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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3301994-10-0707 October 1994 LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20024J3301994-10-0707 October 1994 LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
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i i ,
! N^RTHEAST UTILMES a nera' = c a sa'
- ut I w sfeSNaIsIen s itUbe:$Ec c moUn7 P.O. BOX 270 EoIna**5' IAEIE*'vS* c"o%p,ny liARTFORD. CONNECTICUT 06141-0270 L 'T' Nstheast Nucioar Ene gy Company (203)665-5000 June 18, 1993 MP-93-488 Re: 10CFR50.73(a)(2)(i)
U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 l
Reference:
Facility Operating License No. NPF-49 i
Docket No. 50-423 Licensee Event Report 93-005-00 Gentlemen: ,
, This letter forwards Licensee Event Report 93-005-00 required to be submitted within l thirty (30) days pursuant to 10CFR50.73(a)(2)(i).
Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY F
mw Stephen E. cace Vice President - Millstone Station SES/JSY:dir l i
i
Attachment:
LER 93-005-00 l cc: T. T. Martin, Region 1 Administrator '
P. D. Swetland, Senior Resident Inspector, Millstone Unit Nos.1, 2 and 3 i V. L. Rooney, NRC Project Manager, Millstone Unit No. 3 l
l l PDR 2300.99 9306280209 930618 ADDCK 05000423 r$ ff '
i I
S PDR e
NRC Form 366 U.S. NUCLEAR REGULATORY COMV:SSION APPROVED OMO NO, 3150-0104 16-89) . ,
EXPi RES. 4/30/92 Estimated burden per response to comply with this
, Information ochection reauest 60.0 nrs. Forward Commeq's regarding buroen estifnate to the Recorcs LICENSEE EVENT REPORT (LER) and Reports Management Branch >$30), U.S Nuclear Reguistory Commission, Wasnington DC 20555 and to ,
. The Paperwork Recucleon Protect (3150-0104), Oftece of Management and Budget Wasnmgtors DC 20503 l DOCNET NUMBER (21 Pa M ' l FACluTY NAME (1)
Millstone Nuclear Power Station Unit 3 ol 51 of ol 01412'l 3 1lOFl0l5 TITLE 44)
Inadequate Overlap Testing EVENT DATE ist M A NUMBF A rei AEPOAT DATE 17) OTHE A F ACluTIE S INVOLVED #8) .
MONTF DAY YEAR YEAR 1 "Y -
MONTH DAY YEAR F AC UTY NAME S of si of of of I- l 0l5 2l0 9 3 9 l3 0l0l5 0l 0 0l6 1l8 9l 3 o,3;o;ogo; ; g.
OPERATING THIS REPORT IS BEING SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR $: (Check one o' more of the fohowing)(11) t 20 402(b) 20 402(c) 50.73(a)(2iov) 73.71(c)
POWER 20.405(altt)Os 50 36tc)D) 60,73(a)(2)(v) 73 71(c) l LE VE, L
- 10 1l0l0 20 405(a)(1Heq 50.36(cH2) 50.73. t a)(2)(vtt) _ gyER ISgf in Text, NRC Form 366A) 20.405(alti)(h4 g 50. 731a)(2 H O 50J3(a)(2Hviii)( A) 20 405(aH t)(tv) 50. 73(a H2)(it) 60. 73(a)(2H va0 (B) 20 405Iat tilfiv) 50. 73(a)(2) UiG 60. 73(a H2 H x)
UCENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Jeffrey S. Young, Engineer, Ext. 6442 2l0]3 4l 4l 7l-l 1l 7l 9l 1 COMPLETE ONE UNE FOR FO COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT hh* m }g l CAUSE SYSTEC COMPONENT NvNf 7y,qos s l I I I I I I 3-- 1 III I I l I II I I I I I II I I I I SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY YEAR 1 EXPECTED I SUBMISSION DATE 05)
YES Of yes, complete EXPECTED SUBMISSION DATE) M NO g g g ABSTRACT ILimit to 14DO spaces. Le , approximately fif teen single-space typewritten hnes) (16)
On May 20,1993 at 1400 with the plant in Mode 1 at 100% the Cold Over Pressure Protection System (COPPS) was declared inoperable due to inadequate surveillance testing. The surveillance requirement is a monthly test of the circuit from the sensor up to but not including valve operation, However, only the portion of the circuit from the sensor to the input relays to Solid State Protection System were tested at this frequency.
The discovery was made by the task force reviewing overlap testing issues. This task force was established as a corrective action to Licensee Event Report 93-003. Four other inadequate surveillance tests were discovered in the next twelve days.
