submitted in accordance with NRC Regulatory Guide 1.174 (ML17317A256). Therefore, the NRC staff does not review the licensees probabilistic risk assessment models to determine their technical acceptability.
However, the NRC staff considers qualitative risk insights and associated compensatory measures in its decision on the proposed change.
2
Plant Response to a Postulated High Energy Line Break (HELB)
During the audit, the licensee indicated that the Limerick HELB design basis postulates a hypothetical guillotine type line break, isolates it via an isolation valve or reactor scram, copes with its associated environmental conditions, and achieves plant safe shutdown. The licensee also indicated that the hypothetical turbine enclosure HELB worst case vulnerabilities are a main steam system steam break of a 26 pipe and a feedwater system high energy liquid break of either a 20 or 34 pipe. The licensee indicated that routine operator rounds can detect small steam and liquid leakage well before the margin to piping rupture is challenged.
The plant response to a feedwater line break outside primary containment is described in Section 15.6.6 of the Updated Final Safety Analysis Report (UFSAR). Section 15.6.6.2.2 of the UFSAR states the following:
It is assumed that the normally operating plant instrumentation and controls are functioning. Credit is taken for the actuation of the reactor isolation system and ECCS [emergency core cooling system]. The RPS [reactor protection system]
(MSRVs [main steam relief valves], ECCS, and CRD [control rod drives]) and plant protection system (RHR [residual heat removal] heat exchangers) are assumed to function properly to assure a safe shutdown.
The ESF [engineered safeguards features] and RCIC/HPCI [reactor core isolation cooling/high pressure coolant injection] systems are assumed to operate normally.
Section 15.6.6.2.3 of the UFSAR indicates that a feedwater line break outside primary containment can be isolated, and that either the RCIC or HPCI systems can provide adequate flow to the vessel to maintain core cooling and prevent fuel clad failure. This section also indicates that a single failure of either the HPCI or the RCIC system would still provide sufficient flow to keep the core covered with water.
REQUESTS FOR ADDITIONAL INFORMATION:
- 4. Clarify which supplementary cooling provisions discussed in the LAR that the licensee is requesting NRC staff review and approval and that are beyond the scope of TSTF-477, Revision 3. Describe the function of the temporary chiller water hose/jumper modification and why NRC approval is needed. (Refer to Audit Question 1.)
- 5. Confirm whether all doors between the safety-related control enclosure, control room envelope, and nonsafety-related turbine enclosure are qualified HELB barriers. (Refer to Audit Question 2.)
- 6. Regarding the configuration of the temporary chiller water hose (jumpers):
- a. Describe (e.g., via a simplified sketch or drawing) the temporary chiller water hoses (jumpers) proximity to the control room (including a description of where the jumper will be located and routed from the turbine enclosure to the control enclosure). (Refer to Audit Question 3.)
- b. Are any doors to other rooms kept open to facilitate the routing of jumpers? (Refer to Audit Question 13.b.)
3
- c. Are the rooms along the path of the jumpers to the control room HVAC cooling coils served by any cooling systems? (Refer to Audit Question 13.c.)
- 7. Provide a high-level description of factors that make a catastrophic pipe failure in the turbine building unlikely in the plant configuration requested in the LAR. (Refer to Audit Question 7.)
- 8. [DELETED] In its response to Audit Question 1, the licensee indicated that the peak temperature conditions incorporating power rerate and MUR is estimated to be less than or equal to 135 degrees Fahrenheit (°F) and that this may result in a loss of equipment function to certain types of equipment in room 619 if a hypothetical unit 1 HELB occurred concurrently with the HELB door open while in the LCO. Has the licensee evaluated the capability of control room HVAC equipment, such as damper and valve actuators, located in room 619 to remain functional during the LCO action statement at 135 °F (if not, explain why an evaluation is not necessary)? (Refer to Audit Question 1.)
- 9. Discuss how operators can detect (1) leakage in the turbine enclosure prior to a HELB, including the leak rates that may be detected, and (2) a HELB occurring. (Refer to Audit Questions 3 and 8.)
- 10. Describe the conditions under which implementation of the proposed jumper supplementary cooling provision will be precluded if leakage is detected? (Refer to Audit Question 16.)
- 11. Describe whether control room habitability is affected if there is a HELB or if the temporary chiller water hose (jumper) breaks while the HELB door is partially blocked open. Does the control room habitability envelope include control room cooling equipment, safety related "lters, etc. located in the same room? Please con"rm whether a HELB impact would propagate to this room and, if yes, what measures would be needed to address the temperature and habitability. (Refer to Audit Questions 5 and 15.a.)
