ML18101A548

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Monthly Operating Rept for Jan 1995 for Salem Unit 2
ML18101A548
Person / Time
Site: Salem PSEG icon.png
Issue date: 01/31/1995
From: Morroni M
Public Service Enterprise Group
To:
Shared Package
ML18101A545 List:
References
NUDOCS 9502210277
Download: ML18101A548 (10)


Text

~RAGE DAILY UNIT POWER LE. .

Docket No.: 50-311 Unit Name: Salem #2 Date: 02-10-95 Completed by: Mike Morroni Telephone: 339-2122 Month January 1995 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 0 16 0 P. 8.1-7 Rl

( 9502210277 950214 I PDR ADOCK 05000311 R PDR

~ OPERATING DATA REPORT ~

Docket No: 50-311 Date: 02/10/95 Completed. by: Mike Morroni Telephone: 339-2122 Operating Status

1. Unit Name Salem No. 2 Notes
2. Reporting Period January 1995
3. Licensed Thermal Power (MWt) 3411
4. Nameplate Rating (Gross MWe) 1170
5. Design Electrical Rating (Net MWe) 1115
6. Maximum Dependable Capacity(Gross MWe) 1149
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA
9. Power Level to Which Restricted, if any (Net MWe) NIA
10. Reasons for Restrictions, if any ~~~~N~A=--~~~~~~~~~~~~~~-

This Month Year to Date Cumulative

11. Hours in Reporting Period 744 744 116617
12. No. of Hrs. Rx. was Critical 0 0 75615.2
13. Reactor Reserve Shutdown Hrs~ 0 0 0
14. Hours Generator On-Line 0 0 72967.9
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 0 0 180973784.2 Gross Elec. Energy Generated (MWH) 0 0 76450008
18. Net Elec. Energy Gen. (MWH) -17867 -17867 72705677
19. Unit Service Factor 0 0 62.6
20. Unit Availability Factor 0 0 62.6
21. Unit Capacity Factor (using MDC Net) 0 0 56.4
22. Unit Capacity Factor (using DER Net) 0 0 55.9
23. Unit Forced Outage Rate 0 0 21. 8
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

We are presently in a maintenance outage.

25. If shutdown at end of Report Period, Estimated Date of Startup:

2 12 95.

8-1-7.R2

UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH JANUARY 1995 DOCKET NO.: -'5::..:0:....-..::.27:....:2=-----

UNIT NAME: Salem #2 DATE: 2-10-95 COMPLETED BY: Mike Morroni TELEPHONE: 339-5142 METHOD OF SHUTTING LICENSE L DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # CODE 4 CODE 5 TO PREVENT RECURRENCE 2078 1-1-95 s 744 c 4 -------- RC FUELXX NORMAL REFUELING 1 2 3 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report CLER) File D-Requlatory Restriction 4-Continuation of CNUREG-0161)

E-Operator Training & License Examination Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)

10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 DATE: 02/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.

1. Design Change Packages (DCP) 2EX-2139, Pkg. 1 "Temporary Load Balance Test for 2PR5 Discharge Piping" Rev. 0 - The objectives of this test are to record data and ascertain the impact of the variation in discharge piping loading upon 2PR5 seat leakage at NOP/NOT conditions.

These results will be used to provide a basis for a potential future design change to piping supports so that discharge nozzle loads at the PR 3, 4 and 5 valves are minimized with the end result of achieving their task leak tight operation.

All of the conclusions of the UFSAR Chapter 15 licensing basis safety analysis remain valid and thus the margin of safety is not reduced. The pressurizer safety valves (2PR3, 4 &5) will be operable with the required lift setpoints along with the PORVs (2PR1 & 2) during the Mode 3 operation.

(SORC 95-002) 2EE-0077, Pkg. 1 "2PR 3, 4 and 5 Valve Bonnet Leak-Off Line Elimination" Rev. 0 - The proposed modification entails decoupling the 3/4" valve bonnet leak-off lines from the valve bonnets on the Pressurizer Safety Relie(Valves 2PR3, 4 and 5. The purpose of this change is to alleviate the potential for inducing stresses from the leak-off piping system into the valve bonnets/bodies. Operability of the Pressurizer Safety Relief valves is required by Technical Specifications to provide RCS overpressure protection. The proposed modification represents only a minor configuration change to enhance the long term reliability of the safety relief valves. Since the vent path from the valve bonnets remains unchanged, the design function of the Pressurizer Safety Relief Valves is not affected. There will be no impact on

10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM 2 DATE: 02/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 the margin of safety as defined in the basis for any Technical Specification. (SORC 95-004)

2. Temporary Modifications (T-Mods)95-005 "Pressurizer Safety Relief Valve Piping Instrumentation" Rev. 0 - The purpose of this T-Mod is to provide instrumentation (displacement transducers, strain gauges, thermocouples) downstream of the discharge flanges of valves 2PR3, 4 and 5 and recording system response using a separate, dedicated data acquisition system. The acceptance criteria for design basis accidents will continue to be met, and the existing margins of safety established by UFSAR safety analyses will not be affected. This proposal will not exceed the design limits of any systems, components or structures. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.