The root cause of the event was a management deficiency in that a comprehensive approach to testing was not implemented during procedure development at plant start up. While the exact circumstances of the inadequate tests were different, they all indicate that unusual conditions were not always considered during procedure development. .A broader overview of testing may.have detected these deficiencies.
The immediate correctise action was to declare the affected component or system inoperable and enter the appropriate Limiting Condition for Operation (LCO) Action Statement. All in service components have been tested to confirm operability.
As action to prevent recurrence, the overlap task force will continue to look for other situations where inadequate testing exists. The task force's charter is to review overlap testing for reactor trip and Engineered Safety Features actuations. In addition, the task force will recommend methods for implementing a l comprehensive approach for ct rent test development. l i
NRO Form 356 (6-89)
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N3c FdNn 3%A . U.S NUCLEAR REGULATORY coMM:SSloN APPROVED oMB ND. 3'50-0104 (6-891 EAPiRES : 4/30'92 Estimated buroen per response to compiy with this LICENSEE EVENT REPORT (LER) fg",,*g",gQ'f*75L,6Sf,,h','o ,[,"n*,"lf,o, TEXT CONTINUATION ano Reports Management Branen tp430), u s Nueiear Aepulatory commission. Wastungton DC 205s5. and to ,
tne Faperwork Recuet,o, Project (315G-0104) < o+0ce of -
Management and Buapet. Washington DC 20s03 F AOfLITY NAME I,) DOCK.ET NUMBER [2) i m NuuBFm to PAGE(31 ,
YEAR "M" Ng *"m 6S
?
4 51illstone Nuclear Power Station ,
Umt 3 0l 5l 0j 0l 0l4 [2 l3 9l3 OF
.0 [ 0l 5 0l0 0l 2 0l5 TEXT 01 more soace is reqwed. use add:tional NRC Form 366A s) (17)
- 1. Descretion of Esent On Alay 20,1993 at 1400 with the plant in Atode 1 at 100c1 power (2250 psia and 587 degrees ,
Fahrenheit), the COPPS was declared inoperable due to inadequate surveillance testing. The Instrument !
& Controls (l&C) department's ANALOG CHANNEL OPERATIONAL TEST (ACOT) covers the circuits between the sensor and input relays to Sohd State Protection System (SSPS). The ACOT is
- performed every 31 days when required. 1&C's operational test of SSPS consists of ACTUATION LOGIC TESTS and A1 ASTER RELAY TESTS on a 62 day schedule. Operations Department performs ^
SLAVE RELAY TESTS which cover slave relays and the circuit up to the actuated device. ~ This test is '
performed quarterly. This is the same method required by Technical Specifications in the Instrumentation Section for Engmeered Safety Features (ESF) functions. However, the Technical . i Specification for the COPPS circuit requires an ACOT up to but excluding valve operation within 31 days i of use and then every 31 days while in use. Therefore, two sections of the circuit were not being tested at the required frequency, On hiay 28,1993 at 1530 with the plant in $1 ode 1 at 100r epower (2250 psia and 587 degrees Fahrenheit), the hiam Steam Line Isolation Engineered Safety Features signal to the hiain Steam isolation Valves (51SIVs) was declared inoperable due to inadequate overlap testing. A slave relay actuates on a hiain Steam Line Isolation signal which causes the interposing relays (see attached drawing) to drop out. This causes the A1SIVs to rapidly close. A block is used to maintain the interposing relay when the slave relay is tested. The interposing relay should be tested on a refuel frequency. This event i was conservatively reported under 10CFR50.72(b)(2)(iii) as a loss of safety function. Further testing demonstrated that a loss of safety function had not occurred. A test was written and performed to I demonstrate operabihty of the Steam Line Isolation signal.
On June 1,1993 at 1400 with the plant in 51 ode 1 at 100ccpower (2250 psia and 587 degrees Fahrenheit) the oserlap task force discovered several loads associated with the Loss Of Power (LOP) load shedding function which were not properly tested. The following conditions were determined to be I inadequately tested:
i the "C" Reactor Plant Component Cooling Water (RPCCW) Pump is a suing pump and can be l powered from either bus. The LOP load shedding function was not tested from either bus during performance of the last 18 month surveillance.
the "C" Service Water Pump (one of two " A" train pumps) load shedding was not tested for an LOP with an ESF actuation during the last 15 month surveillance.
after an actuation signal occurs and is reset with the plant in post Loss of Coolant Accident recirculation to either the hot or cold legs, Charging Pumps in both trains receive a load shed signal and then are sequenced back on. None of these load shedding functions were tested.
