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MONTHYEARML20140A6321986-01-17017 January 1986 Forwards Safeguards Info Re Door Hatch & Blowout Panel Monitoring.Info Withheld (Ref 10CFR73.21) Project stage: Other ML20138A0971986-03-0303 March 1986 Proposed Tech Spec Changes,Deleting Tech Spec Table 3.7-1, Primary Containment Isolation Valves, Clarifying Definition & Text & Revising Shutdown Requirement 3.7.D.3 Project stage: Other ML20138A0891986-03-0303 March 1986 Application for Amend to License DPR-57,deleting Tech Spec Table 3.7-1, Primary Containment Isolation Valves, Clarifying Definition & Text & Revising Shutdown Requirement 3.7.D.3.Basis for Request Encl.Fee Paid Project stage: Request ML20141G1141986-04-15015 April 1986 Proposed Tech Specs Re Operability & Surveillance Requirements for Primary Containment Isolation Valves Project stage: Other ML20141G0851986-04-15015 April 1986 Application for Amend to License DPR-57,revising Tech Specs Re Operability & Surveillance Requirements for Primary Containment Isolation Valves.Fee Paid Project stage: Request ML20211B5641986-05-31031 May 1986 Advises of NRC-directed Work to Be Done to Health Physics Network Circuitry for Technical Support Ctr & Emergency Offsite Facility.Nrc Operations Ctr Should Be Notified of Completion of Work Project stage: Other ML20211K6271986-06-19019 June 1986 Forwards Revised Page 3.7-13 & Associated Change to Encl 3 to 860415 Request to Revise Primary Containment Valve Listing in Tech Specs.Page Inadvertently Omitted from Proposed Change 2 Project stage: Request 1986-04-15
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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARHL-5770, Application for Amends to Licenses DPR-57 & NPF-5,revising Acceptance Criteria for Diesel Fuel Oil Storage as Surveillance Requirement 3.8.1.3 Min Fuel Oil Level for DG Day Tanks Will Be Changed to Greater than 500 Gallons1999-10-0101 October 1999 Application for Amends to Licenses DPR-57 & NPF-5,revising Acceptance Criteria for Diesel Fuel Oil Storage as Surveillance Requirement 3.8.1.3 Min Fuel Oil Level for DG Day Tanks Will Be Changed to Greater than 500 Gallons HL-5811, Application for Amends to Licenses DPR-57 & NPF-5,revising Wording Contained in LCO 3.1.7 Re Standby Liquid Control Sys1999-07-29029 July 1999 Application for Amends to Licenses DPR-57 & NPF-5,revising Wording Contained in LCO 3.1.7 Re Standby Liquid Control Sys HL-5591, Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Would Implement Some of Generic Changes to ITSs Previously Approved by NRC1999-02-0505 February 1999 Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Would Implement Some of Generic Changes to ITSs Previously Approved by NRC HL-5694, Revised Application for Amends to Licenses DPR-57 & NPF-5, Revising TS for Increase in Allowable Values for Reactor Bldg & Refueling Floor Ventilation Exhaust Radiation Monitors1999-01-21021 January 1999 Revised Application for Amends to Licenses DPR-57 & NPF-5, Revising TS for Increase in Allowable Values for Reactor Bldg & Refueling Floor Ventilation Exhaust Radiation Monitors HL-5698, Application for Amends to Licenses DPR-57 & NPF-5,revising TS 2.1.1.2 by Deleting Footnote Which Specifies That SLMCPRs Are for Cycle 18 Only & Deleting TS 5.6.5.b.21998-12-0404 December 1998 Application for Amends to Licenses DPR-57 & NPF-5,revising TS 2.1.1.2 by Deleting Footnote Which Specifies That SLMCPRs Are for Cycle 18 Only & Deleting TS 5.6.5.b.2 HL-5658, Application for Amends to Licenses DPR-57 & NPF-5,increasing Allowable Values for High Radiation Trip for Reactor Bldg & Refueling Floor Ventilation Exhaust Monitors1998-07-22022 July 1998 Application for Amends to Licenses DPR-57 & NPF-5,increasing Allowable Values for High Radiation Trip for Reactor Bldg & Refueling Floor Ventilation Exhaust Monitors HL-5400, Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Remove/Modify Existing License Conditions,Surveillance Requirements That Have Been Completed & Exemptions That Are No Longer in Effect1997-12-18018 December 1997 Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Remove/Modify Existing License Conditions,Surveillance Requirements That Have Been Completed & Exemptions That Are No Longer in Effect HL-5413, Application for Amends to Licenses DPR-57 & NPF-5,allowing Plant to Operate at Uprated Power Level of 2763 Mwt Which Represents Power Level Increase of 8%.Proprietary TR NEDC-32749P Encl1997-08-0808 August 1997 Application for Amends to Licenses DPR-57 & NPF-5,allowing Plant to Operate at Uprated Power Level of 2763 Mwt Which Represents Power Level Increase of 8%.Proprietary TR NEDC-32749P Encl HL-5362, Application for Amends to Licenses DPR-57 & NPF-5,revising Operability Requirements for Rod Block Monitor Sys1997-05-0909 May 1997 Application for Amends to Licenses DPR-57 & NPF-5,revising Operability Requirements for Rod Block Monitor Sys HL-5368, Application for Amend to License DPR-57,revising Safety Limit Minimum Critical Power Ratio in TS 2.1.1.2 to Reflect Results of Cycle Specific Calculation.Proprietary Basis for Change,Also Encl.Encl Withheld,Per 10CFR2.790(a)(4)1997-05-0909 May 1997 Application for Amend to License DPR-57,revising Safety Limit Minimum Critical Power Ratio in TS 2.1.1.2 to Reflect Results of Cycle Specific Calculation.Proprietary Basis for Change,Also Encl.Encl Withheld,Per 10CFR2.790(a)(4) ML20138H4021997-04-29029 April 1997 Application for Amend to License DPR-57,revising TS 3.4.9 Re Reactor Coolant Sys Pressure & Temp Limits HL-5345, Application for Amend to License DPR-7,requesting Rev to TS 3.4.9 Re Reactor Coolant Sys Pressure & Temp Limits1997-04-14014 April 1997 Application for Amend to License DPR-7,requesting Rev to TS 3.4.9 Re Reactor Coolant Sys Pressure & Temp Limits HL-5276, Application for Amends to Licenses DPR-57 & NPF-5,which Provides an Alternate Method of Testing S/Rvs During Shutdown Conditions Rather than During Unit Startup as Is Currently Done1997-01-0707 January 1997 Application for Amends to Licenses DPR-57 & NPF-5,which Provides an Alternate Method of Testing S/Rvs During Shutdown Conditions Rather than During Unit Startup as Is Currently Done HL-5270, Application for Amend to License NPF-5,revising SLMCPR Values Based Upon Unique plant-evaluations for Current Cycle 13 & Use of GE Fuel in Next Cycle 141996-12-0303 December 1996 Application for Amend to License NPF-5,revising SLMCPR Values Based Upon Unique plant-evaluations for Current Cycle 13 & Use of GE Fuel in Next Cycle 14 HL-5054, Application for Amends to License DPR-57 & NPF-5, Respectively,Associating Changes W/Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long- Term Stability Solution Hardware1996-10-29029 October 1996 Application for Amends to License DPR-57 & NPF-5, Respectively,Associating Changes W/Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long- Term Stability Solution Hardware HL-5230, Application for Amends to Licenses DPR-57 & NPF-5,revising SRs 3.1.7.7 & 3.4.3.1 & LCOs 3.4.3,3.5.1 & 3.6.1.6 to Increase Nominal Mechanical Pressure Relief Setpoints for All SRVs & Allow Operation W/One SRV1996-10-0707 October 1996 Application for Amends to Licenses DPR-57 & NPF-5,revising SRs 3.1.7.7 & 3.4.3.1 & LCOs 3.4.3,3.5.1 & 3.6.1.6 to Increase Nominal Mechanical Pressure Relief Setpoints for All SRVs & Allow Operation W/One SRV HL-5213, Application for Amends to Licenses DPR-57 & NPF-5,clarifying Applicability of Certain Surveillances Addressing Rvp & Temp Limits & Replacing Vessel Pressure & Temp Limit Curves W/New Curves1996-09-19019 September 1996 Application for Amends to Licenses DPR-57 & NPF-5,clarifying