Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
~RAGE DAILY UNIT POWER LE. .
Docket No.: 50-311 Unit Name: Salem #2 Date: 02-10-95 Completed by: Mike Morroni Telephone: 339-2122 Month January 1995 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 0 16 0 P. 8.1-7 Rl
( 9502210277 950214 I PDR ADOCK 05000311 R PDR
~ OPERATING DATA REPORT ~
Docket No: 50-311 Date: 02/10/95 Completed. by: Mike Morroni Telephone: 339-2122 Operating Status
- 1. Unit Name Salem No. 2 Notes
- 2. Reporting Period January 1995
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating (Gross MWe) 1170
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity(Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA
- 9. Power Level to Which Restricted, if any (Net MWe) NIA
- 10. Reasons for Restrictions, if any ~~~~N~A=--~~~~~~~~~~~~~~-
This Month Year to Date Cumulative
- 11. Hours in Reporting Period 744 744 116617
- 12. No. of Hrs. Rx. was Critical 0 0 75615.2
- 13. Reactor Reserve Shutdown Hrs~ 0 0 0
- 14. Hours Generator On-Line 0 0 72967.9
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 0 0 180973784.2 Gross Elec. Energy Generated (MWH) 0 0 76450008
- 18. Net Elec. Energy Gen. (MWH) -17867 -17867 72705677
- 19. Unit Service Factor 0 0 62.6
- 20. Unit Availability Factor 0 0 62.6
- 21. Unit Capacity Factor (using MDC Net) 0 0 56.4
- 22. Unit Capacity Factor (using DER Net) 0 0 55.9
- 23. Unit Forced Outage Rate 0 0 21. 8
- 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
We are presently in a maintenance outage.
- 25. If shutdown at end of Report Period, Estimated Date of Startup:
2 12 95.
8-1-7.R2
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH JANUARY 1995 DOCKET NO.: -'5::..:0:....-..::.27:....:2=-----
UNIT NAME: Salem #2 DATE: 2-10-95 COMPLETED BY: Mike Morroni TELEPHONE: 339-5142 METHOD OF SHUTTING LICENSE L DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # CODE 4 CODE 5 TO PREVENT RECURRENCE 2078 1-1-95 s 744 c 4 -------- RC FUELXX NORMAL REFUELING 1 2 3 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report CLER) File D-Requlatory Restriction 4-Continuation of CNUREG-0161)
E-Operator Training & License Examination Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)
10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 DATE: 02/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP) 2EX-2139, Pkg. 1 "Temporary Load Balance Test for 2PR5 Discharge Piping" Rev. 0 - The objectives of this test are to record data and ascertain the impact of the variation in discharge piping loading upon 2PR5 seat leakage at NOP/NOT conditions.
These results will be used to provide a basis for a potential future design change to piping supports so that discharge nozzle loads at the PR 3, 4 and 5 valves are minimized with the end result of achieving their task leak tight operation.
All of the conclusions of the UFSAR Chapter 15 licensing basis safety analysis remain valid and thus the margin of safety is not reduced. The pressurizer safety valves (2PR3, 4 &5) will be operable with the required lift setpoints along with the PORVs (2PR1 & 2) during the Mode 3 operation.
(SORC 95-002) 2EE-0077, Pkg. 1 "2PR 3, 4 and 5 Valve Bonnet Leak-Off Line Elimination" Rev. 0 - The proposed modification entails decoupling the 3/4" valve bonnet leak-off lines from the valve bonnets on the Pressurizer Safety Relie(Valves 2PR3, 4 and 5. The purpose of this change is to alleviate the potential for inducing stresses from the leak-off piping system into the valve bonnets/bodies. Operability of the Pressurizer Safety Relief valves is required by Technical Specifications to provide RCS overpressure protection. The proposed modification represents only a minor configuration change to enhance the long term reliability of the safety relief valves. Since the vent path from the valve bonnets remains unchanged, the design function of the Pressurizer Safety Relief Valves is not affected. There will be no impact on
10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM 2 DATE: 02/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 the margin of safety as defined in the basis for any Technical Specification. (SORC 95-004)
- 2. Temporary Modifications (T-Mods)95-005 "Pressurizer Safety Relief Valve Piping Instrumentation" Rev. 0 - The purpose of this T-Mod is to provide instrumentation (displacement transducers, strain gauges, thermocouples) downstream of the discharge flanges of valves 2PR3, 4 and 5 and recording system response using a separate, dedicated data acquisition system. The acceptance criteria for design basis accidents will continue to be met, and the existing margins of safety established by UFSAR safety analyses will not be affected. This proposal will not exceed the design limits of any systems, components or structures. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 95-004)95-013 "2SJ7, Cut and Cap Piping Downstream of Valve to Eliminate Leakage" Rev. 0 - The purpose of this T-Mod is to cut and cap the piping downstream of valve 2SJ7 to eliminate leakage. This will eliminate the contribution of this piping to the unidentified RCS leak rates. The proposed change does not affect the operability or availability of the Emergency Core Cooling System (ECCS) subsystem or the ECCS in general. The piping integrity is still maintained. The acceptance criteria for design basis accidents will continue to be met, and the existing margin of safety as defined by the Technical Specifications will not be affected. (SORC 95-012)
10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 SUPPLEMENT DATE: 02/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed .and concurs with these evaluations.