- 12. Regarding the licensees response to Audit Question 5, cCon"rm whether a dual unit shutdown starts as soon as the control room technical speci"cation temperature limit is exceeded, given that this limit could be exceeded before the 72-hour LCO expiration.
(Refer to Audit Questions 5 and 15.b.)
- 13. Regarding the licensees response to Audit Question 5, cCon"rm whether, if the drywell temperature exceeded the TS limit, Unit 1 would be shut down and Unit 2 would continue to operate until the expiration of the 72-hour LCO, provided the control room temperature is maintained within the TS acceptance level using chiller water from Unit 1 drywell chiller. (Refer to Audit Questions 5 and 15.c.)
- 14. Please con"rm whether, in addition to Control Room HVAC, the control building chillers also support other HVAC equipment (e.g., Battery Rooms). When the chillers are not operating, how are the non-control room HVAC systems supported? (Refer to Audit Question 14.d.)
- 15. Describe the actions operators would take if leakage was detected in the turbine enclosure prior to a HELB. (Refer to Audit Question 9.)
4
- 16. Discuss how operators would shut down the plant if a HELB occurs during the proposed jumper supplementary cooling provision (refer to Audit Questions 4, 6, 12, 16, and 19),
including:
- a. A discussion of the equipment that would be relied upon to shut down the plant and if this equipment would be affected by the HELB. (Refer to Audit Questions 6 and 19.3.a.)
- b. A discussion of the procedures that operators would use to shut down the plant (refer to Audit Questions 9, and 16, and 19.3.b), including any:
- i. verifications that these procedures are adequate to shut down the plant during the postulated conditions (refer to Audit Question 19.3.c)
ii. procedure changes required for operators to be able to shut down the plant during the postulated conditions (refer to Audit Questions 16 and 19.3.d)
iii. additional training required for operators to be able to shut down the plant during the postulated conditions (refer to Audit Question 19.3.e)
- c. A discussion of whether operators can close the HELB door between the turbine enclosure and control enclosure building if a HELB occurs during the proposed jumper supplementary cooling provision and if this action can be credited as a possible mitigative action. (Refer to Audit Question 4.)
- d. In its response to Audit Question 6, the licensee indicated that a potential HELB event with the HELB door propped open is bounded by the fire analysis for fire area 27, which assumes the complete loss of equipment in this fire area. Please confirm whether the fire safe shutdown in this area relies on an alternative shutdown (e.g., confirm whether a safe shutdown can be performed from the control room) or any equipment in the turbine enclosure that could be affected by a HELB. (Refer to Audit Question 12.)
- 17. Regarding the components in Room 619, what are the limiting components at the elevated temperature environment, and are any of them safety related and required for safe shutdown? (Refer to Audit Question 13.a.)
- 18. Regarding application of current TS:
- a. Is the TS equipment in Control Enclosure Room 619 considered inoperable/inoperative under the current TS if the HELB door under consideration is inoperable/inoperative? (Refer to Audit Question 18.1.)
- b. Which technical specification LCO action statements is the licensee required to enter if the HELB door under consideration is inoperable/inoperative? (Refer to Audit Question 18.3.a.)
- c. Would Technical Specification 3.0.3 be entered if the HELB door is breached or only if a HELB occurred while the HELB door is breached? (Refer to Audit Question 19.1.)
5
- 19. During the audit, the licensee indicated (ref. audit question 18.3.b) that the submitted LAR requests NRC approval to not enter the Technical Specification action statements associated with temporarily defeating the subject HELB doors function. The TS footnote, as currently proposed does not include an exception to entering the technical specification action statements associated with temporarily defeating the subject HELB doors function. The proposed TS footnote, which states, Supplemental cooling provisions, if required, may be implemented under this condition, would still require entry into these conditions because an explicit exception is not included.
Limerick LCO 3.0.1 states:
Compliance with the Limiting Conditions for Operation contained in the succeeding Specifications is required during the OPERATIONAL CONDITIONS or other conditions specified therein, except as provided in Specification 3.0.8. Upon failure to meet the Limiting Conditions for Operation, the associated ACTION requirements shall be met, except as provided in Specifications 3.0.5, 3.0.6, and 3.0.9.
As indicated in the audit response, LCO 3.0.9 cannot be applied to the CREFAS, SGT, and EDGs. Therefore, the conditions associated with these LCOs would be entered in accordance with LCO 3.0.1.
The NRC requests the licensee to either explain how the conditions associated with the LCOs discussed above would not be required to be entered with the currently proposed TS, or address (e.g., via revised TS markups) the apparent inconsistencies with the action statement completion time associated with the proposed footnote and the completion times associated with the TS action statements entered when the HELB doors function is temporarily defeated.