Applicability of Certain Surveillances Addressing Rvp & Temp Limits & Replacing Vessel Pressure & Temp Limit Curves W/New Curves HL-5163, Application for Amends to Licenses DPR-57 & NPF-5,revising TSs Re CST Level Indication to Ensure Water Level Sufficient to Provide 50,000 Gallons of Water for Core Spray Makeup to Reactor Pressure Vessel1996-05-21021 May 1996 Application for Amends to Licenses DPR-57 & NPF-5,revising TSs Re CST Level Indication to Ensure Water Level Sufficient to Provide 50,000 Gallons of Water for Core Spray Makeup to Reactor Pressure Vessel HL-5004, Application for Amends to Licenses DPR-57 & NPF-5, Respectively,Revising Changes of Drywell Air Temp LCO from 135 F to 150 F1996-02-21021 February 1996 Application for Amends to Licenses DPR-57 & NPF-5, Respectively,Revising Changes of Drywell Air Temp LCO from 135 F to 150 F HL-5051, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Reflect Implementation of 10CFR50,App J,Option B1995-11-10010 November 1995 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Reflect Implementation of 10CFR50,App J,Option B HL-4861, Application for Amends to Licenses DPR-57 & NPF-5.Amends Would Revise Secondary Containment Draw Down & Maintain Vacuum Surveillance Requirement Acceptance Criteria1995-06-0606 June 1995 Application for Amends to Licenses DPR-57 & NPF-5.Amends Would Revise Secondary Containment Draw Down & Maintain Vacuum Surveillance Requirement Acceptance Criteria HL-4816, Application for Amend to Licenses DPR-57 & NPF-5,minimizing Thermal Stratification Events1995-05-0404 May 1995 Application for Amend to Licenses DPR-57 & NPF-5,minimizing Thermal Stratification Events HL-4789, Application for Amend to License NPF-5 Re Elimination of Selected Response Time Testing Requirements from TS1995-04-14014 April 1995 Application for Amend to License NPF-5 Re Elimination of Selected Response Time Testing Requirements from TS HL-4724, Application for Amends to Licenses DPR-57 & NFP-5,proposing Changes to Ts,To Allow Plant to Operate at Uprated Power Level of 2558 Mwt.Also,Forwards Proprietary Power Uprate SAR for E I Hatch Plant Units 1 & 21995-01-13013 January 1995 Application for Amends to Licenses DPR-57 & NFP-5,proposing Changes to Ts,To Allow Plant to Operate at Uprated Power Level of 2558 Mwt.Also,Forwards Proprietary Power Uprate SAR for E I Hatch Plant Units 1 & 2 HL-4723, Application for Amends to Licenses DPR-57 & NPF-5,replacing Environ TS W/Environ Protection Plan (Nonradiological) & Revising OLs to Reflect Changes1994-12-0202 December 1994 Application for Amends to Licenses DPR-57 & NPF-5,replacing Environ TS W/Environ Protection Plan (Nonradiological) & Revising OLs to Reflect Changes ML20078G7051994-11-0101 November 1994 Application for Amends to Licenses DPR-57 & NPF-5,converting TS to Improved TS Consistent w/NUREG-1433 HL-4587, Application for Amends to Licenses DPR-57 & NPF-5,lowering ATWS-RPT Setpoint & Allowing Restarting Recirculation Pump Following RPT When Temp Differential Between Coolant at Reactor Bottom Head & Reactor Steam Dome Cannot Be Obtained1994-10-13013 October 1994 Application for Amends to Licenses DPR-57 & NPF-5,lowering ATWS-RPT Setpoint & Allowing Restarting Recirculation Pump Following RPT When Temp Differential Between Coolant at Reactor Bottom Head & Reactor Steam Dome Cannot Be Obtained HL-4695, Application for Amend to License DPR-57,requesting Temporary Change to Unit 1 TSs Re Emergency Diesel Generator Operability Requirements During Reactor Shut Down Conditions1994-09-20020 September 1994 Application for Amend to License DPR-57,requesting Temporary Change to Unit 1 TSs Re Emergency Diesel Generator Operability Requirements During Reactor Shut Down Conditions HL-4648, Application for Amend to License DPR-57,proposing one-time Change to TS 3.9.C to Allow Shutdown Operations W/Only One of Two Required EDGs Aligned to Corresponding Core or Containment Cooling Sys1994-08-16016 August 1994 Application for Amend to License DPR-57,proposing one-time Change to TS 3.9.C to Allow Shutdown Operations W/Only One of Two Required EDGs Aligned to Corresponding Core or Containment Cooling Sys HL-4661, Application for Amends to Licenses DPR-51 & NPF-5,revising Result of Meetings & Includes Page Change Insertion Instructions,Per NUREG-14331994-08-0808 August 1994 Application for Amends to Licenses DPR-51 & NPF-5,revising Result of Meetings & Includes Page Change Insertion Instructions,Per NUREG-1433 ML20072B7441994-08-0404 August 1994 Application for Amend to License NPF-5,revising TSs for Traversing Incore Probe Operability Requirements HL-4651, Application for Amend to License NPF-5,revising TS 3.3.6.6 Requirements for All Traversing in-core Probe Machines to Be Operable,To Allow Less than Four Machines to Be Operable1994-07-19019 July 1994 Application for Amend to License NPF-5,revising TS 3.3.6.6 Requirements for All Traversing in-core Probe Machines to Be Operable,To Allow Less than Four Machines to Be Operable HL-4620, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Improved Insertion Instructions,Consistent w/NUREG- 14331994-07-0808 July 1994 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Improved Insertion Instructions,Consistent w/NUREG- 1433 HL-4561, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Allow Testing Planned at Plant to Demonstrate Capability to Operate Plant Up to Core Power Level of 2,558 Mwt1994-06-0707 June 1994 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Allow Testing Planned at Plant to Demonstrate Capability to Operate Plant Up to Core Power Level of 2,558 Mwt HL-4495, Application for Amends to Licenses DPR-57 & DPR-5 Revising Units 1 & 2 TS to Be Consistent w/NUREG-1433 Standard TS GE Plants,BWR/41994-02-25025 February 1994 Application for Amends to Licenses DPR-57 & DPR-5 Revising Units 1 & 2 TS to Be Consistent w/NUREG-1433 Standard TS GE Plants,BWR/4 HL-3433, Application for Amend to Licenses DPR-57 & NPF-5 Revising Unit 1 TS 4.9 & Unit 2 TS 4.8 Re Diesel Generator Testing Under Hot Initial Conditions1993-11-0909 November 1993 Application for Amend to Licenses DPR-57 & NPF-5 Revising Unit 1 TS 4.9 & Unit 2 TS 4.8 Re Diesel Generator Testing Under Hot Initial Conditions HL-3416, Application for Amends to Licenses DPR-57 & NPF-5,revising Unit 1 TS 3.9.D & Unit 2 TS 3/4.8.2 to Add Time Delays to RPS Electric Power Monitoring Trips1993-10-19019 October 1993 Application for Amends to Licenses DPR-57 & NPF-5,revising Unit 1 TS 3.9.D & Unit 2 TS 3/4.8.2 to Add Time Delays to RPS Electric Power Monitoring Trips ML20045E7261993-06-28028 June 1993 Application for Amends to Licenses DPR-57 & NPF-5,revising TS 3.7.A.4 & 3.6.4.1,respectively,to Allow One or More Suppression chamber-drywell Vacuum Breakers to Open During Surveillance Testing ML20044D0771993-05-0303 May 1993 Suppl to 920921 Application for Amends to Licenses DPR-57 & NPF-5,changing TS Administrative Controls Section Re Semiannual Radioactive Effluent Release Rept to Reflect New 10CFR50.36a,per GL 89-01 HL-3048, Application for Amend to License DPR-57,revising TS Re Removal of Primary Containment Isolation Valves E11-F022 & E11-F0231992-12-21021 December 1992 Application for Amend to License DPR-57,revising TS Re Removal of Primary Containment Isolation Valves E11-F022 & E11-F023 HL-2962, Application for Amend to License NPF-5,changing TS to Temporarily Revise Containment Sys Section to Allow Unit 1 Standby Gas Treatment Sys to Be Inoperable for Up to 7 Days During Unit 2 Operation,Per Generic Ltr 89-161992-11-10010 November 1992 Application for Amend to License NPF-5,changing TS to Temporarily Revise Containment Sys Section to Allow Unit 1 