(SORC 95-004)95-013 "2SJ7, Cut and Cap Piping Downstream of Valve to Eliminate Leakage" Rev. 0 - The purpose of this T-Mod is to cut and cap the piping downstream of valve 2SJ7 to eliminate leakage. This will eliminate the contribution of this piping to the unidentified RCS leak rates. The proposed change does not affect the operability or availability of the Emergency Core Cooling System (ECCS) subsystem or the ECCS in general. The piping integrity is still maintained. The acceptance criteria for design basis accidents will continue to be met, and the existing margin of safety as defined by the Technical Specifications will not be affected. (SORC 95-012)

10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 SUPPLEMENT DATE: 02/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed .and concurs with these evaluations.

1. Design change Packages 2EC-3025, Pkg. 1 New Operator's Ready Room" Rev. 0 - The purpose of this design change is to convert an existing janitors closet and maintenance room at elevation 122' -0" in the Unit 2 auxiliary Building into a new Operators Ready Room.

These changes do not affect the allowable design limits addressed in the Technical Specifications. The Control Area Air Conditioning System (CAACS) multipurpose system is not discussed in either the Unit 1 or Unit 2 Technical Specifications and the changes involved do not conflict with or have any bearing on the Emergency Air Conditioning System or the Control Room pressure requirements. The changes to the fire detection system do not affect the bases for fire detection instrumentation addressed in the Technical Specifications. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 90-153) 2SA-00101, Pkg. 1 "Chilled Water and Service Water Update" Rev. 0 - This as-built DCP updates service water and chilled water drawings to bring them into conformance with the actual plant design. Discrepancies were found in an SRG HVAC review documented in NSR REC SRGC 87-084, Task 36 and 37 dated 8/21/87. This DCP will make a number of reference changes in order to add consistency between the drawings and make the drawings easier to read; document removal of analog temperature devices and change component ID for temperature test connections which exist

10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM 2 SUPPLEMENT DATE: 02/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 (Cont'd) in the field but were not documented on the P&ID drawings or instrument schematics; and will document the removal of air regulators which did not exist in field. The proposal does not reduce the margin of safety as defined in the bases for any Technical Specification since the changes documented in this DCP are not described in the Salem Technical Specifications. The changes which are documented in this DCP are sound engineering changes and serve only to increase the overall margin of safety since the design is better. (SORC 90-03 5)

2. Temporary Modifications (T-Mods)90-105 "Ductwork Access Door Modifications" Rev. 0 - This T-Mod allows the opening of an access door on the riser to provide for redirection of air from the Containment Ring Duct, for personnel safety and comfort during work on the 22 Containment Fan Coil Unit (CFCU) motor replacement.

This T-Mod also allows for installation ofherculite over the scaffolding to form a tent. This T-Mod does not impact the operability of any of the CFCUs. The safety function of the system is unchanged and unaffected by the installation of this T-Mod. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.

(SORC 90-130)

REFUELING INFORMATION

  • DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 DATE: 02/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 MONTH: JANUARY 1995
1. Refueling information has changed from last month: YESJ_NO _ _
2. Scheduled date for next refueling: October 14. 1994
3. Scheduled date for restart following refueling: February 14. 1995
4. a. Will Technical Specification changes or other license amendments be required?

YES NO ____x_

NOT DETERMINED TO DATE - -

b. Has the reload fuel design been reviewed by the Station Operating Review Committee?

YES_X_NO If no, when is it scheduled?

5. Scheduled date(s) for submitting proposed licensing action: ---~N~/~A.......__ __
6. Important licensing considerations associated with refueling:
7. Number ofFuel Assemblies:
a. Incore 193
b. In Spent Fuel Storage 556
8. Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632
9. Date oflast refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: March2012 8-l-7.R4

SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

- UNIT 2 JANUARY 1995 SALEM UNIT NO. 2 The Unit remained shutdown throughout the entire period as the 2R8 Refueling Outage activities continued.

PORV & SAFETY VALVE ACTUATIONS

  • DOCKET NO:
  • 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 DATE: 02/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162

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PRESSURIZER OVERPRESSURE PROTECTION SYSTEM ACTUATION On January 25, 1995, upon securing the only operating Reactor Coolant Pump (RCP), the Pressurizer Overpressure Protection System (POPS) actuated. The POPS sensed an apparent pressure increase (or spike) when No. 21 RCP was secured. Reactor Coolant System temperature was at l 80°F and a pressure of 350 psig when the POPS actuated. The setpoint for the POPS relief valves (PRl

& PR2) is 375 psig. Both valves were open for about 20 to 30 seconds. RCS pressure was being maintained by a bubble in the Pressurizer. No change was seen in the pressurizer level or any increase in the Pressurizer Relief Tank (PRT) level.

Wide range reactor coolant pressure indication increased from 350 psig to 368 psig after No. 21 RCP was secured.