- 1. Design change Packages 2EC-3025, Pkg. 1 New Operator's Ready Room" Rev. 0 - The purpose of this design change is to convert an existing janitors closet and maintenance room at elevation 122' -0" in the Unit 2 auxiliary Building into a new Operators Ready Room.
These changes do not affect the allowable design limits addressed in the Technical Specifications. The Control Area Air Conditioning System (CAACS) multipurpose system is not discussed in either the Unit 1 or Unit 2 Technical Specifications and the changes involved do not conflict with or have any bearing on the Emergency Air Conditioning System or the Control Room pressure requirements. The changes to the fire detection system do not affect the bases for fire detection instrumentation addressed in the Technical Specifications. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 90-153) 2SA-00101, Pkg. 1 "Chilled Water and Service Water Update" Rev. 0 - This as-built DCP updates service water and chilled water drawings to bring them into conformance with the actual plant design. Discrepancies were found in an SRG HVAC review documented in NSR REC SRGC 87-084, Task 36 and 37 dated 8/21/87. This DCP will make a number of reference changes in order to add consistency between the drawings and make the drawings easier to read; document removal of analog temperature devices and change component ID for temperature test connections which exist
10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM 2 SUPPLEMENT DATE: 02/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 (Cont'd) in the field but were not documented on the P&ID drawings or instrument schematics; and will document the removal of air regulators which did not exist in field. The proposal does not reduce the margin of safety as defined in the bases for any Technical Specification since the changes documented in this DCP are not described in the Salem Technical Specifications. The changes which are documented in this DCP are sound engineering changes and serve only to increase the overall margin of safety since the design is better. (SORC 90-03 5)
- 2. Temporary Modifications (T-Mods)90-105 "Ductwork Access Door Modifications" Rev. 0 - This T-Mod allows the opening of an access door on the riser to provide for redirection of air from the Containment Ring Duct, for personnel safety and comfort during work on the 22 Containment Fan Coil Unit (CFCU) motor replacement.
This T-Mod also allows for installation ofherculite over the scaffolding to form a tent. This T-Mod does not impact the operability of any of the CFCUs. The safety function of the system is unchanged and unaffected by the installation of this T-Mod. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 90-130)
REFUELING INFORMATION
- DOCKET NO: 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 DATE: 02/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 MONTH: JANUARY 1995
- 1. Refueling information has changed from last month: YESJ_NO _ _
- 2. Scheduled date for next refueling: October 14. 1994
- 3. Scheduled date for restart following refueling: February 14. 1995
- 4. a. Will Technical Specification changes or other license amendments be required?
YES NO ____x_
NOT DETERMINED TO DATE - -
- b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES_X_NO If no, when is it scheduled?
- 5. Scheduled date(s) for submitting proposed licensing action: ---~N~/~A.......__ __
- 6. Important licensing considerations associated with refueling:
- 7. Number ofFuel Assemblies:
- a. Incore 193
- b. In Spent Fuel Storage 556
- 8. Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632
- 9. Date oflast refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: March2012 8-l-7.R4
SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
- UNIT 2 JANUARY 1995 SALEM UNIT NO. 2 The Unit remained shutdown throughout the entire period as the 2R8 Refueling Outage activities continued.
PORV & SAFETY VALVE ACTUATIONS
- 50-311 MONTH: JANUARY 1995 UNIT NAME: SALEM2 DATE: 02/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162
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PRESSURIZER OVERPRESSURE PROTECTION SYSTEM ACTUATION On January 25, 1995, upon securing the only operating Reactor Coolant Pump (RCP), the Pressurizer Overpressure Protection System (POPS) actuated. The POPS sensed an apparent pressure increase (or spike) when No. 21 RCP was secured. Reactor Coolant System temperature was at l 80°F and a pressure of 350 psig when the POPS actuated. The setpoint for the POPS relief valves (PRl
& PR2) is 375 psig. Both valves were open for about 20 to 30 seconds. RCS pressure was being maintained by a bubble in the Pressurizer. No change was seen in the pressurizer level or any increase in the Pressurizer Relief Tank (PRT) level.
Wide range reactor coolant pressure indication increased from 350 psig to 368 psig after No. 21 RCP was secured.