Standby Gas Treatment Sys to Be Inoperable for Up to 7 Days During Unit 2 Operation,Per Generic Ltr 89-16 HL-2006, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Remove Main Steam Line Radiation Monitor Reactor Scram & Group Isolation Functions,Per BWROG Topical Rept NEDO-31400, SE for Eliminating BWR MSIV Closure..1992-10-19019 October 1992 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Remove Main Steam Line Radiation Monitor Reactor Scram & Group Isolation Functions,Per BWROG Topical Rept NEDO-31400, SE for Eliminating BWR MSIV Closure.. HL-2409, Application for Amends to Licenses DPR-57 & NPF-5,revising Definition of Members of the Public & Unrestricted Area, in TS & Deleting Ref in ETS Footnote Re RM Instrumentation, in Response to New 10CFR20 Requirements,Per GL 89-011992-10-14014 October 1992 Application for Amends to Licenses DPR-57 & NPF-5,revising Definition of Members of the Public & Unrestricted Area, in TS & Deleting Ref in ETS Footnote Re RM Instrumentation, in Response to New 10CFR20 Requirements,Per GL 89-01 HL-2390, Application for Amends to Licenses DPR-57 & NPF-5, Incorporating Programmatic Controls for RETS Into Administrative Controls Section of TS & Relocating Procedural Details for RETS to ODCM & Pcp,Per GL 89-011992-09-21021 September 1992 Application for Amends to Licenses DPR-57 & NPF-5, Incorporating Programmatic Controls for RETS Into Administrative Controls Section of TS & Relocating Procedural Details for RETS to ODCM & Pcp,Per GL 89-01 ML20118A5761992-09-18018 September 1992 Application for Amends to Licenses DPR-57 & NPF-5,allowing Southern Nuclear Operating Co,Inc to Possess,Manage,Use, Operate & Maintain Facilities.Certificate of Concurrence from Southern Nuclear Operating Co,Inc Encl HL-2335, Application for Amends to Licenses DPR-57 & NPF-5,changing TS Figure 2.1-1 for Unit 1 & TS Figure 3/4 3-1 for Unit 2 to Reflect Correct Top of Active Fuel Reactor Pressure Vessel Water Level1992-09-0202 September 1992 Application for Amends to Licenses DPR-57 & NPF-5,changing TS Figure 2.1-1 for Unit 1 & TS Figure 3/4 3-1 for Unit 2 to Reflect Correct Top of Active Fuel Reactor Pressure Vessel Water Level HL-2355, Application for Amend to License DPR-57,changing TS to Revise Allowable Outage Times for EDG 1B to 14 Days to Perform Work on DG & Revising DG Surveillance Requirements 4.9.B.1 & 4.9.B.2 to Correct Adminstrative Error1992-07-30030 July 1992 Application for Amend to License DPR-57,changing TS to Revise Allowable Outage Times for EDG 1B to 14 Days to Perform Work on DG & Revising DG Surveillance Requirements 4.9.B.1 & 4.9.B.2 to Correct Adminstrative Error HL-2231, Application for Amends to Licenses DPR-57 & NPF-5,proposing to Revise Several Portions of TS Involving Shutdown & Refueling Operations1992-07-17017 July 1992 Application for Amends to Licenses DPR-57 & NPF-5,proposing to Revise Several Portions of TS Involving Shutdown & Refueling Operations HL-2225, Application for Amends to Licenses DPR-57 & NPF-5,revising TSs to Add Addl Electrical Sys Requirements,Per Generic Ltr 91-11, Resolution of Generic Issues 48, 'Lcos for Class 1E' & 49, 'Interlocks & LCOs for Class 1E Tie Breakers....'1992-07-17017 July 1992 Application for Amends to Licenses DPR-57 & NPF-5,revising TSs to Add Addl Electrical Sys Requirements,Per Generic Ltr 91-11, Resolution of Generic Issues 48, 'Lcos for Class 1E' & 49, 'Interlocks & LCOs for Class 1E Tie Breakers....' HL-1946, Application for Amends to Licenses DPR-57 & NPF-5,changing Snubber Functional Test Insp Interval to 18 Months,Per Generic Ltr 90-091992-02-20020 February 1992 Application for Amends to Licenses DPR-57 & NPF-5,changing Snubber Functional Test Insp Interval to 18 Months,Per Generic Ltr 90-09 1999-07-29
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARHL-5770, Application for Amends to Licenses DPR-57 & NPF-5,revising Acceptance Criteria for Diesel Fuel Oil Storage as Surveillance Requirement 3.8.1.3 Min Fuel Oil Level for DG Day Tanks Will Be Changed to Greater than 500 Gallons1999-10-0101 October 1999 Application for Amends to Licenses DPR-57 & NPF-5,revising Acceptance Criteria for Diesel Fuel Oil Storage as Surveillance Requirement 3.8.1.3 Min Fuel Oil Level for DG Day Tanks Will Be Changed to Greater than 500 Gallons HL-5811, Application for Amends to Licenses DPR-57 & NPF-5,revising Wording Contained in LCO 3.1.7 Re Standby Liquid Control Sys1999-07-29029 July 1999 Application for Amends to Licenses DPR-57 & NPF-5,revising Wording Contained in LCO 3.1.7 Re Standby Liquid Control Sys HL-5591, Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Would Implement Some of Generic Changes to ITSs Previously Approved by NRC1999-02-0505 February 1999 Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Would Implement Some of Generic Changes to ITSs Previously Approved by NRC HL-5694, Revised Application for Amends to Licenses DPR-57 & NPF-5, Revising TS for Increase in Allowable Values for Reactor Bldg & Refueling Floor Ventilation Exhaust Radiation Monitors1999-01-21021 January 1999 Revised Application for Amends to Licenses DPR-57 & NPF-5, Revising TS for Increase in Allowable Values for Reactor Bldg & Refueling Floor Ventilation Exhaust Radiation Monitors HL-5698, Application for Amends to Licenses DPR-57 & NPF-5,revising TS 2.1.1.2 by Deleting Footnote Which Specifies That SLMCPRs Are for Cycle 18 Only & Deleting TS 5.6.5.b.21998-12-0404 December 1998 Application for Amends to Licenses DPR-57 & NPF-5,revising TS 2.1.1.2 by Deleting Footnote Which Specifies That SLMCPRs Are for Cycle 18 Only & Deleting TS 5.6.5.b.2 HL-5658, Application for Amends to Licenses DPR-57 & NPF-5,increasing Allowable Values for High Radiation Trip for Reactor Bldg & Refueling Floor Ventilation Exhaust Monitors1998-07-22022 July 1998 Application for Amends to Licenses DPR-57 & NPF-5,increasing Allowable Values for High Radiation Trip for Reactor Bldg & Refueling Floor Ventilation Exhaust Monitors HL-5400, Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Remove/Modify Existing License Conditions,Surveillance Requirements That Have Been Completed & Exemptions That Are No Longer in Effect1997-12-18018 December 1997 Application for Amends to Licenses DPR-57 & NPF-5, Respectively.Amends Remove/Modify Existing License Conditions,Surveillance Requirements That Have Been Completed & Exemptions That Are No Longer in Effect ML20211J9351997-10-0606 October 1997 Corrected TS Pps to Amends 208 & 150 for Licenses DPR-57 & NPF-5,respectively,consisting of Pps 3.4-8 & 3.5-6 for Unit 1 & Pps 3.4-8 & 3.5-5 for Unit 2 to Reflect Revised SRV Setpoints HL-5413, Application for Amends to Licenses DPR-57 & NPF-5,allowing Plant to Operate at Uprated Power Level of 2763 Mwt Which Represents Power Level Increase of 8%.Proprietary TR NEDC-32749P Encl1997-08-0808 August 1997 Application for Amends to Licenses DPR-57 & NPF-5,allowing Plant to Operate at Uprated Power Level of 2763 Mwt Which Represents Power Level Increase of 8%.Proprietary TR NEDC-32749P Encl HL-5368, Application for Amend to License DPR-57,revising Safety Limit Minimum Critical Power Ratio in TS 2.1.1.2 to Reflect Results of Cycle Specific Calculation.Proprietary Basis for Change,Also Encl.Encl Withheld,Per 10CFR2.790(a)(4)1997-05-0909 May 1997 Application for Amend to License DPR-57,revising Safety Limit Minimum Critical Power Ratio in TS 2.1.1.2 to Reflect Results of Cycle Specific Calculation.Proprietary Basis for Change,Also Encl.Encl Withheld,Per 10CFR2.790(a)(4) HL-5362, Application for Amends to Licenses DPR-57 & NPF-5,revising Operability Requirements for Rod Block Monitor Sys1997-05-0909 May 1997 Application