In each case, the discovery was made by the task force reviewing overlap testing issues.
- 11. Cause of Event The root cause of these events was a management deficiency. An integrated approach to testing was not put in place during procedure development at plant start up.
COPPS - The ACOT for COPPS was written based on the methodology used for ESF testing and as described in the FSAR for COPPS. The conflict between the FSAR and Technical Specification requirements was not previously identified.
Wili""'
Nac Form 366A , U.S NUCLEAR REGULAToAY COMMISSION APPROVED oMB NO. 3150-01D4 t6-89) EXPIRE S. C30/92 Estimated butaen per respor se to comoty with thes LlCENSEE EVENT REPORT (LER) f'o"","ty,co;*c}**
, ,, '*%5,3,0,,"',5, ,l7s*,"cy,c, TEXT CONTINUATION and Reports Management Branch m-530L U S. Nuclear Regulatory Comm:ssion. Wasnington De ?C5Es. and to tne Pawwon Aeduction Pwatt (315".~0104 ; Office of ,
Management anc Buapet. Washincton DC 20503 i F ACILITV N AME (1) DOCKET NUMBER (21 ( F A N(MRrA @ PAGE (3)
YEAA E .
d j
Niillstone Nuclear Power Station U"" 3 0l 5l 0l 0l 0l4 l2 l3 9l3 0l 0l 5 0l0 0l 3 OF 0l5 TEXT Pf more space es reou' red use and tiona' NRO Form 366A si 117)
MSIVs - the test did not require positionmg of the MSIVs while shutdown during the 18 month surveillance.
LOP load shedding - the test did not ensure that all combinations of load shedding were properly performed.
111. Anah sis of Event These events are being reported in accordance with 10CFR50.73(a)(2)(i) as a condition prohibited by Technical Specifications. In each case, the surveillance procedures did not adecuately implement surveillance requirements. The inadequate surveillance for the MSIVs was conservatively reported under 10CFR50.72(b)(2)(iii) as a loss of safety function. Further testing determined that a loss of safety function had not occurred.
COPPS - Surveillance requirement 4.4.9.3.1 (Overpressure Protection) requires an ACOT on the Power Operated Relief Valve (PORY) actuation channel, but excludmg valve operation within 31 days prior to entenng a condition m which the PORV is required to be OPERABLE. The surveillance procedure was consistent with other ACOTs and therefore, did not include SSPS logic or output relay testing. The remainder of the circuit is properly tested by ACTUATION LOGIC TESTS and SLAVE RELAY TESTS l but not at the required monthly frequency.
This deficiency had minimal safety significance. There have been no test failures of the monthly )
L suneillance as performed. There have been no failures of the bimonthly test of the SSPS circuitry for ;
the PORVs as part of the COPPS. There have been no failures of the quarterly slave relay testing for l l PORY actuation as part of COPPS. Therefore, the circuit can reasonably be expected to have ,
l functioned properly if challenged. l MSlY - Suneillance requirement 4.3.2.1 (Engineered Safety Features Actuation System - ESFAS) requires CHANNEL CAllBRATION every 18 months of the Main Steam Line Isolation signal. The suneillance procedure covered the circuit from sensor to output of the slave relays but did not test the interposing relay and its associated contacts.
This deficiency had mmimal safety significance. The circuit has an interposing relay from each safety l train, either of which will cause the MSIVs to close. In addition, each relay has two series contacts, l
either of which will cause the MSlVs to close. Finally, several Steam Line Isolation events have occurred on the unit, all MSIVs closed properly. The interposing relays were tested and performed satisfactorily.
l LOP load shedding - Surveillance requirement 4.S.1.1.2 g.4 (AC Sources) requires 18 month verification of load shedding for a simulated LOP and surveillance requirement 4.8.1.1.2.g.6 requires 18 month verification of load shedding for a simulated LOP in conjunction with an ESF actuation.
l l This event has minimal safety significance. The condition for which the Charging Pumps were not tested l
(LOP occurs with the plant in the recirculation mode) is a post accident condition. In addition, all Charging Pumps presently in service have now been tested satisfactorily. The "C" Service Water Pump was tested satisfactorily, and therefore would have been shed if required. The "C" RPCCW pump has been tested satisfactorily on the train to which it is aligned and will be tested on the other train in the near future. Additionally, start up testing demonstrated that the Emergency Diesel Generators were capable of sustaining higher initial loadmg conditions without tripping.