for Amends to Licenses DPR-57 & NPF-5,revising Operability Requirements for Rod Block Monitor Sys ML20138H4021997-04-29029 April 1997 Application for Amend to License DPR-57,revising TS 3.4.9 Re Reactor Coolant Sys Pressure & Temp Limits HL-5345, Application for Amend to License DPR-7,requesting Rev to TS 3.4.9 Re Reactor Coolant Sys Pressure & Temp Limits1997-04-14014 April 1997 Application for Amend to License DPR-7,requesting Rev to TS 3.4.9 Re Reactor Coolant Sys Pressure & Temp Limits ML20137N1751997-04-0404 April 1997 Amends 206 & 147 to Licenses DPR-57 & NPF-5,respectively, Revising Surveillance Requirements Addressing Reactor Vessel Pressure & Temperature HL-5276, Application for Amends to Licenses DPR-57 & NPF-5,which Provides an Alternate Method of Testing S/Rvs During Shutdown Conditions Rather than During Unit Startup as Is Currently Done1997-01-0707 January 1997 Application for Amends to Licenses DPR-57 & NPF-5,which Provides an Alternate Method of Testing S/Rvs During Shutdown Conditions Rather than During Unit Startup as Is Currently Done HL-5270, Application for Amend to License NPF-5,revising SLMCPR Values Based Upon Unique plant-evaluations for Current Cycle 13 & Use of GE Fuel in Next Cycle 141996-12-0303 December 1996 Application for Amend to License NPF-5,revising SLMCPR Values Based Upon Unique plant-evaluations for Current Cycle 13 & Use of GE Fuel in Next Cycle 14 HL-5054, Application for Amends to License DPR-57 & NPF-5, Respectively,Associating Changes W/Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long- Term Stability Solution Hardware1996-10-29029 October 1996 Application for Amends to License DPR-57 & NPF-5, Respectively,Associating Changes W/Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long- Term Stability Solution Hardware HL-5230, Application for Amends to Licenses DPR-57 & NPF-5,revising SRs 3.1.7.7 & 3.4.3.1 & LCOs 3.4.3,3.5.1 & 3.6.1.6 to Increase Nominal Mechanical Pressure Relief Setpoints for All SRVs & Allow Operation W/One SRV1996-10-0707 October 1996 Application for Amends to Licenses DPR-57 & NPF-5,revising SRs 3.1.7.7 & 3.4.3.1 & LCOs 3.4.3,3.5.1 & 3.6.1.6 to Increase Nominal Mechanical Pressure Relief Setpoints for All SRVs & Allow Operation W/One SRV HL-5213, Application for Amends to Licenses DPR-57 & NPF-5,clarifying Applicability of Certain Surveillances Addressing Rvp & Temp Limits & Replacing Vessel Pressure & Temp Limit Curves W/New Curves1996-09-19019 September 1996 Application for Amends to Licenses DPR-57 & NPF-5,clarifying Applicability of Certain Surveillances Addressing Rvp & Temp Limits & Replacing Vessel Pressure & Temp Limit Curves W/New Curves HL-5163, Application for Amends to Licenses DPR-57 & NPF-5,revising TSs Re CST Level Indication to Ensure Water Level Sufficient to Provide 50,000 Gallons of Water for Core Spray Makeup to Reactor Pressure Vessel1996-05-21021 May 1996 Application for Amends to Licenses DPR-57 & NPF-5,revising TSs Re CST Level Indication to Ensure Water Level Sufficient to Provide 50,000 Gallons of Water for Core Spray Makeup to Reactor Pressure Vessel HL-5004, Application for Amends to Licenses DPR-57 & NPF-5, Respectively,Revising Changes of Drywell Air Temp LCO from 135 F to 150 F1996-02-21021 February 1996 Application for Amends to Licenses DPR-57 & NPF-5, Respectively,Revising Changes of Drywell Air Temp LCO from 135 F to 150 F HL-5051, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Reflect Implementation of 10CFR50,App J,Option B1995-11-10010 November 1995 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Reflect Implementation of 10CFR50,App J,Option B HL-4861, Application for Amends to Licenses DPR-57 & NPF-5.Amends Would Revise Secondary Containment Draw Down & Maintain Vacuum Surveillance Requirement Acceptance Criteria1995-06-0606 June 1995 Application for Amends to Licenses DPR-57 & NPF-5.Amends Would Revise Secondary Containment Draw Down & Maintain Vacuum Surveillance Requirement Acceptance Criteria HL-4816, Application for Amend to Licenses DPR-57 & NPF-5,minimizing Thermal Stratification Events1995-05-0404 May 1995 Application for Amend to Licenses DPR-57 & NPF-5,minimizing Thermal Stratification Events HL-4789, Application for Amend to License NPF-5 Re Elimination of Selected Response Time Testing Requirements from TS1995-04-14014 April 1995 Application for Amend to License NPF-5 Re Elimination of Selected Response Time Testing Requirements from TS HL-4724, Application for Amends to Licenses DPR-57 & NFP-5,proposing Changes to Ts,To Allow Plant to Operate at Uprated Power Level of 2558 Mwt.Also,Forwards Proprietary Power Uprate SAR for E I Hatch Plant Units 1 & 21995-01-13013 January 1995 Application for Amends to Licenses DPR-57 & NFP-5,proposing Changes to Ts,To Allow Plant to Operate at Uprated Power Level of 2558 Mwt.Also,Forwards Proprietary Power Uprate SAR for E I Hatch Plant Units 1 & 2 HL-4723, Application for Amends to Licenses DPR-57 & NPF-5,replacing Environ TS W/Environ Protection Plan (Nonradiological) & Revising OLs to Reflect Changes1994-12-0202 December 1994 Application for Amends to Licenses DPR-57 & NPF-5,replacing Environ TS W/Environ Protection Plan (Nonradiological) & Revising OLs to Reflect Changes ML20078G7051994-11-0101 November 1994 Application for Amends to Licenses DPR-57 & NPF-5,converting TS to Improved TS Consistent w/NUREG-1433 HL-4587, Application for Amends to Licenses DPR-57 & NPF-5,lowering ATWS-RPT Setpoint & Allowing Restarting Recirculation Pump Following RPT When Temp Differential Between Coolant at Reactor Bottom Head & Reactor Steam Dome Cannot Be Obtained1994-10-13013 October 1994 Application for Amends to Licenses DPR-57 & NPF-5,lowering ATWS-RPT Setpoint & Allowing Restarting Recirculation Pump Following RPT When Temp Differential Between Coolant at Reactor Bottom Head & Reactor Steam Dome Cannot Be Obtained HL-4695, Application for Amend to License DPR-57,requesting Temporary Change to Unit 1 TSs Re Emergency Diesel Generator Operability Requirements During Reactor Shut Down Conditions1994-09-20020 September 1994 Application for Amend to License DPR-57,requesting Temporary Change to Unit 1 TSs Re Emergency Diesel Generator Operability Requirements During Reactor Shut Down Conditions HL-4648, Application for Amend to License DPR-57,proposing one-time Change to TS 3.9.C to Allow Shutdown Operations W/Only One of Two Required EDGs Aligned to Corresponding Core or Containment Cooling Sys1994-08-16016 August 1994 Application for Amend to License DPR-57,proposing one-time Change to TS 3.9.C to Allow Shutdown Operations W/Only One of Two Required EDGs Aligned to Corresponding Core or Containment Cooling Sys HL-4661, Application for Amends to Licenses DPR-51 & NPF-5,revising Result of Meetings & Includes Page Change Insertion Instructions,Per NUREG-14331994-08-0808 August 1994 Application for Amends to Licenses DPR-51 & NPF-5,revising Result of Meetings & Includes Page Change Insertion Instructions,Per NUREG-1433 ML20072B7441994-08-0404 August 1994 Application for Amend to License NPF-5,revising TSs for Traversing Incore Probe Operability Requirements HL-4651, Application for Amend to License NPF-5,revising TS 3.3.6.6 Requirements for All Traversing in-core Probe Machines to Be Operable,To Allow Less than Four Machines to Be Operable1994-07-19019 July 1994 Application for Amend to License NPF-5,revising TS 3.3.6.6 Requirements for All Traversing in-core Probe Machines to Be Operable,To Allow Less than Four Machines to Be Operable HL-4620, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Improved Insertion Instructions,Consistent w/NUREG- 14331994-07-0808 July 1994 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Improved Insertion Instructions,Consistent w/NUREG- 1433 HL-4561, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Allow Testing Planned at Plant to Demonstrate Capability to Operate Plant Up to Core Power Level of 2,558 Mwt1994-06-0707 June 1994 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Allow Testing Planned at Plant to Demonstrate Capability to Operate Plant Up to Core Power Level of 2,558 Mwt HL-4495, Application for Amends to Licenses DPR-57 & DPR-5 Revising Units 1 & 2 TS to Be Consistent w/NUREG-1433 Standard TS GE Plants,BWR/41994-02-25025 February 1994 Application for Amends to Licenses DPR-57 & DPR-5 Revising Units 1 & 2 TS to Be Consistent w/NUREG-1433 Standard TS GE Plants,BWR/4 HL-3433, Application for Amend to Licenses DPR-57 & NPF-5 Revising Unit 1 TS 4.9 & Unit 2 TS 4.8 Re Diesel Generator Testing Under Hot Initial Conditions1993-11-0909 November 1993 Application for Amend to Licenses DPR-57 & NPF-5 Revising Unit 1 TS 4.9 & Unit 2 TS 4.8 Re Diesel Generator Testing Under Hot Initial Conditions ML20059E6831993-10-21021 October 1993 Amends 190 & 129 to Licenses DPR-57 & NPF-5,respectively, Relocating Procedural Details Contained in Radiological Effluent Ts,Incorporating New Part 20 & Revising Frequency of Reporting Radiological Effluent Releases HL-3416, Application for Amends to Licenses DPR-57 & NPF-5,revising Unit 1 TS 3.9.D & Unit 2 TS 3/4.8.2 to Add Time Delays to RPS Electric Power Monitoring Trips1993-10-19019 October 1993 Application for Amends to Licenses DPR-57 & NPF-5,revising Unit 1 TS 3.9.D & Unit 2 TS 3/4.8.2 to Add Time Delays to RPS Electric Power Monitoring Trips ML20045E7261993-06-28028 June 1993 Application for Amends to Licenses DPR-57 & NPF-5,revising TS 3.7.A.4 & 3.6.4.1,respectively,to Allow One or More Suppression chamber-drywell Vacuum Breakers to Open During Surveillance Testing ML20044D0771993-05-0303 May 1993 Suppl to 920921 Application for Amends to Licenses DPR-57 & NPF-5,changing TS Administrative Controls Section Re Semiannual Radioactive Effluent Release Rept to Reflect New 10CFR50.36a,per GL 89-01 HL-3048, Application for Amend to License DPR-57,revising TS Re Removal of Primary Containment Isolation Valves E11-F022 & E11-F0231992-12-21021 December 1992 Application for Amend to License DPR-57,revising TS Re Removal of Primary Containment Isolation Valves E11-F022 & E11-F023 HL-2962, Application for Amend to License NPF-5,changing TS to Temporarily Revise Containment Sys Section to Allow Unit 1 Standby Gas Treatment Sys to Be Inoperable for Up to 7 Days During Unit 2 Operation,Per Generic Ltr 89-161992-11-10010 November 1992 Application for Amend to License NPF-5,changing TS to Temporarily Revise Containment Sys Section to Allow Unit 1 Standby Gas Treatment Sys to Be Inoperable for Up to 7 Days During Unit 2 Operation,Per Generic Ltr 89-16 HL-2006, Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Remove Main Steam Line Radiation Monitor Reactor Scram & Group Isolation Functions,Per BWROG Topical Rept NEDO-31400, SE for Eliminating BWR MSIV Closure..1992-10-19019 October 1992 Application for Amends to Licenses DPR-57 & NPF-5,revising TS to Remove Main Steam Line Radiation Monitor Reactor Scram & Group Isolation Functions,Per BWROG Topical Rept NEDO-31400, SE for Eliminating BWR MSIV Closure.. HL-2409, Application for Amends to Licenses DPR-57 & NPF-5,revising Definition of Members of the Public & Unrestricted Area, in TS & Deleting Ref in ETS Footnote Re RM Instrumentation, in Response to New 10CFR20 Requirements,Per GL 89-011992-10-14014 October 1992 Application for Amends to Licenses DPR-57 & NPF-5,revising Definition of Members of the Public & Unrestricted Area, in TS & Deleting Ref in ETS Footnote Re RM Instrumentation, in Response to New 10CFR20 Requirements,Per GL 89-01 HL-2390, Application for Amends to Licenses DPR-57 & NPF-5, Incorporating Programmatic Controls for RETS Into Administrative Controls Section of TS & Relocating Procedural Details for RETS to ODCM & Pcp,Per GL 89-011992-09-21021 September 1992 Application for Amends to Licenses DPR-57 & NPF-5, Incorporating Programmatic Controls for RETS Into Administrative Controls Section of TS & Relocating Procedural Details for RETS to ODCM & Pcp,Per GL 89-01 ML20118A5761992-09-18018 September 1992 Application for Amends to Licenses DPR-57 & NPF-5,allowing Southern Nuclear Operating Co,Inc to Possess,Manage,Use, Operate & Maintain Facilities.Certificate of Concurrence from Southern Nuclear Operating Co,Inc Encl HL-2335, Application for Amends to Licenses DPR-57 & NPF-5,changing TS Figure 2.1-1 for Unit 1 & TS Figure 3/4 3-1 for Unit 2 to Reflect Correct Top of Active Fuel Reactor Pressure Vessel Water Level1992-09-0202 September 1992 Application for Amends to Licenses DPR-57 & NPF-5,changing TS Figure 2.1-1 for Unit 1 & TS Figure 3/4 3-1 for Unit 2 to Reflect Correct Top of Active Fuel Reactor Pressure Vessel Water Level HL-2355, Application for Amend to License DPR-57,changing TS to Revise Allowable Outage Times for EDG 1B to 14 Days to Perform Work on DG & Revising DG Surveillance Requirements 4.9.B.1 & 4.9.B.2 to Correct Adminstrative Error1992-07-30030 July 1992 Application for Amend to License DPR-57,changing TS to Revise Allowable Outage Times for EDG 1B to 14 Days to Perform Work on DG & Revising DG Surveillance Requirements 4.9.B.1 & 4.9.B.2 to Correct Adminstrative Error 1999-07-29
[Table view] |
Text
j Georgia Power Company 333 Piedmont Avence Atlanta, Gectg a 30308 Telephone 404 526-7020 MaJing Address Post Office Box 4545 At:arta. Georg a 30302 h
Georgia Power J. T. Beckham, Jr. " v w m e% tw wrym V,ce Presidet and General Manager naciear operatons SL-580 April 15,1986 0467C Director of Nuclear Reactor Regulation Attention: Mr. D. Muller, Project Director BWR Project Directorate No. 2 Division of Boiling Water Reactor Licensing U. S. Nuclear Regulatory Commission Washington, D. C. 20555 NRC DOCKET 50-321 OPERATING LICENSE DPR-57 EDWIN I. HATCH NUCLEAR PLANT UNIT 1 REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS Gentlemen:
In accordance with the provisions of 10 CFR 50.90 as required by 10 CFR 50.59(c)(1), Georgia Power Company (GPC) hereby proposes changes to the Technical Specifications, Appendix A to Operating License DPR-57.
The proposed changes would update valve listings contained in Table 3.7-1,
" Primary Containment Isolation Yalves," and Table 3.7-4, " Primary Containment Testable Isolation Yalves." The requested changes fall into several areas:
Wording associated with the tables has been clarified to reflect the tables' intent. Primary containment isolation valves added to the plant as a result of modifications are proposed for addition to the tables. Valves which have been modified so that they do not perform a containment isolation function are deleted from Table 3.7-4. Yalves which have been incorrectly listed as containment isolation valves are removed from Table 3.7-4 Incorrect descriptive information appearing in tables 3.7-1 and 3.7-4 has been corrected. Notes to the tables have been corrected, deleted, or added as appropriate. -
Previous GPC submittals dated March 5,1979, and March 3,1986, proposed deletion of Tables 3.7-4 and 3.7-1, respectively. A comprehensive plant procedure has been developed to implement primary containment valve surveillance and control valve listings following removal of the listings from the. Technical Specifications. We continue to believe that plant procedures provide the most appropriate vehicle for this type of information, and we request that NRC continue its review of the above submittals.