The safety significance of all deficiencies is further minimited by the fact that similar circuitry is used through out the plant and has no record of failures. Therefore, portions of circuits which have not been tested can reasonably be expected to have operated properly if challenged.
gorm we
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NRC Form 366A
- U S. NUCLEAR REoVLATORY COMMISSION APmROVED OMB fJO. 3160-0104 (6-89) EXPfRE S: 4/30/92
. Estimat d ourcen per respons. to compiy witn this LO O ** F "* *'d LICENSEE EVENT REPORT (LER) c'nt* mater omm.nts r ce*ctan ~5t:
TEXT CONTINUATION ana R. port,egaroing euro.n estimat. to in. Recoras uananment eramn in-sao). u.s Naci r
- Regulatory Commissvin, Wasriangton DC 20556 and to the Paperwork Reduction Prciect (3150-01041 Offic. of Manao.mor.1 ano suco.t wasninoton oc 2osca FActUTY NAME 0) DOCKET NUMBER (2) i rn NUMRf A H;t PAGE (31 YEAR NN asm mam Millstone Nuclear Power Station Unit 3 Oj 4 OF 0l 5l 0l 0l 0l4 l2 l3 9l3 0 l 0l 5 0l0 0l5 TEXT (ff more spac. is reouw.c us. adattional NRC Form 366A s1 (17)
IV. Corrective Action immediate corrective action was to declarc the affected components inoperable and enter the appropriate -l LCO Action Statement, All in semce components were tested and restored to OPERABLE status. ;
As action to prevent recurrence, the following actions are being taken:
the task force will continue to review procedures associated with reactor trip and ESF to determine >
if any similar conditions exist.
- the task force will make recommendations to unit management on methods to implement a ;
comprehensive approach to testing. ;
l The series of tests which satisfies the surveillance requirements for COPPS will be performed prior to
! declaring the system operable. The surveillance procedures are being revised for clarity of -
requirements.
l a change to the FSAR regarding test methodology for COPPS will be investigated.
V. Addinonal Inferm ition l l
l Other Licensee Event Reports (LERs) which have been submitted where portions 01 circuits have not ,
been properly tested due to inadequate procedures are as follows 1 l i LER Number Title 93-003 Inadequate Testmg of Slave Relays93-001 Failure to Verify Testing of NIS Inputs Into Westinghouse 7300 Process Control System Due to Procedural Deficiency 92-031 Failure io Test High Pressure Output Relay for Power Operated Relief Valves Due to Procedural Dehciency 91-025 Failure to Verify De-energitation of Solid State Protection input Relays for Cold Overpressure Protection Due to Procedural Deficiency l
l 91-022 Failure to Adequately Perform Overlap Testing of the Containment l Depressurization Actuation Loops Due to Management Deficiency 90-007 Inadequate Load Shed Verification
~
l 87-042 Missed Intermediate Range / Power Range Surveillance Due to Procedural Inadequacy Prior to LER 93-003, procedural deficiencies were addressed as individual events. As a result of LER 93-003 a task force was formed to apply an integrated approach to slave relay testing. The deficiencies noted in the current LER are a result of this review.
Ells codes Systemji Comoonent Engineered Safety Relay - RLY Features Actuation System - JE I$EaI"""
NRC F9rm 366A . U S NUCLEAR REGULATORY COMM:SSION APPROVED OMB NO. 3tSO-0104 (4-89) ,
EXPIRE S: 4/30/92 Estimated buroen per rerponse to comply with this
'n' 'm*'*" co"*ct *" 'covest ; 5 . 0 hrs, Forward LICENSEE EVENT REPORT (LER) Comments regarding bur den estimate to the ROCoros TEXT CONTINUATION and Reporte uan oernent Branen in-530), U S. Nuclear Aeguiatory Commassen. Washington DC 20555. and to the Paperwork Reduction Project (315'J-0104). Oftsce of Manape rent and Buopet Wasntngton. DC 20503 FACIUTY NAME (1) DOCKET NUMBER (2) [F A NUM9gq pp, PAGE (3) l N
YEAR Nmus"ca maEn '
Millstone Nuclear Power Station Unit 3 - -
ol 5l 0l ol ol4 l2 l3 9l3 0l 0l 5 0l0 0l 5 OF 0l5 TEXT (N more space is requered. use moditonal NRC Form 366A's) (17)
Blocking .
r Relay ,, / Steam Line Contact _' Is lation Slave Relay Contact l , . . . . . ' Interposing Relay
, Associated Contact t
l l '
( '
MSIV solenoid Interposing (Typical) j Relay l
Simplified MSIV Circuit ,
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l j.- NHC Form 366 r ts-89)
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