The Plant Review Board and the Safety Review Board Subcommittee have !
reviewed the proposed changes.
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GeorgiaPower d Attention: Mr. D. Muller, Project Director BWR Project Directorate No. 2 Director of Nuclear Reactor Regulation April 15, 1986 Page Two i
Enclosure 1 provides a detailed description of the proposed changes and bases for the changes.
1 Enclosure 2 details the basis for our determination that the proposed changes do not involve a significant hazards consideration.
Enclosure 3 provides page change instructions for incorporating the proposed changes into the Technical Specifications.
. The proposed changed Technical Specifications pages follow Enclosure 3 Payment of filing fee is enclosed.
In order to allow time for procedure revision and orderly incorporation into copies of the Technical Specifications, we request that the proposed amendment, once approved by the NRC, be issued with an effective date to be no later than 60 days from the issuance of the amendment.
Pursuant to the requirements of 10 CFR 50.91, Mr. J. L. Ledbetter of the Environmental Protection Division of the Georgia Department of Natural Resources will be sent a copy of this letter and all applicable enclosures.
Mr. J. T. Beckham, Jr. states that he is Vice President of Georgia Power Company and is authorized to execute this oath on behalf of Georgia Power Company, and that to the best of his knowledge and belief the facts set forth in the letter and enclosures are true.
GEORGIA POWER COMPANY By: O J. T. Beckham, Jr. V Ow Sworn to and subscribed before me this 15th day of April,1986, a)m k. 0gj ry M iC ceary Pabl.c. Charon Csty, My comnvssion E,pires Dec. 12.1989 Attachments c: Mr. H. C. Nix, Jr.
Senior Resident Inspector, Plant Hatch Dr. J. N. Grace Mr. J. L. Ledbetter GO-NORMS ,
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Georgialbwer m. k ENCLOSURE 1 NRC DOCKET 50-321 OPERATING LICENSE DPR-57 EDWIN I. HATCH NUCLEAR PLANT UNIT 1 REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS BASIS FOR CHANGE REQUEST Changes are proposed to clarify and correct Plant Hatch Unit 1 Technical Specifications associated with Operability and Surveillance requirements for Primary Containment Isolation Valves ,(PCIVs). The proposed changes cover two general areas: The first area involves clarifying changes to wording associated with the performance of PCIV surveillance. The second area involves additions, deletions, and corrections to valve listings and descriptive information contained ivi Tables 3.7-1 and 3.7-4 The proposed changes and associated justifications are described below.
Proposed Change 1:
It is proposed to change the title of Table 3.7-1, " Primary Containment Isolation Yalves," to clarify its intent. The proposed new title is " Primary Containment Isolation Yalves Which Receive a Primary Containment Isolation Signal . " Table 3.7-1 is required for implementation of Technical Specification 4.7.D.1.a, which requires that " isolation valves that are power operated and automatically i ni tiated. . .be tested for simulated automatic initiation and the closure times specified in Table 3.7-1." This requirement can only apply to power-operated PCIVs which receive a containment isolation signal. The present title implies that the table is a complete listing of automatic and non-automatic PCIVs. Table 3.7-4 provides a listing of all PCIVs, including those listed in Table 3.7-1.
This change provides clarification and does not affect probabilities or consequences of analyzed accidents or margins of safety. No new accident types are created.
j Proposed Change 2:
The second proposed change would delete the reference to Table 3.7-1 from
, Technical Specification 3.7.D.1. This Specification presently requires that
"...all primary containment isolation valves listed in Table 3.7-1...shall be
~
operable..." Removal of the reference results in a requirement that all PCIVs (including those not listed in Table 3.7-1) shall be operable. As explained above, Table 3.7-1 merely provides a subset of PCIVs subject to additional surveillance requirements per Specification 4.7.D.l.a and is not intended to be a complete listing of all PCIVs.
1 0467C
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Georgia Power k m ENCLOSURE 1 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS BASIS FOR CHANGE REQUEST This conservative change represents an additional requirement and does not affect probabilities or consequences of analyzed accidents or margins of safety. No new accident types are created.
Proposed Change 3:
It is proposed to delete check valves from Table 3.7-1. Again, Table 3.7-1 is for surveillance of automatic PCIVs which receive a primary containment isolation signal. No automatic actuation, closure time, or any other surveillances are involved for the presently listed check valves; therefore, their appearance in Table 3.7-1 is superfluous.
This change provides clarification and does not affect probabilities or consequences of analyzed accidents or margins of safety. No new accident types are created.
Proposed Change 4:
Additional valves are proposed for inclusion in Table 3.7-1. These valves are added as a result of a comprehensive review of automatic PCIVs performed by GPC with assistance from the Architect / Engineer. Certain of thene valves have been added to the plant due to design changes. Our review identified other valves which meet the criteria for inclusion in Table 3.7-1 but have not previously been listed in the table. These valves are now proposed for addition to the table. For the Hydrogen /0xygen analyzer system, the previous single designation for the entire system has been replaced with a listing of all individual PCIVs and their normal and accident positions.
No valves are proposed for deletion by change number 4 Since all proposed changes represent additions to the table and additional Technical Specifications requirements, these changes are clearly conservative.
Probabilities and consequences of analyzed accidents are not increased.
Margins of safety are not decreased. No new accident types are created.
Proposed Change 5:
Changes are proposed for descriptive information associated with Table 3.7-1. Our review has identified inaccuracies in the " normal position" and
" action on initiating signal" designations for several valves listed in 2
0467C 700775
Georgia Powerkh ENCLOSURE 1 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS BASIS FOR CHANGE REQUEST the table. Changes are proposed to correct these. The proposed changes do not represent changes to PCIV operation or configuration, but correct the Technical Specifications to accurately reflect actual plant conditions.
Under Specification 4.7.D.1.c(1), valves whose normal positions are changed from closed to open will require once per quarter cycling. Yalves whose normal positions are changed from closed to open will be removed from the requirement for quarterly cycling. This change is appropriate, since the actual normal valve position is closed, and the accident position is closed.
Additionally, certain signals initiating group isolations are added to the Hotes for Table 3.7-1.
l These changes correct errors or omissions in the current Technical Specifications and do not affect plant operation. These changes have no effect on probabilities or consequences of analyzed accidents or margins of safety. No new accident types are created, l
Proposed Change 6:
Table 3.7-4, " Primary Containment Testable Isolation Valves," provides a listing of PCIVs subject to leak rate testing under the provisions of 10 CFR 50 Appendix J. A review of leak rate testing and Inservice Inspection procedures versus this table has been performed. To correct erroneous listings, additions and deletions to valve listings, as well as changes to I descriptive information and notes pertaining to this table, are in order.
It is proposed to correct the valve listings for valves 821-F010A and B, B21-FD 9, B21-F020, B21-F031 A and B, P33-F003, P33-F0ll, P33-F004, P33-F012, Ell-F016B, P70-F002, and P70-F003 These valves have been listed beside the wrong penetration numbers. The proposed change would move the listings to the correct penetration numbers. Yalve B21-F019 was incorrectly listed beside two penetration numbers. The incorrect listing would be deleted.
This proposed change corrects inaccurate information to correspond to actual plant conditions. No changes in plant operation are involved. This change does not increase probabilities or consequences of analyzed accidents.
Margins of safety are not affected. No new accident types are created. !
Proposed Change 7:
Plant modifications underway in the current maintenance / refueling outage have resul ted in changes to the Notes associated with Table 3.7-4 These modifications will correct previous problems associated with local leak rate 3
0467C 700775
Georgia Power mk ENCLO5UDE 1 (Continued) f REQUEST TO REVISE PRIMARY CONTAINMENT TALVE LISTING TECHNICAL SPECIFICATIONS BASIS FCR CHANGE REQUEST testing of certain PCIVs in the direction opposite post accident flow.
Because of the configuration of these valves within their respective systems, they could not be pressurized and tested in their isolation direction.
Design modifications, including the installation of blocking valves and test connections between the affected valves and the penetration, will now allow these valves to be tested in the isolation direction. Therefore, the Notes for Table 3.7-4 corresponding to these valves have been changed to indicate the method of testing. The revised method of testing meets applicable criteria per 10 CFR 50 Appendix J.
This proposed change does not affect accident probabilities or consequences.
Plant operation is not affected. The revised valve testing methods will more realistically model post accident conditions. Margins of safety are not affected. No new accident types are created.
Proposed Change 8:
l It is proposed that 72 valves be added to Table 3.7-4 As stated above, GPC has performed a comprehensive review of leak rate testing requirements. This review has identified a large number of valves currently listed in plant leak rate test procedures which do not appear in Table 3.7-4 In some cases the valves have been added as a result of plant modifications. In other cases the valves have never appeared in the table even though they are leak rate tested.
Addition of the valves to the Technical Specifications is a conservative change to allow the Technical Specifications to reflect plant leak rate test )
procedures. No changes to plant operation are involved. Probabilities and consequences of analyzed accidents are not affected. !!argins of safety are not affected. No new accident types are created.
Proposed Change 9 GPC's review of leak rate testing procedures and requirements has identified 26 valves presently listed in Table 3.7-4 which should n require leak rate testing. Valves so identified are proposed for deletto.. from Table 3.7-4 Each valve proposed for deletion, and its associated justification, follow:
Yalve G31-F042 is located downstream of two leak rate tested PCIVs, B21-F010A (p esently listed in Table 3.7-4) and G31-F039 (proposed for addition to ')ble 3.7-4).
4 0467C mm
0@@m sh ENCLOSURE 1 (Continued)
REQUEST TO REVISE PRDtARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS BASIS FOR CHANGE REQUEST Valve C11-F086 is a manual, normally open valve which serves no containment isolation function. This valve number was originally assigned to a PCIV. However, plant modifications have resulted in removal of the original valve and, subsequently, reassigned valve number Cll-F086 to another valve which perfoms no containment isolation function.
Valve C11-F083 is located downstream of two leak rate tested PCIVs, B21-F010A (presently listed in Table 3.7-4) and G31-F039 (proposed for addition to Table 3.7-4).
Yalves Ell-F021A and B do receive isolation signals; however, these valves are not considered the primary isolation boundary. Yalves E11-F019A and B and a cl osed system outside containment provide the correct isolation boundary. This is in agreement with the Inservice Inspection (ISI) plan.
Yalves E11-F065A, B, C, and D are nomally open, fail open, maintenance isolation valves. Containment isolation for these penetrations (X-205A, B, C, D) is provided, respecti vely, by valves Ell-F030A, B, C, and D (residual heat removal (RHR) suction isolation valves); by valves E11-F004 A, B, C, and D (RHR suction bypass isolation valves); and by a closed syster outside containment. Proposed changes to Table 3.7-4 include the addition of valves E11-F004A, B, C and D.
Yalve P21-F420 is being added in place of valve P21-F406 P21-F420 is the correct isolation valve in If ne with P21-F353 P21-F406 is a capped drain valve.
Yalves E21-F019A and B are normally open, fail open valves which ar, ISI Category "B" valves. (Seal leakage in the closed pos'tfoi is inconsequential for fulfillment of their function. ) Thus, ther valv(s do not serve a containment isolation function.
Valves G11-F007A and B and G11-F008A and B are located on a line which once tied into loop B of the Core Spray system. This line has been capped as part of a design modification. Thus, these valves no longer serve a primary containment isolation function or any other function.
Yalves E41-F007 and E41-F008 are both located downstream of two leak rate tested PCIVs. These PCIVs, B21-F010B and E41-F006, are presently included in Table 3.7-4 5
0467C 700775
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~; e, Georgialbwerh ENCLOSURE 1 (Continued) ,
REQUEST TO REVISE PRIMRY ' CONT $5NMENT; 3 _
VALVE LISTING TECHNICAL SPECIFICATIGNS - / . . ']
~N
BASIS FOR CrtANGE REQU1512 n ;
b
/ .
Valves E51-F012 and eel-F022. ere both located ddwnstream of 'twolleak' ratd:
tested PCIVs. These PCI A , B21-F010A andjE51-F013,' .are presently ~
included in Table 0.7-4 Valves E11-F017A and , Ell-F017B' are not consf riered part of the primary containment isolation ^ boundary. Valves Ell-F015A and Ell-F0158, respectivelf , 2nd a7 closed system outside containment form the containment. isolatiie:pboundary for these lines.
Valves E21 F004A and E21-F004B are not considered part of the primary containment isolation boundary. Valves E21-F005A and Ell-F005B, respectively, -and a closed system outsitte containment form the containment isolation f oundary for these lifies. >
y Valve B21-F020 is aa automatic valve, not' receiving a containment isolation signal, located downstream of other lida esch containing two PCIVs. This valve is located downstream of the'-tie-in' point for four 2-inch lines , which come off the Main Stema .Linas downstream of. the outboard Main Steam Isolation Valves (MSIVs). ' There " a re two PCIVs ~
located in each of these 2-inch lines, s These PCIVs are B21-F022A, B, C, and D (inboard) and B21-F028A, B, C, and D (outboard). Yalve B21-F020 is d .
also located downstream of PCIVs B21-F016 and B21-F019, which are located' in a 3-ir;ch' drain line that is a tie-in for four 2-inch lines coming off the MainDSteam Lines upstream 'of the inboard MSIVs. Thus, for all. '
potential. leakage paths through B?l-F020, two other PCIVs are provided to N form the containment isolation boundary. ,
^
For each of the valves listed above; our review has detcrmined, for the reasons given, that the subject valve is not a PCIY an? should not be subject to Appendix J leakj rate test requi rements. Implementation. of this change will not resul t in increased . probabilities or consequerces -of analyzed "
accidents.
In each case where . deletion of leak rate testics i proposed,-
other valves, or closed systems, meeting all applicable criteria will still; perform the required containment isolation function. No new types of accidents are created. Margin; of safety are not reduced, since the testing program will still. conform to all applicable criteria.
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0467C 700775
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GeorgiaPoker d i ENCLOSURE 2 s
NRC DOCKET 50-321 OPERATING LICENSE DPR-57 EDWIN I. HATCH NUCLEAR PLANT UNIT 1 REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS I
10 CFR 50.92 EVALUATION
+
' Pursuant to 10 CFR 50.92, Georgia Power Company has evaluated the
' . attached proposed amendment for Plant Hatch Unit 1 and has determined that its adoption would not involve a significant hazards consideration. The basis for this determination is as follows:
Proposed Change 1:
This change will modify the title of Table 3.7-1 of the Unit 1 Technical Specifications to clarify the table listings. Specifically, the title would reflect the fact that its listings are for Primary Containment Isolation Valves (PCIVs) that are power operated and automatically initiated.
Basis:
This change is consistent with Iten (i) of the " Examples of Amendments that are Considered Not Likely to Involve Significant Hazards Considerations" listed on page 14,870 of the Federal Register, April 6, 1983. The proposed editorial change is made to achieve clarf fication in the Technical Spacifications and, therefore, meets the requirements of Item (il for an amendment involving no significant hazards considerations, w - This change does not involve a significant increace in the probability or consequences of an accident, because it is editorial and is intended to add clarity to the Technical Specifications.
The possibility of a different kind of accident from any analyzed previously is not created by this change, because plant design and operation are not affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
Proposed Change 2:
This proposed change would delete a reference to Table 3.7-1 from Technical Specification 3.7.D.1. Specifically this Specification presently requires that "...all primary containment isolation valves listed in Table 3.7-1...shall be operabl e. . . " Removal of the reference resul ts in a requirement that all PCIVs (including those not listed in Table 3.7-1) shall be operable.
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ENCLOSURE 2 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS 10 CFR 50.92 EVALUAT10N Basis:
This change is consistent with Item (ii) of the " Examples of Amendments that are Considered Not Likely to Involve Significant Hazards Considerations" listed on page 14,870 of the Federal Register, April 6, 1983 This conservative change represents an additional requirement. Therefore, the change meets the requirements of Item (ii) for an amendment involving no significant hazards considerations.
This change does not involve a significant increase the probability or consequences cf an accident, because it will add to Tesnnical Specifications requirements.
The possibility of a different kind of accident from any analyzed previously is not created by this change, because plant design and operation are not affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
Proposed Change 3:
This proposed change would delete the check valves listed in the Unit 1 Technical Specifications Table 3.7-1. Table 3.7-1 is for surveillance of automatic PCIVs which receive a primary containment isolation signal, and the inclusion of the presently listed check valves in this table is superfluous.
Basis:
This change is consistent with Item (i) of the " Examples of Amendments that are Considered Not Likely to Involve Significant Hazards Considerations" listed on page 14,870 of the Federal Register, April 6,1983 The proposed editorial change is made to achieve clarification in the Technical Specifications and, therefore, meets the requirements of Item (i) for an amendment involving no significant hazards considerations.
This change does not involve a significant increase in the probability or consequences of an accident, because it is editorial and is intended to add clarity to the Technical Specifications. No automatic actuation, closure time, or any other surveillances are involved for the presently listed check valves, and their appearance in Table 3.7-1 is not necessary.
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ENCLOSURE 2 (Continued) l REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS 10 CFR 50.92 EVALUATION l
The possibility of a different kind of accident from any analyzed previously is not created by this change, because plant design and operation are not affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
l
$ Proposed Change 4:
y This proposed change would add additional valves to the listings in Table 3.7-1.
Basis:
The valves proposed for inclusion in Table 3.7-1 are added as a result of a comprehensive review of automatic PCIVs performed by GPC with assistance l from the Architect / Engineer. Certain of these valves have been added to the l plant due to design changes. Our review identified other valves which meet the criteria for inclusion in Table 3.7-1 but have not previously been listed in the table. These valves are now proposed for addition to the table.
This change is consistent with Item (ii) of the " Examples of Amendments that are Considered Not Likely to Involve Significant Hazards Considerations" listed on page 14,870 of the Federal Register, April 6,1983. The proposed change is conservative, since it adds valves to the table and additional Technical Specifications requirements. No valves are proposed for deletion.
This change does not involve a significant increase in the probability or consequences of an accident, because it is conservative in nature and will result in additional Technical Specifications requirements.
{
The possibility of a di f ferent kind of accident from any analyzed previously is not created by this change, because plant design and operation are not affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
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Georgia Powerkh ENCLOSURE 2 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS 10 CFR 50.92 EVALUATION Proposed Change 5:
This change proposes to correct descriptive information associated with Table 3.7-1. Specifically, these changes would correct inaccuracies in the
" normal position" and " action on initiating signal" designations for several valves listed in the table. Additionally, certain signals initiating group isolations are added to the Notes for Table 3.7-1~.
Basis:
This change does not involve a significant increase in the probability or consequences of an accident, because it will correct Technical Specifications to accurately reflect plant conditions. No changes to PCIV operation or configuration are involved.
The possibility of a different kind of accident from any analyzed previously is not created by this change, because plant design and operation are not affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
Proposed Change 6:
This proposed change would modify the Unit 1 Technical Specifications Table 3.7-4, " Primary Containment Testable Isolation Valves." Valve listings and descriptive information for presently listed valves would be changed, as appropriate, to reflect the actual plant design and conditions.
Basis:
The proposed change corrects inaccurate information. No changes in plant operation are involved with this change.
This change is consistent with Item (i) of the " Examples of Amendments that are Considered Not Likely to Involve Significant Hazards Considerations" listed on page 14,870 of the Federal Register, April 6,1983 The proposed editorial change corrects errors and adds clarification to the Technical Specifications and, therefore, meets the requirements of Item (i) for an amendment involving no significant hazards considerations.
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ENCLOSURE 2 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS 10 CFR 50.92 EVALUATION This change does not involve a significant increase in the probability or consequences of an accident, because it is editorial and is intended to accurately reflect plant conditions in the Technical Specifications.
The possibility of a differont kind of accident from any analyzed previously is not created by this change, because plant design and operation will be more clearly reflected in the Technical Specifications.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
Proposed Change 7: l l
This proposed change involves modifications to the notes on local leak rate !
testing of certain PCIVs associated with Table 3.7-4 Applicable testing i criteria specified in 10 CFR 50 Appendix,J are satisfied by the revised notes. '
Basis:
These changes will correct previous problems associated with local leak rate testing of certain PCIVs in the direction opposite post accident flow.
Because of the configuration of these valves within their respective systems, they could not be pressurized and tested in their isolation direction. Design modifications, including the installation of blocking valves and test connections between the affected valves and the penetration, will now allow these valves to be tested in the isolation direction.
Therefore, the Hotes to Table 3.7-4 corresponding to these valves have been changed to indicate the method of testing. The revised method of testing meets applicable criteria per 10 CFR 50 Appendix J.
This change does not involve a significant increase in the probability or consequences of an accident, because it will resul t in Technical Specifications requirements being more consistent with local leak rate testing.
The possibility of a different kind of accident from any analyzed l previously is not created by this change, because plant design and operation l are not affected. '
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
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GeorgiaPowerkh ENCLOSURE 2 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT VALVE LISTING TECHNICAL SPECIFICATIONS O GFR 50.92 EVALUATION Proposed Change 8:
The proposed change would add 71 valves to Table 3.7-4 of the Unit 1 Technical Specifications.
Basis:
The addition of valves to the Technical Specifications is a conservative change enacted after a comprehensive review of leak rate testing requirements. This review has identified a large number of valves currently listed in plant leak rate test procedures which do not appear in Table 3.7-4 In some cases the valves have been added as a resul t of plant modifications. In other cases the valves have never appeared in the Table even though they are leak rate tested.
Addition of the valves to the Technical Specifications is a conservative change to allow the Technical Specifications to reflect plant leak rate test procedures. This change is consistent with Item (ii) of the " Examples of Amendments that are Considered Not Likely to Involve Significant Hazards Considerations" listed on page 14,870 of the Federal Register, April 6, 1983. The proposed change is conservative, since it adds valves to the table and additional Technical Specifications requirements. No valves are proposed for deletion.
This change does not involve a significant increase in the probability or consequences of an accident, because it is conservative in nature and will result in additional Technical Specifications requirements.
The possibility of a different kind of accident from any analyzed previously is not created by this change, because plant design and operation are not affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
Proposed Change 9:
This proposed change would delete 26 valves from Table 3.7-4 These valves proposed for deletion are as follows:
a) Are not automatic PCIVs, b) Do not receive a primary containment isolation signal, c) Are located downstream of two leak rate tested PCIVs or capped lines, or d) Are not considered part of the primary isolation boundary.
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i i
r GeorgiaPowerd ENCLOSURE 2 (Continued)
REQUEST TO REVISE PRIMARY CONTAINMENT j VALVE LISTING TECHNICAL SPECIFICATIONS 10 GFR 50.92 EVALUATION '
l l
l Georgia Power Company's comprehensive review of leak rate testing procedures and requirements resulted in the identification of certain valves which i
should not require leak rate testing. Enclosure 1 details the justification i
for the deletion of each of the 26 valves from Table 3.7-4 This change will not involve a significant increase in the probability or consequences of accident; because for each of the 26 valves, our review has determined that the subject valve is not a PCIV which should be subject to the leak rate test requirements of Table 3.7-4.
The possibility of a different kind of accident from any analyzed previously l is not created by this change, because plant design and operation are not l affected.
Margins of safety are not significantly reduced by this change, because the plant safety analyses are not affected.
l 7
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l GeorgiaPower d ENCLOSURE 3 NRC DOCKET 50-321 OPERATING LICENSE DPR-57 EDWIN I. HATCH NUCLEAR PLANT UNIT 1 ,
REQUEST TO REVISE PRIMARY CONTAINMENT l YALVE LISTING TECHNICAL SPECIFICATIONS PROPOSED CHANGE TO TECHNICAL SPECIFICATIONS The proposed changes to the Technical Specifications (Appendix A to Operating License DPR-57) would be incorporated as follows:
Remove Page Insert Page IX IX 3.7-16 3.7-16 3.7-16a 3.7-17 3.7-17 3.7-18 3.7-18 3.7-18a 3.7-18b 3.7-19 3.7-19 3.7-19a 3.7-23 3.7-23 3.7-24 3.7-24 3.7-25 3.7-25 3.7-26 3.7-26 3.7-26a 3.7-26b 3.7-27 3.7-27 t 1
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